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37-063-27440

Well Details

Well ID: 37-063-27440
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Country: United States
State: Pennsylvania
County: Indiana
Municipality: Cherryhill Township
Operator Name: ALLIANCE PETRO CO LLC
Well Pad ID:
Farm/Lease Name: DANIEL J LIEB ET UX 2
License Status: ACTIVE
Spud Date: 1983-04-12
Permit Date: 1983-02-09
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.618697
Longitude: -78.953678

For data sources see[1][2][3]

Well History

Date Event
1983-02-09 New Permit Application
1983-04-12 Performed Spud Operation
1983-04-19 Drilling Completion
1983-04-27 Perforation
1983-07-01 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1992 ATLAS RESOURCES INC 5926.00 365 0.00 0 0.00 0
1996 POWER GAS MKT & TRANS INC 2533 240 0.00 0 0.00 0
1997 POWER GAS MKT & TRANS INC 4053 365 0.00 0 0.00 0
1998 POWER GAS MKT & TRANS INC 4995 365 0.00 0 0.00 0
1999 POWER GAS MKT & TRANS INC 2933 365 0.00 0 0.00 0
2000 POWER GAS MKT & TRANS INC 2658 365 0.00 0 0.00 0
2001 POWER GAS MKT & TRANS INC 2312 325 0.00 0 0.00 0
2002 POWER GAS MKT & TRANS INC 2341 365 0.00 0 0.00 0
2003 POWER GAS MKT & TRANS INC 2663.84 365 0 0 0.00 0
2004 POWER GAS MKT & TRANS INC 2843 365 0 365 0.00 0
2005 POWER GAS MKT & TRANS INC 3895 365 0.00 0 0.00 0
2006 POWER GAS MKT & TRANS INC 2,732.00 365 0.00 0 0.00 0
2007 POWER GAS MKT & TRANS INC 0.00 0 0.00 0 0.00 0
2008 POWER GAS MKT & TRANS INC 2713.00 365 0.00 0 0.00 0
2009 EXCO RESOURCES PA INC 3256.00 365 0.00 0 0.00 0
2010 EXCO RESOURCES PA INC 2,748.00 365 0.00 0 0.00 0
2011 EXCO RESOURCES PA INC 2,111.00 365 0.00 0 0.00 0
2012 EXCO RESOURCES PA LLC 2,102.00 366 0.00 0 0.00 0
2013 EXCO RESOURCES PA LLC 1,745.00 365 0.00 0 0.00 0
2014 EXCO RESOURCES PA LLC 2,233.00 365 0.00 0 0.00 0
2015 EXCO RESOURCES PA LLC 1,968.00 364 0.00 0 0.00 0
2016 ALLIANCE PETRO CO LLC 793.00 183 0.00 0 0.00 0
2017 ALLIANCE PETRO CO LLC 2,177.00 365 0.00 0 0.00 0
2018 ALLIANCE PETRO CO LLC 2,214.00 365 0.00 0 0.00 0
2019 ALLIANCE PETRO CO LLC 1,887.00 365 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
1996 POWER GAS MKT & TRANS INC Brine 30.00 Bbl Injection Disposal Well 033-22059
1996 POWER GAS MKT & TRANS INC Brine 25.00 Bbl Road Spreading UNK
1999 POWER GAS MKT & TRANS INC Brine 63.00 Bbl Brine or Industrial Waste Treatment Plt PA0095443
1999 POWER GAS MKT & TRANS INC Brine 50.00 Bbl Injection Disposal Well 1788201
2000 POWER GAS MKT & TRANS INC Brine 42.00 Bbl Injection Disposal Well 1788201
2001 POWER GAS MKT & TRANS INC Brine 50.00 Bbl Injection Disposal Well
2002 POWER GAS MKT & TRANS INC Brine 63.00 Bbl Injection Disposal Well PAS2D902BCLE-02
2003 POWER GAS MKT & TRANS INC Brine 128.00 Bbl Injection Disposal Well PAS2D902BCLE-02
2004 POWER GAS MKT & TRANS INC Brine 43.00 Bbl Injection Disposal Well PAS2D902BCLE-02
2005 POWER GAS MKT & TRANS INC Brine 71.00 Bbl Injection Disposal Well PA1788201
2005 POWER GAS MKT & TRANS INC Brine 30.00 Bbl Brine or Industrial Waste Treatment Plt PA0095273
2006 POWER GAS MKT & TRANS INC Brine 63.00 Bbl Injection Disposal Well PAS2D902BCLE-02
2009 EXCO RESOURCES PA INC Brine 20.00 Bbl Injection Disposal Well PAS2D205BCLE
2013 EXCO RESOURCES PA LLC Produced Fluid 8.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095273
2013 EXCO RESOURCES PA LLC Produced Fluid 8 Bbl CENT WASTE TRT FAC NPDES PA0095273
2014 EXCO RESOURCES PA LLC Produced Fluid 20.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095273
2014 EXCO RESOURCES PA LLC Produced Fluid 20 Bbl CENT WASTE TRT FAC NPDES PA0095273
2014 EXCO RESOURCES PA LLC Produced Fluid 16 Bbl CENT WASTE TRT FAC NPDES PA0101508
2014 EXCO RESOURCES PA LLC Produced Fluid 16.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0101508

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2364842 Primary Facility 2015-04-20 Routine/Complete Inspection Violation(s) Noted At time of insp,tag present/legible.BT appears sound.Site appears stabilized.Dept obs'ed area of dead/no veg that may be indicative of brine release. Dept collected soil samples;1 background,3 of potentially impacted soils.Dept spoke to EXCO on 4-21-15.Byers stated would test with conductivity meter. Replied there was ’historic brine spillage,'BT replaced for ‘field-wide hardware upgrades’ and would ‘lime,seed, straw’ area. Dept stated to ‘lime, seed and mulch’ not approved option - spills /releases at O&G locations. Dept rec Opr follow O&G spill policy to address ‘historic brine spillage.' Insp result PEND until review of results. Insp with WQS Foulk.UPDATE: 9-14-15. Soil sample results from Dept show there are Constituents of Concern/ Indicators of brine release present in 3 soil samples taken of impacted soils. The levels of COC's present, when compared to the back ground sample, indicate a brine release.Viols being issued for:Opr discharged brine on/into the ground, and Failure to notify DEP of pollution incident. Add'l remarks on paper SAIR
2422632 Primary Facility 2015-10-28 Follow-up Inspection Outstanding Violations - No Viols Req'd Follow up inspection to inspection ID # 2364842.
2424631 Primary Facility 2015-11-09 Follow-up Inspection Outstanding Violations - No Viols Req'd Inspection is result of on-site meeting request by EXCO rep Ron Jenkins. EXCO rep Denny Fennell also in attendance.
2429881 Primary Facility 2015-12-02 Compliance Evaluation No Violations Noted Compliance Evaluation Inspection to Inspection # 2364842 for previously issued violations for Operator's discharge of brine and failure to report a release.
2429893 Primary Facility 2015-12-03 Administrative/File Review No Violations Noted Admin Inspection to Inspection # 2429881.
2521369 Primary Facility 2016-09-22 Routine/Complete Inspection No Violations Noted At time of inspection no E&S issues observed on gated access road. No E&S issues observed on site. Well appears equipped for production. Well tag present. Brine tank appears structurally sound.

Impacted soils that were excavated due to a release (inspection record #2364842) have been removed. Site appears permanently stabilized with >70% uniform vegetative growth.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
2364842 734577 04/20/2015 2015-04-20 78.57(a) - CONTROL, STORAGE AND DISPOSAL OF PRODUCTION FLUIDS - Operator failed to collect the brine and other fluids produced during operation, service and plugging of the well in a tank, pit or a series of pits or tanks, or other device approved by Environmental Health & Safety
2364842 734578 04/20/2015 2015-04-20 91.33A - Failure to notify DEP of pollution incident. No phone call made forthwith Administrative

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
734577 329485 NOV - Notice of Violation Comply/Closed 2015-12-24
734578 329485 NOV - Notice of Violation Comply/Closed 2015-12-24

For data sources see[7]

References