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Well ID: 37-047-00517 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Elk | |
Municipality: Jones Township | |
Operator Name: DIVERSIFIED OIL & GAS LLC | |
Well Pad ID: | |
Farm/Lease Name: HARRY G CLAY 4450 | |
License Status: ACTIVE | |
Spud Date: | |
Permit Date: | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 41.6088 | |
Longitude: -78.7915 |
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1991 | NATL FUEL GAS SUPPLY CORP | 1247.00 | 365 | 0.00 | 0 | 0.00 | 0 |
1992 | NATL FUEL GAS SUPPLY CORP | 1366.00 | 366 | 0.00 | 0 | 0.00 | 0 |
1993 | NATL FUEL GAS SUPPLY CORP | 1356.00 | 364 | 0.00 | 0 | 0.00 | 0 |
1995 | SENECA RESOURCES CO LLC | 2336.65 | 360 | 0.00 | 0 | 0.00 | 0 |
1996 | SENECA RESOURCES CO LLC | 1050 | 365 | 0.00 | 0 | 0.00 | 0 |
1997 | SENECA RESOURCES CO LLC | 1042 | 365 | 0.00 | 0 | 0.00 | 0 |
1998 | SENECA RESOURCES CO LLC | 1593 | 365 | 0.00 | 0 | 0.00 | 0 |
1999 | SENECA RESOURCES CO LLC | 1047 | 365 | 0.00 | 0 | 0.00 | 0 |
2000 | SENECA RESOURCES CO LLC | 1050 | 365 | 0.00 | 0 | 0.00 | 0 |
2001 | SENECA RESOURCES CO LLC | 1047 | 365 | 0.00 | 0 | 0.00 | 0 |
2002 | SENECA RESOURCES CO LLC | 1076 | 365 | 0.00 | 0 | 0.00 | 0 |
2003 | SENECA RESOURCES CO LLC | 1269 | 364 | 0.00 | 0 | 0.00 | 0 |
2004 | SENECA RESOURCES CO LLC | 790 | 364 | 0.00 | 0 | 0.00 | 0 |
2006 | SENECA RESOURCES CO LLC | 984.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2007 | SENECA RESOURCES CO LLC | 1038.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2008 | SENECA RESOURCES CO LLC | 1038.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2009 | SENECA RESOURCES CO LLC | 602.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2010 | SENECA RESOURCES CO LLC | 349.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2011 | SENECA RESOURCES CO LLC | 338.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2012 | SENECA RESOURCES CO LLC | 368.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2013 | SENECA RESOURCES CO LLC | 286.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | SENECA RESOURCES CO LLC | 331.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | SENECA RESOURCES CO LLC | 288.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2016 | DIVERSIFIED OIL & GAS LLC | 57.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2017 | DIVERSIFIED OIL & GAS LLC | 23.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2018 | DIVERSIFIED OIL & GAS LLC | 214.00 | 365 | 0.00 | 0 | 0.00 | 0 |
For data sources see[4]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2558778 | Primary Facility | 2017-02-06 | Routine/Complete Inspection | No Violations Noted | On 2/6/17 at 1220 hrs., I conducted a routine inspection of Diversified's 4450 well (API 047-00517) in Jones Twp., Elk Co. The snow cover prevented complete evaluation of E&S conditions, site stabilization, and whether or not the pad is restored. A site ID sign is present; however it needs to be updated with Diversified's information. A well tag was present at the time of inspection. There are no violations noted for this inspection. |
2660616 | Primary Facility | 2017-11-15 | Routine/Complete Inspection | No Violations Noted | This well is not in production at this time it is shut in and leaking gas at a dented threat reducer shown in photo #2. Production was reported for 2016 57 mcf in 365 days. |
387340 | Primary Facility | 1999-05-11 | Routine/Complete Inspection | No Violations Noted |
For data sources see[5]