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Well ID: 37-063-33083 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Indiana | |
Municipality: North Mahoning Township | |
Operator Name: ALLIANCE PETRO CO LLC | |
Well Pad ID: | |
Farm/Lease Name: JAY HAMILTON 3 | |
License Status: ACTIVE | |
Spud Date: 2002-05-30 | |
Permit Date: 2002-04-23 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.889261 | |
Longitude: -78.998345 |
Date | Event |
---|---|
2002-04-23 | New Permit Application |
2002-05-30 | Performed Spud Operation |
2002-06-03 | Drilling Completion |
2002-06-06 | Perforation |
2003-02-27 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2002 | CONSOL GAS CO | 16927 | 365 | 0.00 | 0 | 0.00 | 0 |
2003 | CONSOL GAS CO | 22364 | 365 | 0.00 | 0 | 0.00 | 0 |
2005 | CONSOL GAS CO | 10495 | 365 | 0.00 | 0 | 0.00 | 0 |
2006 | CONSOL GAS CO | 8,549.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2007 | CONSOL GAS CO | 7513.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2008 | CONSOL GAS CO | 6914.22 | 365 | 0.00 | 0 | 0.00 | 0 |
2009 | CONSOL GAS CO | 6138.76 | 365 | 0.00 | 0 | 0.00 | 0 |
2010 | CONSOL GAS CO | 5,674.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2011 | CONSOL GAS CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | CNX GAS CO LLC | 5,074.00 | 366 | 0.00 | 0 | 0.00 | 0 |
2013 | CNX GAS CO LLC | 4,476.04 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | CNX GAS CO LLC | 4,338.74 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | CNX GAS CO LLC | 3,928.74 | 365 | 0.00 | 0 | 0.00 | 0 |
2016 | CNX GAS CO LLC | 3,861.68 | 366 | 0.00 | 0 | 0.00 | 0 |
2017 | CNX GAS CO LLC | 4,412.09 | 365 | 0.00 | 0 | 0.00 | 0 |
2018 | CNX GAS CO LLC | 3,158.24 | 365 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2002 | CONSOL GAS CO | Fracking Fluid | 80.00 Bbl | Brine or Industrial Waste Treatment Plt | |
2002 | CONSOL GAS CO | Drilling | 80.00 Bbl | Brine or Industrial Waste Treatment Plt | |
2003 | CONSOL GAS CO | Brine | 80.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0095273 |
2003 | CONSOL GAS CO | Brine | 67.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0091472 |
2003 | CONSOL GAS CO | Brine | 128.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0026034 |
2003 | CONSOL GAS CO | Brine | 173.00 Bbl | Injection Disposal Well | 5690201 |
2005 | CONSOL GAS CO | Brine | 65.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0095273 |
2005 | CONSOL GAS CO | Brine | 94.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0091472 |
2008 | CONSOL GAS CO | Brine | 62.50 Bbl | Brine or Industrial Waste Treatment Plt | PA0091472 |
2009 | CONSOL GAS CO | Brine | 65.00 Bbl | Injection Disposal Well | PA101656 |
2010 | CONSOL GAS CO | Produced Fluid | 65.00 Bbl | Injection Disposal Well | PAS2D902BCLE |
2011 | CNX GAS CO LLC | Produced Fluid | 60.00 Bbl | Injection Disposal Well | 34-155-23584 |
2012 | CNX GAS CO LLC | Produced Fluid | 61.00 Bbl | Injection Disposal Well | 34-155-21447 |
2013 | CNX GAS CO LLC | Produced Fluid | 51.00 Bbl | Injection Disposal Well | PAS2D912BSOM |
2013 | CNX GAS CO LLC | Produced Fluid | 54.00 Bbl | Injection Disposal Well | 34-119-28776 |
2014 | CNX GAS CO LLC | Produced Fluid | 48.16 Bbl | Injection Disposal Well | 34-013-20609 |
2015 | CNX GAS CO LLC | Produced Fluid | 6.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 |
2015 | CNX GAS CO LLC | Produced Fluid | 6 Bbl | CENT WASTE TRT FAC NPDES | PA0095273 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2416988 | Primary Facility | 2015-10-15 | Administrative/File Review | In Compliance with Policy | SPILL. |
2417048 | Primary Facility | 2015-10-15 | Administrative/File Review | In Compliance with Policy | Admin inspt conducted in response to inspt ID 2416988 for the 10/15 reportable release of brine water.Upon receipt of spill report, Dept contacted Opr rep R.Vrobel via phone at 1416.Mr. V stated a release of 1.5 bbl brine water w/skim of oil occurred w/in an earthen dike as a result of a leaking BT.Source of leak has not yet been identified as tank has not yet been removed and inspected.Mr. V stated that although dike is lined w/plastic, there are numerous holes in plastic.Per Mr. V, BT lost 2 in of brine & oil, equating to 1.5 bbl.Leak was discovered by well-tender at 1155 on 10/15 and subsequently reported to SWRO at 1330.Mr. V stated release appears to be visibly contained w/in dike,appears to be dripping straight down into ground.No waterways reported to be impacted.According to Mr. V, a water truck is en route to site to empty BT;Spartan will be out tomorrow (10/16) to remove tank, commence excavation.Opr appears to be ICP at this time. A FUI will be conducted to assess environmental impact and/or issue any assoc viols as necessary. |
2417087 | Primary Facility | 2015-10-16 | Incident- Response to Accident or Event | Violation(s) Noted | On-site inspection conducted in response to inspection ID 2416988 for the 10/15/15 reportable release of brine water. |
2420598 | Primary Facility | 2015-10-30 | Administrative/File Review | Outstanding Violations - No Viols Req'd | Admin inspt conducted in response to viols issued under record 2417087 (enf ID 330622) for reportable release of 1.5 bbl brine water/oil.In accordance w/Spill Policy, 15 day written response received by Dept on 10/23 notifying Dept that Opr will be utilizing Alternative Remediation method for remediation of release.Upon review of 15 day written response, Opr did not identify all COCs that will be analyzed and method of attainment for remediation to be utilized for each constituent.During Dept’s on-site inspt on 10/16 (inspection 2417087), Dept was notified that a “skim of crude oil” was also released.This was not identified in 15 day written response.Dept contacted Opr rep J. Valentine via phone to request that a list be included w/15 day written response that identifies all COCs that will be analyzed and method of attainment for remediation to be utilized for each constituent.Dept recom’d that Opr also analyze COCs for crude oil in addition to brine water.Mr. Valentine agreed to re-submit 15 day written response as requested. |
2434474 | Primary Facility | 2015-12-14 | Follow-up Inspection | Outstanding Violations - No Viols Req'd | On-site FUI conducted in response to viols issued under record 2417087 (enf ID 330622) for reportable release of 1.5 bbl brine water/oil.At time of inspt, BT re-located w/in earthen dike, located on gravel base and plywood.Excavated contaminated soils not on-site.No accelerated E&S issues observed in relation to well site at this time.Dept recommends Opr cont’ to monitor/maintain AR as necessary in order to prevent any potential additional pollution events from occurring.Although a 15 day written response was received by the Dept on 10/23/15 notifying Dept that Opr will be utilizing Alternative Remediation method for remediation of release, a revised 15 day written response was requested by Dept on 10/30/15 (inspection ID 2420598).This revised 15 day written response has not yet been received.To date, a Site Characterization Report has not yet been received.Viols issued under record 2417087 (enf ID 330622) remain outstanding. |
2440205 | Primary Facility | 2016-01-13 | Compliance Evaluation | No Violations Noted | Admin CEI conducted in response to violations issued under inspection record 2417087 (enf ID 330622) for the reportable release of 1.5 bbl brine water/oil. Remedial Action Completion Report to be forwarded to ECB Program for review.
As the site is permanently stabilized (inspection record 2434474) and the Operator has submitted a RACR to the Department for review, violations issued under inspection record 2417087 (enf ID 330622) have been corrected. Violations may be forthcoming pending future inspections monitoring site remediation. |
2454831 | Primary Facility | 2016-02-22 | Administrative/File Review | In Compliance with Policy | Admin CEI conducted in response to violations issued under inspection record 2417087 (enf ID 330622) for the reportable release of 1.5 bbl brine water/oil.
Although a 15 day written response was received by the Department on 10/23/2015 notifying the Department that the Operator will be utilizing the Alternative Remediation method for the remediation of this release, a revised 15 day written response was requested by the Department on 10/30/2015 (inspection ID 2420598). This revised 15 day written response was received on 11/6/2015. The Remedial Action Completion Report was received by the Department on 12/28/2015. The ECB acknowledged receipt of the Remedial Action Plan Completion on 2/1/2016. Operator appears to be in compliance with current policy at this time. |
2483690 | Primary Facility | 2016-05-02 | Administrative/File Review | In Compliance with Policy | Admin inspection conducted in response to violations issued under inspection record 2417087 (enf ID 330622) for the reportable release of 1.5 bbl brine water/oil. Violations were previously corrected under inspection ID 2440205.
Although a 15 day written response was received by the Department on 10/23/2015 notifying the Department that the Operator will be utilizing the Alternative Remediation method for the remediation of this release, a revised 15 day written response was requested by the Department on 10/30/2015 (inspection ID 2420598). This revised 15 day written response was received on 11/6/2015. The Remedial Action Completion Report was received by the Department on 12/28/2015. The Operator is utilizing the method of Alternative Remediation for the following constituents of concern: Aluminum, Barium, Boron, Iron, Lithium, Manganese, Fluoranthene, Phenol, Selenium, Strontium, Chloride, Vanadium, Zinc, Benzene, Fluorene, Pyrene, sec-Butyl benzene, tert-Butyl benzene, Cyclohexane, Ethylbenzene, Isopro |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
2417087 | 737097 | 10/15/2015 | 2015-10-15 | 78.54 - GENERAL REQUIREMENTS - Operator failed to control and dispose of fluids, residual waste and drill cuttings, including tophole water, brines, drilling fluids, drilling muds, stimulation fluids, well servicing fluids, oil, and production fluids | Environmental Health & Safety |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
737097 | 330622 | NOV - Notice of Violation | Comply/Closed | 2016-05-18 |
For data sources see[7]