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37-063-23470

Well Details

Well ID: 37-063-23470
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Country: United States
State: Pennsylvania
County: Indiana
Municipality: Grant Township
Operator Name: ALLIANCE PETRO CO LLC
Well Pad ID:
Farm/Lease Name: CLIFFORD K MCQUOWN C378
License Status: INACTIVE
Spud Date: 1976-12-02
Permit Date: 1976-08-24
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.755173
Longitude: -78.984052

For data sources see[1][2][3]

Well History

Date Event
1976-08-24 New Permit Application
1976-12-02 Performed Spud Operation
1976-12-06 Drilling Completion
1977-01-05 Perforation
1977-02-28 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1996 CASTLE GAS CO INC 14 351 0.00 0 0.00 0
2002 CASTLE GAS CO INC 0.00 0 0.00 0 0.00 0
2003 CASTLE GAS CO INC 0.00 0 0.00 0 0.00 0
2004 CASTLE GAS CO INC 0.00 0 0.00 0 0.00 0
2005 CASTLE GAS CO INC 0.00 0 0.00 0 0.00 0
2006 CASTLE GAS CO INC 0.00 0 0.00 0 0.00 0
2007 CASTLE GAS CO INC 0.00 0 0.00 0 0.00 0
2009 PETRO DEV CORP 0.00 0 0.00 0 0.00 0
2010 PETRO DEV CORP 0.00 0 0.00 0 0.00 0
2011 PDC MOUNTAINEER LLC 0.01 1 0.01 1 0.00 0
2012 PDC MOUNTAINEER LLC 0.00 0 0.00 0 0.00 0
2013 PDC MOUNTAINEER LLC 0.00 0 0.00 0 0.00 0
2014 ALLIANCE PETRO CO LLC 1.00 365 0.00 0 0.00 0
2015 ALLIANCE PETRO CO LLC 0.00 0 0.00 0 0.00 0
2016 ALLIANCE PETRO CO LLC 100.00 365 0.00 0 0.00 0
2017 ALLIANCE PETRO CO LLC 100.00 334 0.00 0 0.00 0
2018 ALLIANCE PETRO CO LLC 100.00 365 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2011 PDC MOUNTAINEER LLC Produced Fluid 34.53 Bbl PUBLIC SEWAGE TREATMENT PLANT PA0020346

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2469696 Primary Facility 2016-03-21 Routine/Complete Inspection No Violations Noted At time of inspection well appears equipped for production. Well tag present and legible. Brine tank appears structurally sound.

It appears recent earthmoving activities have taken place on site. A trench has been dug exposing underground piping. Department contacted Operator by phone from field to inquire about site disturbance. Operator Rep Tom Juart returned call later that day. Mr. Juart stated he would contact field personel and follow up with Department. UPDATE: Mr. Juart followed up later that same day and stated that well is used for house gas and that landowner disturbed site. Department recommends Operator ensure that landowner backfill disturbed area and ensure that site is temporarily stabilized. A follow up inspection will be conducted at a later date to ensure permanent stabilization has been achieved.

For data sources see[7]

References