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37-047-23955

Well Details

Well ID: 37-047-23955
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Country: United States
State: Pennsylvania
County: Elk
Municipality: Millstone Township
Operator Name: SENECA RESOURCES CO LLC
Well Pad ID:
Farm/Lease Name: FEE ANF WARRANT 2639 1 38010
License Status: Plugged and Abandoned
Spud Date:
Permit Date: 2007-07-11
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 41.416509
Longitude: -79.021007

For data sources see[1][2][3]

Well History

Date Event
2006-06-30 Performed Spud Operation
2007-07-11 New Permit Application
2017-09-12 Begin Plugging
2017-12-01 Finished Plugging

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2007 SENECA RESOURCES CO LLC 345.00 365 0.00 0 0.00 0
2008 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2009 SENECA RESOURCES CO LLC 1.00 365 0.00 0 0.00 0
2010 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2011 SENECA RESOURCES CO LLC 2.00 365 0.00 0 0.00 0
2012 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2013 SENECA RESOURCES CO LLC 0.00 0 19.90 365 0.00 0
2014 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2015 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2016 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2017 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2017 SENECA RESOURCES CO LLC Produced Fluid 355.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW005

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2632194 Primary Facility 2017-09-05 Routine/Complete Inspection No Violations Noted This is a plugged well that appears to be leaking. The well seems to have 2 permit #s. It was originally permitted as 047-23675. I have a plugging certificate for the permit 047-23675 and 047-23955 shows as an active well. I notified Lee Swanson and Amanda Veazey of Seneca about the well leaking and needing replugged.
2637991 Primary Facility 2017-09-20 Plugging(Includes Plugged/Mined Through) No Violations Noted This well was plugged but found to be leaking and is now being drilled out and plugged again. The surface casing is set at 812.4'. I found this well bubbling out the 7" casing. The well had 2 permit numbers one was expired and the other showed as active. The paperwork for plugging was sent in under the expired permit number 047-23675 and should have been submitted for 047-23955. I ask Seneca to resend the NOI for the permit number that had production on it and was showing as active 047-23955.

There is a rig over the hole and they are currently at 100' using a sand pump to remove the pea gravel. All fluid and cuttings are being contained in a lined pit.

2640652 Primary Facility 2017-09-27 Plugging(Includes Plugged/Mined Through) No Violations Noted This well was plugged but found to be leaking and is now being drilled out and plugged again. The surface casing is set at 812.4'. I found this well bubbling out the 7" casing. The well had 2 permit numbers one was expired and the other showed as active. The paperwork for plugging was sent in under the expired permit number 047-23675 and should have been submitted for 047-23955. Seneca resend the NOI for the permit number that had production on it and was showing as active 047-23955.

There is a rig over the hole and they are currently at 820' drilling on cement. They are going to run the camera tomorrow morning to ensure the leak is not coming through the casing or around the casing seat.

All fluid and cuttings are being contained in a lined pit.
2652174 Primary Facility 2017-10-25 Plugging(Includes Plugged/Mined Through) No Violations Noted This well was found to be leaking and is being replugged. Drilled down to 1690 and ran camera and found no bubbles below that depth. Going to run gel from 1690' to 1230' then a cement plug from 1230' to 832' with 3% calcium add to the cement from 923' to 832'.
2666201 Primary Facility 2017-12-01 Administrative/File Review No Violations Noted

For data sources see[7]

References