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37-039-22409

Well Details

Well ID: 37-039-22409
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Country: United States
State: Pennsylvania
County: Crawford
Municipality: Wayne Township
Operator Name: RANGE RESOURCES APPALACHIA LLC
Well Pad ID:
Farm/Lease Name: L LEGNOSKY 1
License Status: Plugged and Abandoned
Spud Date: 1985-05-05
Permit Date: 1985-05-08
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: Yes
Latitude: 41.554386
Longitude: -79.945836

For data sources see[1][2][3]

Well History

Date Event
1985-05-08 New Permit Application
1985-05-15 Drilling Completion
1986-04-28 NEWLY DRILLED
2018-09-04 Begin Plugging
2018-09-20 Finished Plugging
2018-10-04 Fully Plugged

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1986 MARK RESOURCES CORP 14,807.00 271 0.00 0 0.00 0
1987 MARK RESOURCES CORP 10,823.00 226 0.00 0 0.00 0
1988 MARK RESOURCES CORP 19,101.00 365 0.00 0 0.00 0
1989 MARK RESOURCES CORP 10,814.00 363 0.00 0 0.00 0
1990 MARK RESOURCES CORP 10236.00 341 0.00 0 0.00 0
1991 MARK RESOURCES CORP 8821.00 312 0.00 0 0.00 0
1992 MARK RESOURCES CORP 9233.00 355 0.00 0 0.00 0
1993 RANGE OPR CO 9036.00 360 0.00 0 0.00 0
1994 RANGE OPR CO 7126.00 341 0.00 0 0.00 0
1995 RANGE OPR CO 5946.00 365 0.00 0 0.00 0
1996 RANGE OPR CO 7333 365 0.00 0 0.00 0
1997 RANGE OPR CO 6409 365 0.00 0 0.00 0
1998 RANGE OPR CO 6423 365 0.00 0 0.00 0
1999 RANGE OPR CO 4359 365 0.00 0 0.00 0
2000 RANGE RESOURCES APPALACHIA LLC 4609 365 0.00 0 0.00 0
2001 RANGE RESOURCES APPALACHIA LLC 4021 365 0.00 0 0.00 0
2002 RANGE RESOURCES APPALACHIA LLC 3523 365 0.00 0 0.00 0
2003 RANGE RESOURCES APPALACHIA LLC 2973.23 365 0.00 0 0.00 0
2004 RANGE RESOURCES APPALACHIA LLC 2705.56 365 0.00 0 0.00 0
2005 RANGE RESOURCES APPALACHIA LLC 2701.36 365 0.00 0 0.00 0
2006 RANGE RESOURCES APPALACHIA LLC 2678.12 365 0.00 0 0.00 0
2007 RANGE RESOURCES APPALACHIA LLC 2432 365 0.00 0 0.00 0
2008 RANGE RESOURCES APPALACHIA LLC 2357.75 365 0.00 0 0.00 0
2009 RANGE RESOURCES APPALACHIA LLC 2295.45 365 0.00 0 0.00 0
2010 RANGE RESOURCES APPALACHIA LLC 1,755.59 365 0.00 0 0.00 0
2011 RANGE RESOURCES APPALACHIA LLC 1,385.97 365 0.00 0 0.00 0
2012 RANGE RESOURCES APPALACHIA LLC 398.89 366 0.00 0 0.00 0
2013 RANGE RESOURCES APPALACHIA LLC 304.00 365 0.00 0 0.00 0
2014 RANGE RESOURCES APPALACHIA LLC 1,251.86 365 0.00 0 0.00 0
2015 RANGE RESOURCES APPALACHIA LLC 638.00 365 0.00 0 0.00 0
2016 RANGE RESOURCES APPALACHIA LLC 0.00 0 0.00 0 0.00 0
2017 RANGE RESOURCES APPALACHIA LLC 0.00 0 0.00 0 0.00 0
2018 RANGE RESOURCES APPALACHIA LLC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
1997 RANGE OPR CO Brine 70.00 Bbl Road Spreading OIL CREEK TWP.
1999 RANGE OPR CO Brine 75.00 Bbl Injection Disposal Well 2585201
2004 RANGE RESOURCES APPALACHIA LLC Brine 75.00 Bbl Road Spreading
2006 RANGE RESOURCES APPALACHIA LLC Brine 75.00 Bbl Road Spreading
2008 RANGE RESOURCES APPALACHIA LLC Brine 30.00 Bbl Brine or Industrial Waste Treatment Plt PA0101508
2012 RANGE RESOURCES APPALACHIA LLC Produced Fluid 35.00 Bbl REUSE OTHER THAN ROAD SPREADING
2018 RANGE RESOURCES APPALACHIA LLC Produced Fluid 300.00 Bbl Injection Disposal Well 34-007-21847

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2468855 Primary Facility 2016-03-29 Routine/Partial Inspection No Violations Noted
2772021 Primary Facility 2018-09-07 Plugging(Includes Plugged/Mined Through) No Violations Noted Inspected location, rig and supporting plugging equipment have been setup, crew is getting ready to rig up hot water to pump down on 1 1/2 inch tubing to try to flush out a salt bridge at 3000 feet.
2773145 Primary Facility 2018-09-11 Plugging(Includes Plugged/Mined Through) No Violations Noted Inspected location, rig crew was pulling out tubing at time of inspection, they flushed out salt bridge, wireline will be on location 9/12/18 to cut casing and begin cementing operations.
2774431 Primary Facility 2018-09-13 Plugging(Includes Plugged/Mined Through) No Violations Noted Inspected location, cement crew was pumping bottom plug with 130 sacks of cement, after cement crew pumped cement and flushed lines crew then rigged down to start pulling work string and pipe became stuck in hole, rig crew worked the string for approx 45 minutes and was not able to get work string free, after consulting with company official they are going to let the pipe sit over night then come in with wireline run a bond log then shoot the work string at top of cement then set top plug.
2775021 Primary Facility 2018-09-14 Plugging(Includes Plugged/Mined Through) No Violations Noted Inspected location, when arrived wireline crew was setting up to run bond log, could not get down below 3100', wireline then pulled out and put cutter on and ran down too 3060' and then cut casing then pulled out of hole and rigged down, rig crew then made sure that the pipe was free by pulling up on joint, cement crew then broke circulation and then spotted 100' stub plug, rig crew then pulled up hole and finished setting remaining plugs.
357489 Primary Facility 1988-04-11 Routine/Complete Inspection No Violations Noted
357490 Primary Facility 1989-05-09 Routine/Complete Inspection No Violations Noted
357491 Primary Facility 1989-06-29 Routine/Complete Inspection No Violations Noted
357492 Primary Facility 1989-07-31 Routine/Complete Inspection No Violations Noted

For data sources see[7]

References