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Well ID: 37-047-24450 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Elk | |
Municipality: Ridgway Township | |
Operator Name: DIVERSIFIED OIL & GAS LLC | |
Well Pad ID: | |
Farm/Lease Name: ANF WARRANT 4870 39200 | |
License Status: | |
Spud Date: | |
Permit Date: 2010-04-06 | |
Well Type: COMB. OIL&GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 41.410370 | |
Longitude: -78.783396 |
Date | Event |
---|---|
2010-04-06 | New Permit Application |
2010-08-16 | Performed Spud Operation |
2010-08-23 | Drilling Completion |
2011-01-28 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2010 | SENECA RESOURCES CO LLC | 815.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2011 | SENECA RESOURCES CO LLC | 5,006.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2012 | SENECA RESOURCES CO LLC | 4,867.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2013 | SENECA RESOURCES CO LLC | 3,018.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | SENECA RESOURCES CO LLC | 3,674.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | SENECA RESOURCES CO LLC | 3,599.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2016 | DIVERSIFIED OIL & GAS LLC | 3,349.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2017 | DIVERSIFIED OIL & GAS LLC | 1,193.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2018 | DIVERSIFIED OIL & GAS LLC | 1,048.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2019 | DIVERSIFIED OIL & GAS LLC | 3,854.00 | 365 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2010 | SENECA RESOURCES CO LLC | Produced Fluid | 158.33 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0101508 |
2010 | SENECA RESOURCES CO LLC | Fracing Fluid Waste | 305.38 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0101508 |
2011 | SENECA RESOURCES CO LLC | Produced Fluid | 75.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | 3192 |
2011 | SENECA RESOURCES CO LLC | Produced Fluid | 60.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0101508 |
2012 | SENECA RESOURCES CO LLC | Produced Fluid | 90.00 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2013 | SENECA RESOURCES CO LLC | Produced Fluid | 75.00 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NW005 |
2015 | SENECA RESOURCES CO LLC | Produced Fluid | 80.00 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2017 | DIVERSIFIED OIL & GAS LLC | Produced Fluid | 170.00 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NW005 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2716498 | Primary Facility | 2018-04-10 | Routine/Complete Inspection | Violation(s) Noted | This well is leaking gas from the annulus of the conductor and surface casing. The well is shut in and not producing at this time. The reading on the annulus was 100 % methane and 5 ppm H2s. You can hear water bubbling on the backside of the surface casing. |
2754714 | Primary Facility | 2018-07-23 | Routine/Complete Inspection | No Violations Noted | The casing was leaking on this well. They installed 641' of 4 1/2" on a packer about 40' below the original casing seat. No gas is detected but water can be heard cascading down inside the well bore. |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
2716498 | 813215 | 2018-04-10 | 78.86 | Environmental Health & Safety | ||
2716498 | 813216 | 2018-04-10 | 78.81(a)2 | Environmental Health & Safety | ||
2716498 | 813217 | 2018-04-10 | 78.88(d) | Environmental Health & Safety |
For data sources see[7]