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37-063-34637

Well Details

Well ID: 37-063-34637
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Country: United States
State: Pennsylvania
County: Indiana
Municipality: Brush Valley Township
Operator Name: ALLIANCE PETRO CO LLC
Well Pad ID:
Farm/Lease Name: GRACE L JONES (34A) 1
License Status: ACTIVE
Spud Date: 2006-04-17
Permit Date: 2006-02-10
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.492635
Longitude: -79.115867

For data sources see[1][2][3]

Well History

Date Event
2006-02-10 New Permit Application
2006-04-17 Performed Spud Operation
2006-04-20 Drilling Completion
2006-05-02 Perforation
2006-06-05 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2006 PHILLIPS EXPLORATION INC 5,627.00 195 0.00 0 0.00 0
2007 PHILLIPS EXPLORATION INC 8363.00 365 0.00 0 0.00 0
2008 PHILLIPS EXPLORATION INC 10367.00 316 0.00 0 0.00 0
2009 PHILLIPS EXPLORATION INC 7752.00 365 0.00 0 0.00 0
2010 PHILLIPS EXPLORATION INC 6,036.00 365 0.00 0 0.00 0
2011 PHILLIPS EXPLORATION INC 4,355.00 365 0.00 0 0.00 0
2012 XTO ENERGY INC 5,197.00 366 0.00 0 0.00 0
2013 XTO ENERGY INC 4,562.00 365 0.00 0 0.00 0
2014 XTO ENERGY INC 4,086.00 365 0.00 0 0.00 0
2015 XTO ENERGY INC 3,496.64 365 0.00 0 0.00 0
2016 XTO ENERGY INC 2,187.51 366 0.00 0 0.00 0
2017 ALLIANCE PETRO CO LLC 1,617.00 334 0.00 0 0.00 0
2018 ALLIANCE PETRO CO LLC 3,272.00 365 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2008 PHILLIPS EXPLORATION INC Brine 400.00 Bbl Brine or Industrial Waste Treatment Plt PA0101508
2010 PHILLIPS EXPLORATION INC Produced Fluid 147.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE 301353
2010 PHILLIPS EXPLORATION INC Produced Fluid 20.00 Bbl PUBLIC SEWAGE TREATMENT PLANT PA0026310
2010 PHILLIPS EXPLORATION INC Produced Fluid 18.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0095443
2010 PHILLIPS EXPLORATION INC Produced Fluid 23.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0095273
2010 PHILLIPS EXPLORATION INC Produced Fluid 1.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0020346
2010 PHILLIPS EXPLORATION INC Produced Fluid 1.00 Bbl PUBLIC SEWAGE TREATMENT PLANT PA0026034
2010 PHILLIPS EXPLORATION INC Produced Fluid 6.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0091472
2011 PHILLIPS EXPLORATION INC Produced Fluid 150.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0095273
2012 XTO ENERGY INC Produced Fluid 216.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0095273
2013 XTO ENERGY INC Produced Fluid 136.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095273
2013 XTO ENERGY INC Produced Fluid 136 Bbl CENT WASTE TRT FAC NPDES PA0095273
2014 XTO ENERGY INC Produced Fluid 124.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095273
2014 XTO ENERGY INC Produced Fluid 124 Bbl CENT WASTE TRT FAC NPDES PA0095273
2015 XTO ENERGY INC Produced Fluid 99 Bbl CENT WASTE TRT FAC NPDES PA0095273
2015 XTO ENERGY INC Produced Fluid 99.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095273
2016 XTO ENERGY INC Produced Fluid 23.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095273
2016 XTO ENERGY INC Produced Fluid 23 Bbl CENT WASTE TRT FAC NPDES PA0095273
2017 ALLIANCE PETRO CO LLC Produced Fluid 41.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095273
2018 ALLIANCE PETRO CO LLC Produced Fluid 48.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095273
2019 ALLIANCE PETRO CO LLC Produced Fluid 146.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095273

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2094076 Primary Facility 2012-08-23 Incident- Response to Accident or Event Violation(s) Noted ON 8/22/12 at 1200hrs, Steve Smith of XTO called to report a discharge of approximately 25bbls of production water from a poly tank as result of an animal (believed to be porcupine) eating a hole through tank. Release found by well tender approximately 1- 1 1/2 earlier. Several attempts were made to reach SWRO but he was unable to reach a "voice," therefore, he called WQS April Weiland. Department met with XTO well tender in order to access location. At the time of today's inspection, brine tank had been emptied and removed from area of contamination. Contaminated soils have been removed and placed in 7 covered roll off boxes located onsite. Based on current observation it appears that brine contaminated soils successfully removed, department is awaiting confirmatory samples to ensure all impacted soils have been removed. Once it has been confirmed all contaminated soils have been removed operator may proceed with restoring area. Violations are being issued for this reportable release. Addtl Viols 78.57, 91.34, SWMA 301
2180554 Primary Facility 2013-07-02 Compliance Evaluation No Violations Noted Compliance evaluation inspt for violations previously issued on 8/23/2012 for reportable release of brine (inspection record 2094076).
2217259 Primary Facility 2013-10-24 Routine/Complete Inspection No Violations Noted At time of inspection, well equipped for production. According to records, date of spud was 4/17/2006. Well tag present, legible. Brine tank sound. Shared access road stable.
2446328 Primary Facility 2016-02-03 Routine/Complete Inspection No Violations Noted At time of inspection no E&S issues observed on access road or on site. Well tag present and legible. Brine tank appears structurally sound.
2851163 Primary Facility 2019-03-11 Administrative/File Review No Violations Noted REVIEWED FILE AND COMPLETED START SHEET

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
2094076 647454 08/23/2012 2012-08-23 78.54* - Failure to properly control or dispose of industrial or residual waste to prevent pollution of the waters of the Commonwealth. Environmental Health & Safety

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
647454 287770 NOV - Notice of Violation Comply/Closed 2013-07-02

For data sources see[7]

References