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37-047-24450

Well Details

Well ID: 37-047-24450
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Country: United States
State: Pennsylvania
County: Elk
Municipality: Ridgway Township
Operator Name: DIVERSIFIED OIL & GAS LLC
Well Pad ID:
Farm/Lease Name: ANF WARRANT 4870 39200
License Status:
Spud Date:
Permit Date: 2010-04-06
Well Type: COMB. OIL&GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 41.410370
Longitude: -78.783396

For data sources see[1][2][3]

Well History

Date Event
2010-04-06 New Permit Application
2010-08-16 Performed Spud Operation
2010-08-23 Drilling Completion
2011-01-28 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2010 SENECA RESOURCES CO LLC 815.00 365 0.00 0 0.00 0
2011 SENECA RESOURCES CO LLC 5,006.00 365 0.00 0 0.00 0
2012 SENECA RESOURCES CO LLC 4,867.00 365 0.00 0 0.00 0
2013 SENECA RESOURCES CO LLC 3,018.00 365 0.00 0 0.00 0
2014 SENECA RESOURCES CO LLC 3,674.00 365 0.00 0 0.00 0
2015 SENECA RESOURCES CO LLC 3,599.00 365 0.00 0 0.00 0
2016 DIVERSIFIED OIL & GAS LLC 3,349.00 365 0.00 0 0.00 0
2017 DIVERSIFIED OIL & GAS LLC 1,193.00 365 0.00 0 0.00 0
2018 DIVERSIFIED OIL & GAS LLC 1,048.00 365 0.00 0 0.00 0
2019 DIVERSIFIED OIL & GAS LLC 3,854.00 365 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2010 SENECA RESOURCES CO LLC Produced Fluid 158.33 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0101508
2010 SENECA RESOURCES CO LLC Fracing Fluid Waste 305.38 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0101508
2011 SENECA RESOURCES CO LLC Produced Fluid 75.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE 3192
2011 SENECA RESOURCES CO LLC Produced Fluid 60.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0101508
2012 SENECA RESOURCES CO LLC Produced Fluid 90.00 Bbl REUSE OTHER THAN ROAD SPREADING
2013 SENECA RESOURCES CO LLC Produced Fluid 75.00 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123NW005
2015 SENECA RESOURCES CO LLC Produced Fluid 80.00 Bbl REUSE OTHER THAN ROAD SPREADING
2017 DIVERSIFIED OIL & GAS LLC Produced Fluid 170.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW005

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2716498 Primary Facility 2018-04-10 Routine/Complete Inspection Violation(s) Noted This well is leaking gas from the annulus of the conductor and surface casing. The well is shut in and not producing at this time. The reading on the annulus was 100 % methane and 5 ppm H2s. You can hear water bubbling on the backside of the surface casing.
2754714 Primary Facility 2018-07-23 Routine/Complete Inspection No Violations Noted The casing was leaking on this well. They installed 641' of 4 1/2" on a packer about 40' below the original casing seat. No gas is detected but water can be heard cascading down inside the well bore.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
2716498 813215 2018-04-10 78.86 Environmental Health & Safety
2716498 813216 2018-04-10 78.81(a)2 Environmental Health & Safety
2716498 813217 2018-04-10 78.88(d) Environmental Health & Safety

For data sources see[7]

References