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Well ID: 37-047-00714 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Elk | |
Municipality: Millstone Township | |
Operator Name: SENECA RESOURCES CO LLC | |
Well Pad ID: | |
Farm/Lease Name: W CLYDE 4747 | |
License Status: Plugged and Abandoned | |
Spud Date: 1947-10-11 | |
Permit Date: | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 41.385564 | |
Longitude: -78.989380 |
Date | Event |
---|---|
1947-11-06 | Drilling Completion |
2017-07-22 | Begin Plugging |
2017-09-05 | Finished Plugging |
2017-12-04 | Old Well |
2017-12-04 | Reworked |
2018-07-13 | Fully Plugged |
For data sources see[4]
Stimulation Date | Phase Number | Chemical Agent | Volume (gal) | Treating Pressure (psi) | Breakdown Pressure (psi) |
---|---|---|---|---|---|
Salt Water | 0 | 0 | 0 |
For data sources see[5]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1991 | NATL FUEL GAS SUPPLY CORP | 5017.00 | 364 | 0.00 | 0 | 0.00 | 0 |
1992 | NATL FUEL GAS SUPPLY CORP | 5004.00 | 365 | 0.00 | 0 | 0.00 | 0 |
1993 | NATL FUEL GAS SUPPLY CORP | 4961.00 | 365 | 0.00 | 0 | 0.00 | 0 |
1994 | NATL FUEL GAS SUPPLY CORP | 4939.00 | 365 | 0.00 | 0 | 0.00 | 0 |
1995 | SENECA RESOURCES CO LLC | 5204.00 | 365 | 0.00 | 0 | 0.00 | 0 |
1996 | SENECA RESOURCES CO LLC | 4691 | 365 | 0.00 | 0 | 0.00 | 0 |
1997 | SENECA RESOURCES CO LLC | 4782 | 365 | 0.00 | 0 | 0.00 | 0 |
1998 | SENECA RESOURCES CO LLC | 4418 | 365 | 0.00 | 0 | 0.00 | 0 |
1999 | SENECA RESOURCES CO LLC | 4463 | 365 | 0.00 | 0 | 0.00 | 0 |
2000 | SENECA RESOURCES CO LLC | 4475 | 365 | 0.00 | 0 | 0.00 | 0 |
2001 | SENECA RESOURCES CO LLC | 4463 | 365 | 0.00 | 0 | 0.00 | 0 |
2002 | SENECA RESOURCES CO LLC | 4374 | 365 | 0.00 | 0 | 0.00 | 0 |
2003 | SENECA RESOURCES CO LLC | 2929 | 365 | 0.00 | 0 | 0.00 | 0 |
2004 | SENECA RESOURCES CO LLC | 625 | 365 | 0.00 | 0 | 0.00 | 0 |
2006 | SENECA RESOURCES CO LLC | 623.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2007 | SENECA RESOURCES CO LLC | 537.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2008 | SENECA RESOURCES CO LLC | 521.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2009 | SENECA RESOURCES CO LLC | 520.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2010 | SENECA RESOURCES CO LLC | 258.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2011 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2013 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2014 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2015 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2016 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2017 | SENECA RESOURCES CO LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[6]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2017 | SENECA RESOURCES CO LLC | Produced Fluid | 60.00 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NW005 |
For data sources see[7]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2626034 | Primary Facility | 2017-08-09 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | |
2629225 | Primary Facility | 2017-08-25 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | They have been attempting to get to TD since 7/18/2017, 6 weeks. They got casing and production pipe out and set new 4" on a packer. They have only made 6' in the past 7 days due to the well caving at 1047'. They are currently at 1849". Gave permission to plug at an attainable bottom of 1849'. They set a temporary bridge at 2290'to 2265',above the shot hole in 2003 and there is no gas on the well at this time. They will put 100 sacks of cement 550' at the attainable bottom. Then plug the remainder of the well per regulation. |
2629985 | Primary Facility | 2017-08-29 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Cemented bottom plugs today. 1812' to 1262' with 100 sacks of cement. |
2642212 | Primary Facility | 2017-10-02 | Administrative/File Review | No Violations Noted |
For data sources see[8]