X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

37-059-27715

Well Details

Well ID: 37-059-27715
Loading map...
Country: United States
State: Pennsylvania
County: Greene
Municipality: Morris Township
Operator Name: CNX GAS CO LLC
Well Pad ID: 155389
Farm/Lease Name: CONSOL MOR10GHSU
License Status: Plugged and Abandoned
Spud Date:
Permit Date: 2018-08-02
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: Yes
Latitude: 39.974883
Longitude: -80.368377

For data sources see[1][2][3]

Well History

Date Event
2018-01-24 Fully Plugged
2018-08-02 New Permit Application
2018-08-27 Performed Spud Operation
2018-09-13 Begin Plugging
2018-09-13 Finished Plugging

For data sources see[4]


Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2018 CNX GAS CO LLC Drill Cuttings 44.35 Tons LANDFILL 100277
2018 CNX GAS CO LLC Drilling Fluid Waste 19.50 Bbl SURFACE IMPOUNDMENT 95-7-37312-19
2018 CNX GAS CO LLC Produced Fluid 22.00 Bbl RESIDUAL WASTE PROCESSING FACILITY
2018 CNX GAS CO LLC Drilling Fluid Waste 4.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE 2014-184
2018 CNX GAS CO LLC Drill Cuttings 132.96 Tons LANDFILL 100172
2018 CNX GAS CO LLC Drill Cuttings 78.66 Tons LANDFILL 06-08438
2018 CNX GAS CO LLC Other Oil & Gas Wastes 2.00 Bbl RESIDUAL WASTE PROCESSING FACILITY
2018 CNX GAS CO LLC Produced Fluid 398.00 Bbl SURFACE IMPOUNDMENT 95-7-37312-19
2018 CNX GAS CO LLC Other Oil & Gas Wastes 21.00 Bbl RESIDUAL WASTE PROCESSING FACILITY ORDER 2016-29
2018 CNX GAS CO LLC Other Oil & Gas Wastes 1.00 Bbl RESIDUAL WASTE PROCESSING FACILITY ODNR 2015-29
2018 CNX GAS CO LLC Drilling Fluid Waste 21.00 Bbl RESIDUAL WASTE PROCESSING FACILITY
2018 CNX GAS CO LLC Drilling Fluid Waste 20.00 Bbl RESIDUAL WASTE PROCESSING FACILITY ORDER 2016-29
2018 CNX GAS CO LLC Produced Fluid 44.00 Bbl SURFACE IMPOUNDMENT 95-7-37312-21
2018 CNX GAS CO LLC Other Oil & Gas Wastes 133.60 Bbl SURFACE IMPOUNDMENT 95-7-37312-19

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2767718 Primary Facility 2018-08-27 Drilling/Alteration No Violations Noted The well was spud on 8/25/18. The operator drilled a 36" hole to 100'. A 30" diameter conductor pipe has been installed at 100' and cemented to the surface. A well cellar has also been installed.
2777569 Primary Facility 2018-09-20 Drilling/Alteration No Violations Noted 24" surface casing was set at 632' and cemented to the surface on 9/10/18. The casing passed the required 30 minute pressure test. A defect in the casing was identified when the operator attempted to drill ahead. The operator was unable to correct the defect. The well was plugged and abandoned on 9/13/18 according to 3220 (d) of the oil and gas act.

For data sources see[6]

References