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Well ID: 37-047-23955 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Elk | |
Municipality: Millstone Township | |
Operator Name: SENECA RESOURCES CO LLC | |
Well Pad ID: | |
Farm/Lease Name: FEE ANF WARRANT 2639 1 38010 | |
License Status: Plugged and Abandoned | |
Spud Date: | |
Permit Date: 2007-07-11 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 41.416509 | |
Longitude: -79.021007 |
Date | Event |
---|---|
2006-06-30 | Performed Spud Operation |
2007-07-11 | New Permit Application |
2017-09-12 | Begin Plugging |
2017-12-01 | Finished Plugging |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2007 | SENECA RESOURCES CO LLC | 345.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2008 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2009 | SENECA RESOURCES CO LLC | 1.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2010 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2011 | SENECA RESOURCES CO LLC | 2.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2012 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2013 | SENECA RESOURCES CO LLC | 0.00 | 0 | 19.90 | 365 | 0.00 | 0 |
2014 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2015 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2016 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2017 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2017 | SENECA RESOURCES CO LLC | Produced Fluid | 355.00 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NW005 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2632194 | Primary Facility | 2017-09-05 | Routine/Complete Inspection | No Violations Noted | This is a plugged well that appears to be leaking. The well seems to have 2 permit #s. It was originally permitted as 047-23675. I have a plugging certificate for the permit 047-23675 and 047-23955 shows as an active well. I notified Lee Swanson and Amanda Veazey of Seneca about the well leaking and needing replugged. |
2637991 | Primary Facility | 2017-09-20 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | This well was plugged but found to be leaking and is now being drilled out and plugged again. The surface casing is set at 812.4'. I found this well bubbling out the 7" casing. The well had 2 permit numbers one was expired and the other showed as active. The paperwork for plugging was sent in under the expired permit number 047-23675 and should have been submitted for 047-23955. I ask Seneca to resend the NOI for the permit number that had production on it and was showing as active 047-23955.
There is a rig over the hole and they are currently at 100' using a sand pump to remove the pea gravel. All fluid and cuttings are being contained in a lined pit. |
2640652 | Primary Facility | 2017-09-27 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | This well was plugged but found to be leaking and is now being drilled out and plugged again. The surface casing is set at 812.4'. I found this well bubbling out the 7" casing. The well had 2 permit numbers one was expired and the other showed as active. The paperwork for plugging was sent in under the expired permit number 047-23675 and should have been submitted for 047-23955. Seneca resend the NOI for the permit number that had production on it and was showing as active 047-23955.
There is a rig over the hole and they are currently at 820' drilling on cement. They are going to run the camera tomorrow morning to ensure the leak is not coming through the casing or around the casing seat. All fluid and cuttings are being contained in a lined pit. |
2652174 | Primary Facility | 2017-10-25 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | This well was found to be leaking and is being replugged. Drilled down to 1690 and ran camera and found no bubbles below that depth. Going to run gel from 1690' to 1230' then a cement plug from 1230' to 832' with 3% calcium add to the cement from 923' to 832'. |
2666201 | Primary Facility | 2017-12-01 | Administrative/File Review | No Violations Noted |
For data sources see[7]