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37-105-20383

Well Details

Well ID: 37-105-20383
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Country: United States
State: Pennsylvania
County: Potter
Municipality: Stewardson Township
Operator Name:
Well Pad ID:
Farm/Lease Name: PA DEPT OF W&F TRACT #58 RW-66
License Status: PLUGGED & ABANDONED
Spud Date:
Permit Date: 1998-01-27
Well Type: STORAGE WELL
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 41.512976
Longitude: -77.676851

For data sources see[1][2][3]

Well History

Date Event
1971-04-20 Performed Spud Operation
1971-05-27 Perforation
1971-06-04 Drilling Completion
1971-11-03 NEWLY DRILLED
1998-01-27 New Permit Application
2014-09-24 Begin Plugging
2014-10-24 Drilling Completion
2014-10-24 Finished Plugging
2015-09-02 FULLY PLUGGED
2018-07-31 Begin Plugging
2018-11-06 Finished Plugging

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2003 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2006 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2007 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2008 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2009 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2010 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2011 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2012 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2013 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2014 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0
2018 DOMINION ENERGY TRANS INC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2018 DOMINION ENERGY TRANS INC Servicing Fluid 325.20 Tons RESIDUAL WASTE PROCESSING FACILITY WMGR123
2018 DOMINION ENERGY TRANS INC Other Oil & Gas Wastes 18.90 Tons RESIDUAL WASTE PROCESSING FACILITY WMGR123
2018 DOMINION ENERGY TRANS INC Other Oil & Gas Wastes 23.10 Tons RESIDUAL WASTE PROCESSING FACILITY WMGR123SW019
2018 DOMINION ENERGY TRANS INC Other Oil & Gas Wastes 83.80 Tons RESIDUAL WASTE PROCESSING FACILITY WMGR123NC010
2018 DOMINION ENERGY TRANS INC Servicing Fluid 151.40 Tons RESIDUAL WASTE PROCESSING FACILITY WMGR123NC010
2019 DOMINION ENERGY TRANS INC Waste Water Treatment Sludge 17.90 Tons LANDFILL 301358
2019 DOMINION ENERGY TRANS INC Drilling Fluid Waste 19.70 Tons LANDFILL 301358
2019 DOMINION ENERGY TRANS INC Synthetic Liner Materials 26.80 Tons LANDFILL 301358

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1069262 Primary Facility 2001-10-18 Routine/Complete Inspection No Violations Noted
1173963 Primary Facility 2002-10-02 Routine/Complete Inspection No Violations Noted
1584425 Primary Facility 2006-10-13 Routine/Complete Inspection No Violations Noted
1661324 Primary Facility 2007-10-16 Routine/Complete Inspection No Violations Noted
1747232 Primary Facility 2008-10-28 Routine/Complete Inspection No Violations Noted
2010512 Primary Facility 2011-10-06 Routine/Complete Inspection No Violations Noted
2229614 Primary Facility 2013-10-31 Routine/Complete Inspection No Violations Noted
2264561 Primary Facility 2014-04-15 Plugging(Includes Plugged/Mined Through) No Violations Noted
2306391 Primary Facility 2014-09-10 Plugging(Includes Plugged/Mined Through) No Violations Noted
2307123 Primary Facility 2014-09-25 Plugging(Includes Plugged/Mined Through) No Violations Noted
2311179 Primary Facility 2014-10-08 Plugging(Includes Plugged/Mined Through) No Violations Noted
2311461 Primary Facility 2014-10-09 Plugging(Includes Plugged/Mined Through) No Violations Noted
2312211 Primary Facility 2014-10-10 Plugging(Includes Plugged/Mined Through) No Violations Noted
2315136 Primary Facility 2014-10-22 Plugging(Includes Plugged/Mined Through) No Violations Noted
2315145 Primary Facility 2014-10-23 Plugging(Includes Plugged/Mined Through) No Violations Noted
2317917 Primary Facility 2014-10-29 Plugging(Includes Plugged/Mined Through) No Violations Noted
2394134 Primary Facility 2015-07-21 Plugging(Includes Plugged/Mined Through) No Violations Noted At the time of inspection Overcast, ~ 78 degrees F.
2415566 Primary Facility 2015-10-07 Routine/Complete Inspection No Violations Noted
2528019 Primary Facility 2016-10-06 Routine/Complete Inspection No Violations Noted
2755477 Primary Facility 2018-07-24 Plugging(Includes Plugged/Mined Through) No Violations Noted Routine inspection of this storage well which is being replugged since it was partially plugged back to 4800' in 2014. The well was originally drilled with 7" casing ran, later reworked with 4 1/2" casing cemented to surface with all 7" left in the hole. During this replugging the operator intends to address annular flow by milling window in the 4 1/2", spotting resin and squeezing, mill window uphole for purpose of accessing 7" casing for perf and squeeze behind the 7". At the time of inspection, the rig is on location rigged up on the well. No crew was on location at the time of inspection. The cellar was full of water outside of 10 3/4" surface casing. No bubbling was observed. 4 1/2" casing is lined out to choke/ gas buster tank. BOP is installed. Tubing is in the hole TIW. I called the operator and found out the crew had to go on another job and is expected to return Friday or next week to resume operations. No obvious major issues were observed.
2758320 Primary Facility 2018-07-31 Plugging(Includes Plugged/Mined Through) No Violations Noted A routine inspection of a storage well which is being replugged after after initial plugging attempt in 2014. A rig is on location for final plug and abandonment. Rig is down at time of inspection waiting on equipment in preparation of milling a window 4 1/2" casing to spot resin and squeeze annulus. I spoke with the plugging contractor and discussed the well history, plugging procedure and objectives. No obvious major issues were observed during this inspection.
2767311 Primary Facility 2018-08-24 Plugging(Includes Plugged/Mined Through) No Violations Noted A routine inspection of a storage well which is being replugged after after initial plugging attempt in 2014. A rig is on location for final plug and abandonment. I met with the plugging contractor to discuss operations on the pad. The rig successfully milled window in 4 1/2" production casing as planned. They ran in with tubing on packer above the window and shut in overnight. Tubing reportedly pressured to 90 PSI overnight indicating they accessed the gas by milling the window. The rig is on standby for squeeze work while the cement company and operator line out negotiations. No obvious major issues were observed.
2773467 Primary Facility 2018-09-11 Plugging(Includes Plugged/Mined Through) No Violations Noted A routine inspection of a storage well which is being replugged after after initial plugging attempt in 2014. A rig is on location for final plug and abandonment. The rig has been on standby during recent weeks during negotiations with the cement company. At the time of inspection, no crew was onsite. The plugging and rig contractor were on location. Squeeze work on 4 1/2" casing window was scheduled for today but just got pushed back to tomorrow. No obvious major issues were observed.
2775253 Primary Facility 2018-09-12 Plugging(Includes Plugged/Mined Through) No Violations Noted A routine inspection of a storage well which is being replugged after after initial plugging attempt in 2014 was conducted September 12, 2018. A rig is on location for final plug and abandonment. Cementers are rigged down and pulling off location after spotting squeeze resin in the wellbore. I met with the plugging contractor to discuss depths and volumes relating to the job. The resin was spotted in 4 1/2" casing across 20' window in casing (4603'-4623'). Well diagnostics conducted previously have revealed the window has communication with gas zone of interest. A retainer has been set at 4273'. Cementers pumped approximately 6 bbls of resin, displaced to retainer with water, stung out of retainer and reverse circulate to clear out any potential residual resin above retainer. Rigged down cementers, rigged up test truck to pressure up for hesitation squeeze. Starting squeeze pressure was 2300 PSI. Saw very little bleed off and increased pressure in increments up to 2900 PSI where pressure appears to be holdin
2783281 Primary Facility 2018-09-21 Plugging(Includes Plugged/Mined Through) No Violations Noted Rig is on location for final plug and abandonment (re-plug). The rig is milling window in 4 1/2" casing above retainer set for squeeze last week, in order to have access to 7" casing for perf and squeeze on 7". The operator and main plugging contractor are not on location. I inspected resin samples from last weeks squeeze work. No obvious major issues were observed at this time.
2784161 Primary Facility 2018-10-03 Plugging(Includes Plugged/Mined Through) No Violations Noted Rig is on location for final plug and abandonment (re-plug). Halliburton are rigged up for resin squeeze, pressure testing pump iron when I arrived on location. They bled off, I walked over and met with the operator and plugging contractor to discuss recent operations and today's squeeze procedure. Since last window/squeeze, they moved uphole to cut additional window in the 4 1/2" from 4210'-4222' to allow access to the 7" casing which was then perforated for today's squeeze work. The crew unhooked service line, tried to sting into retainer, could not sting in. Rigged up service line and pumped. Since they could not sting into the retainer, they will run in with a packer on the workstring so they can execute the squeeze as intended. No obvious major issues were observed.
2791880 Primary Facility 2018-10-19 Plugging(Includes Plugged/Mined Through) No Violations Noted Routine inspection following last squeeze attempt as a part of a re-plugging project. Window was cut in 4 1/2" casing from 1130'-1140' to access 7" casing where it was cut at 1132', 1135' and 1138' for resin squeeze on the 7" x 10 3/4" annulus. 8 bbls resin were pumped with 55 bbls squeezed reportedly. At the time of inspection, no one was on location. Tubing is in the hole, shut in with analog gauge. 10 3/4" lined out to the edge of pad via steel hose. No obvious visible significant flow or venting was observed on the 10 3/4". No obvious issues were observed during this inspection.
2806890 Primary Facility 2018-11-27 Plugging(Includes Plugged/Mined Through) No Violations Noted A routine inspection of this re-plugged well was conducted November 27, 2018. At the time of inspection, the recently re-plugged well is in a 4-5' fenced off depression. Casing is cut off and open and there are two annular vents extending above ground level. There was no visible or audible venting or discharge observed. The area surrounding the well was snow-covered; no evidence of discharge was observed. Access to the well is somewhat limited at this time. No obvious issues were observed.
2811990 Primary Facility 2018-12-07 Administrative/File Review No Violations Noted December 7, 2018: The (re-plugging) Certificate of Well Plugging for the RW 66 (105-20383) has been received, reviewed, signed, and sent to file. The well was previously plugged 10/24/2014 and has been replugged at this time to address gas on annuli.
2815538 Primary Facility 2018-12-14 Plugging(Includes Plugged/Mined Through) No Violations Noted A routine (post-plugging) inspection of the RW 66 was conducted December 14, 2018. The plugged well was recently re-plugged by the operator. At the time of inspection, the plugged well is buried and the well cellar has been filled with material. There were three 2" candy cane vent pipes extending upward approximately 7' above ground level, one of which was marked with The permit number and (re)plug date (11/6/2018). There was no visible or audible venting observed. No open holes or discharge was observed. There were no obvious immediate issues observed at this time.
681295 Primary Facility 1988-10-13 Routine/Complete Inspection No Violations Noted
681296 Primary Facility 1989-10-05 Routine/Complete Inspection No Violations Noted
682960 Primary Facility 1990-10-18 Routine/Complete Inspection No Violations Noted
683715 Primary Facility 1991-10-03 Routine/Complete Inspection No Violations Noted
685160 Primary Facility 1993-10-14 Routine/Complete Inspection No Violations Noted
685981 Primary Facility 1994-10-19 Routine/Complete Inspection No Violations Noted
686842 Primary Facility 1995-10-19 Routine/Complete Inspection No Violations Noted
687675 Primary Facility 1996-10-21 Routine/Complete Inspection No Violations Noted
688376 Primary Facility 1997-10-16 Routine/Complete Inspection No Violations Noted
688896 Primary Facility 1998-03-25 Drilling/Alteration No Violations Noted
688911 Primary Facility 1998-04-02 Drilling/Alteration No Violations Noted
688914 Primary Facility 1998-03-30 Drilling/Alteration No Violations Noted
688918 Primary Facility 1998-04-08 Drilling/Alteration No Violations Noted
688922 Primary Facility 1998-04-15 Drilling/Alteration No Violations Noted
688925 Primary Facility 1998-04-23 Drilling/Alteration No Violations Noted
688931 Primary Facility 1998-04-27 Drilling/Alteration No Violations Noted
689016 Primary Facility 1998-07-14 Routine/Complete Inspection No Violations Noted
689040 Primary Facility 1998-08-05 Routine/Complete Inspection No Violations Noted
689315 Primary Facility 1998-10-07 Routine/Complete Inspection No Violations Noted
881812 Primary Facility 1999-10-07 Routine/Complete Inspection No Violations Noted
975885 Primary Facility 2000-10-19 Routine/Complete Inspection No Violations Noted

For data sources see[7]

References