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37-033-26681

Well Details

Well ID: 37-033-26681
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Country: United States
State: Pennsylvania
County: Clearfield
Municipality: Lawrence Township
Operator Name: SENECA RESOURCES CO LLC
Well Pad ID: 147030
Farm/Lease Name: PUNXSUTAWNEY HUNTING CLUB 8H
License Status: ACTIVE
Spud Date:
Permit Date: 2008-07-11
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: No
Latitude: 41.171648
Longitude: -78.447156

For data sources see[1][2][3]

Well History

Date Event
2008-07-11 New Permit Application
2009-07-28 Permit Renewal Application
2009-08-05 Performed Spud Operation
2009-09-07 Drilling Completion
2009-11-12 Perforation
2010-06-28 DEVIATED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2008 EOG RESOURCES INC 0.00 0 0.00 0 0.00 0
2009 EOG RESOURCES INC 0.00 0 0.00 0 0.00 0
2010 EOG RESOURCES INC 197,073.62 225 0.00 0 0.00 0
2011 EOG RESOURCES INC 214,484.00 365 0.00 0 0.00 0
2012 EOG RESOURCES INC 220,711.00 366 0.00 0 0.00 0
2013 EOG RESOURCES INC 148,616.00 358 0.00 0 0.00 0
2014 EOG RESOURCES INC 122,931.03 352 0.00 0 0.00 0
2015 EOG RESOURCES INC 111,390.93 365 0.00 0 0.00 0
2016 EOG RESOURCES INC 79,635.46 236 0.00 0 0.00 0
2017 SENECA RESOURCES CO LLC 86,752.38 327 0.00 0 0.00 0
2018 SENECA RESOURCES CO LLC 91,788.62 347 0.00 0 0.00 0
2019 SENECA RESOURCES CO LLC 100,684.48 331 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2010 EOG RESOURCES INC Produced Fluid 3,613.50 Bbl REUSE OTHER THAN ROAD SPREADING
2010 EOG RESOURCES INC Produced Fluid 5,483.50 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0101508
2010 EOG RESOURCES INC Produced Fluid 1,808.50 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0023213
2010 EOG RESOURCES INC Produced Fluid 54.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0095273
2010 EOG RESOURCES INC Produced Fluid 25.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0102784
2011 EOG RESOURCES INC Produced Fluid 200.00 Bbl INJECTION DISPOSAL WELL 34-049-23127
2011 EOG RESOURCES INC Produced Fluid 6,434.00 Bbl REUSE OTHER THAN ROAD SPREADING
2011 EOG RESOURCES INC Produced Fluid 267.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0023213
2011 EOG RESOURCES INC Produced Fluid 1,966.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0101508
2011 EOG RESOURCES INC Produced Fluid 192.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE 34-099-23127
2011 EOG RESOURCES INC Produced Fluid 493.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0095273
2012 EOG RESOURCES INC Produced Fluid 617.00 Bbl INJECTION DISPOSAL WELL 34-155-23584
2012 EOG RESOURCES INC Produced Fluid 4,593.00 Bbl REUSE OTHER THAN ROAD SPREADING
2012 EOG RESOURCES INC Produced Fluid 392.00 Bbl INJECTION DISPOSAL WELL 34-155-21893
2012 EOG RESOURCES INC Produced Fluid 380.00 Bbl INJECTION DISPOSAL WELL 34-155-23795
2012 EOG RESOURCES INC Produced Fluid 285.00 Bbl INJECTION DISPOSAL WELL 34-151-23420
2012 EOG RESOURCES INC Produced Fluid 1,108.00 Bbl STORAGE PENDING DISPOSAL OR REUSE
2012 EOG RESOURCES INC Produced Fluid 689.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE 525-1
2012 EOG RESOURCES INC Produced Fluid 190.00 Bbl INJECTION DISPOSAL WELL 34-007-22038
2013 EOG RESOURCES INC Produced Fluid 130.00 Bbl INJECTION DISPOSAL WELL 34-155-23795
2013 EOG RESOURCES INC Produced Fluid 95.00 Bbl INJECTION DISPOSAL WELL 34-133-20114
2013 EOG RESOURCES INC Produced Fluid 106.80 Bbl INJECTION DISPOSAL WELL 34-151-23420
2013 EOG RESOURCES INC Produced Fluid 95.00 Bbl INJECTION DISPOSAL WELL 34-133-21076
2013 EOG RESOURCES INC Produced Fluid 220.00 Bbl REUSE OTHER THAN ROAD SPREADING
2013 EOG RESOURCES INC Produced Fluid 524.00 Bbl INJECTION DISPOSAL WELL 34-155-23732
2013 EOG RESOURCES INC Produced Fluid 68.00 Bbl INJECTION DISPOSAL WELL 34-155-23203
2013 EOG RESOURCES INC Produced Fluid 68.00 Bbl INJECTION DISPOSAL WELL 34-155-21894
2013 EOG RESOURCES INC Produced Fluid 978.00 Bbl STORAGE PENDING DISPOSAL OR REUSE
2013 EOG RESOURCES INC Produced Fluid 302.00 Bbl INJECTION DISPOSAL WELL 34-155-21438
2013 EOG RESOURCES INC Produced Fluid 723.80 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE WMGR123SW018
2013 EOG RESOURCES INC Produced Fluid 105.00 Bbl INJECTION DISPOSAL WELL 34-155-22403
2013 EOG RESOURCES INC Produced Fluid 68.00 Bbl INJECTION DISPOSAL WELL 34-155-21893
2013 EOG RESOURCES INC Produced Fluid 190.00 Bbl INJECTION DISPOSAL WELL 34-133-24096
2014 EOG RESOURCES INC Produced Fluid 415.00 Bbl INJECTION DISPOSAL WELL 34-155-21438
2014 EOG RESOURCES INC Produced Fluid 199.00 Bbl INJECTION DISPOSAL WELL 34-155-23759
2014 EOG RESOURCES INC Produced Fluid 819.00 Bbl INJECTION DISPOSAL WELL 34-155-23732
2014 EOG RESOURCES INC Produced Fluid 525.00 Bbl INJECTION DISPOSAL WELL 34-155-23795
2014 EOG RESOURCES INC Produced Fluid 950.00 Bbl INJECTION DISPOSAL WELL 34-155-22403
2014 EOG RESOURCES INC Produced Fluid 307.00 Bbl INJECTION DISPOSAL WELL 34-155-21447
2014 EOG RESOURCES INC Produced Fluid 183.30 Bbl INJECTION DISPOSAL WELL 34-155-21893
2014 EOG RESOURCES INC Produced Fluid 183.30 Bbl INJECTION DISPOSAL WELL 34-155-23203
2014 EOG RESOURCES INC Produced Fluid 104.00 Bbl INJECTION DISPOSAL WELL 34-155-23223
2014 EOG RESOURCES INC Produced Fluid 183.30 Bbl INJECTION DISPOSAL WELL 34-155-21894
2015 EOG RESOURCES INC Produced Fluid 105.00 Bbl INJECTION DISPOSAL WELL 34-133-24096
2015 EOG RESOURCES INC Produced Fluid 105.00 Bbl INJECTION DISPOSAL WELL 34-151-23420
2015 EOG RESOURCES INC Produced Fluid 102.50 Bbl INJECTION DISPOSAL WELL 34-155-2-3794
2015 EOG RESOURCES INC Produced Fluid 528.50 Bbl INJECTION DISPOSAL WELL 34-155-23795
2015 EOG RESOURCES INC Produced Fluid 210.00 Bbl INJECTION DISPOSAL WELL 34-155-21438
2015 EOG RESOURCES INC Produced Fluid 615.00 Bbl INJECTION DISPOSAL WELL 34-155-23196
2015 EOG RESOURCES INC Produced Fluid 173.33 Bbl INJECTION DISPOSAL WELL 34-155-21893
2015 EOG RESOURCES INC Produced Fluid 173.33 Bbl INJECTION DISPOSAL WELL 34-155-23203
2015 EOG RESOURCES INC Produced Fluid 410.00 Bbl INJECTION DISPOSAL WELL 34-155-23223
2015 EOG RESOURCES INC Produced Fluid 173.33 Bbl INJECTION DISPOSAL WELL 34-155-21894
2015 EOG RESOURCES INC Produced Fluid 1,147.00 Bbl INJECTION DISPOSAL WELL 34-155-22403
2016 EOG RESOURCES INC Produced Fluid 105.00 Bbl INJECTION DISPOSAL WELL 34-155-22403
2016 EOG RESOURCES INC Produced Fluid 35.00 Bbl INJECTION DISPOSAL WELL 34-155-21894
2016 EOG RESOURCES INC Produced Fluid 322.00 Bbl INJECTION DISPOSAL WELL 34-155-24063
2016 EOG RESOURCES INC Produced Fluid 1,381.00 Bbl INJECTION DISPOSAL WELL 34-133-24462
2016 EOG RESOURCES INC Produced Fluid 35.00 Bbl INJECTION DISPOSAL WELL 34-155-23203
2016 EOG RESOURCES INC Produced Fluid 35.00 Bbl INJECTION DISPOSAL WELL 34-155-21893
2016 EOG RESOURCES INC Produced Fluid 130.00 Bbl REUSE OTHER THAN ROAD SPREADING
2017 SENECA RESOURCES CO LLC Produced Fluid 210.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC003
2017 SENECA RESOURCES CO LLC Produced Fluid 844.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW011
2017 EOG RESOURCES INC Produced Fluid 150.00 Bbl STORAGE PENDING DISPOSAL OR REUSE
2017 EOG RESOURCES INC Produced Fluid 315.00 Bbl INJECTION DISPOSAL WELL 34-155-24063
2017 SENECA RESOURCES CO LLC Produced Fluid 350.00 Bbl REUSE (AT WELL PAD)
2017 SENECA RESOURCES CO LLC Produced Fluid 75.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW005
2017 EOG RESOURCES INC Produced Fluid 415.00 Bbl INJECTION DISPOSAL WELL 34-133-24462
2018 SENECA RESOURCES CO LLC Produced Fluid 225.00 Bbl INJECTION DISPOSAL WELL 34-155-24099
2018 SENECA RESOURCES CO LLC Produced Fluid 1,743.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW011
2018 SENECA RESOURCES CO LLC Produced Fluid 175.00 Bbl REUSE (AT WELL PAD)
2018 SENECA RESOURCES CO LLC Produced Fluid 1,453.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC003
2019 SENECA RESOURCES CO LLC Produced Fluid 110.00 Bbl INJECTION DISPOSAL WELL 34-155-23795
2019 SENECA RESOURCES CO LLC Produced Fluid 110.00 Bbl INJECTION DISPOSAL WELL 34-155-24079
2019 SENECA RESOURCES CO LLC Produced Fluid 250.00 Bbl INJECTION DISPOSAL WELL 34-155-24099
2019 SENECA RESOURCES CO LLC Produced Fluid 110.00 Bbl RESIDUAL WASTE TRANSFER FACILITY WMGR123NC039
2019 SENECA RESOURCES CO LLC Produced Fluid 2,480.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW011
2019 SENECA RESOURCES CO LLC Produced Fluid 110.00 Bbl INJECTION DISPOSAL WELL PAS2D025BELK
2019 SENECA RESOURCES CO LLC Produced Fluid 165.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC003
2019 SENECA RESOURCES CO LLC Produced Fluid 307.00 Bbl REUSE (AT WELL PAD)

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1822534 Primary Facility 2008-08-13 Drilling/Alteration No Violations Noted The following items were noted during the inspection:
1823888 Primary Facility 2009-08-13 Drilling/Alteration No Violations Noted Site inspected with OGI Bruce Jankura. Also spoke with Drilling and Completion Consultant, Kelly Spoonts on site. Conductor pipe and top hole had already been drilled, drilling of horizontal section was in progress. All disturbed areas have been seeded and mulched with about 45% vegetation already grown back in. Site has brush row reinforced with line of silt fence surrounding parameter. All E&S control BMPs have been installed properly and are working adequately. The pit is constructed and lined properly. Liner appears sound with no visible cuts or punctures. More than 2ft of freeboard is being maintained
1824644 Primary Facility 2009-08-27 Complaint Inspection No Violations Noted Site was inspected from perimeter of pad. In response to complaint #265864, Alex branch was field tested from just below McGregor Rd Crossing to headwaters. Stream begins approximately 700 Ft from edge of well pad. Meter readings indicated elevated TDS and Conductivity here. Pit appears sound. A properly installed sediment fence reinforced with haybales follows the edge of the pad. The are no signs of erosion or that any fluids have left the site on the surface. Inspection was conducted jointly with the following personel from the PA Fish and Boat Commission: Waterways Conservation Officer, Robert V. Dunbar, Fisheries Biologists, Steven Kepler and Heather Smiles. Officer Dunbar spoke with Matt Williams on-site. Mr. Williams mentioned that the well had low water returns.
1829048 Primary Facility 2009-09-04 Routine/Partial Inspection Violation(s) Noted Miller - on-site meeting w/EOG & PaFBC reps, multiple investigations between 8/25/09 & 9/4/09 resulted in determination that activities at this well site released contaminants from Marcellus shale drilling to atmosphere, written response requested w/in 10 days. See 401CSL violation comment. NOV to MBC for input 9/21, insp not previously input. MBC 9/21/09
1829540 Primary Facility 2009-09-10 Follow-up Inspection No Violations Noted Site was inspected with Nathan Wells, Tom McNerney and Caleb Woolever. Pit had been excavated and all recovered materials placed in 9 containers that have been covered and stored on-site until approval has been aquired to haul them to landfill. A water truck comes every other day to pull any water produced from contents. Pit has been backfilled with cleanfill. Field testing shows TDS, conductivity and pH levels in stream originating about 700' from pad have improved significantly. Casing being run on day of inspection, no E&S problems at this time
1833329 Primary Facility 2009-09-30 Drilling/Alteration No Violations Noted -No activity on site at this time. Fraccing tanks were being staged further up the access road (on remaing pad of #3H)
1834892 Primary Facility 2009-09-30 Drilling/Alteration No Violations Noted The following items were noted during the inspection:
1836100 Primary Facility 2009-10-14 Drilling/Alteration Violation(s) Noted Spill response: Monday, October 12, 2009 Joe Wilson, independent consultant, noticed spring behind 8H was cloudy and sudsy. EOG was notified and found that a gasket on one of the holding tanks had gone bad. approx. 190 bbls of fluids were unaccounted for. There was no indication of a spill on-site. Fluid containing about 98% fresh water, 1.06% well wash and .25% ultra vis, soaked into the pad and made its way to the nearby stream. The stream had booms placed in it and the water was being pumped out to be contained on site. Suds were seen as far down as Camp Read. EOG also flushed the area a couple of times with fresh water. They will continue to monitor the stream quality and flush if necessary. Greg Shaffer, of EOG along with Joe wilson were on site during the inspection. Representatives of the Fish and Boat Commission were also present
1836167 Primary Facility 2009-10-19 Follow-up Inspection Outstanding Violations - No Viols Req'd -Site inspected with WQS Supervisor John Ryder and Geologic Trainee Caleb Woolever. Joe Wilson was conducting routine sampling at the Spring affected by the recent spill.
1851110 Primary Facility 2009-12-15 Routine/Complete Inspection No Violations Noted - Inpsection conducted with WQS Sam Jones. Drilling complete and there are no related activities on site at this time. A small crew was on-site pumping water amongst tanks.
1852738 Primary Facility 2009-12-29 Routine/Complete Inspection No Violations Noted Conducted Inspection with WQS Jessica MIller and WQS Heather Agosta.
1853885 Primary Facility 2009-12-29 Routine/Complete Inspection No Violations Noted -Inspection Conducted with OGI Travis and WQS from Altoona, Heather Agosta.
1884384 Primary Facility 2010-05-12 Routine/Complete Inspection De minimus Violations Noted Production well in line with digital meter. Well tag did not have permit number, I informed the well tender, and he will replace.
1907334 Primary Facility 2010-08-16 Routine/Complete Inspection No Violations Noted
1919583 Primary Facility 2010-09-27 Site Restoration No Violations Noted
1954461 Primary Facility 2011-03-02 Routine/Complete Inspection No Violations Noted
2476658 Primary Facility 2016-04-19 Routine/Complete Inspection No Violations Noted
2851562 Primary Facility 2019-02-21 Routine/Complete Inspection No Violations Noted The weather is 34 Deg. F and sunny at time of inspection. Routine inspection of Seneca Resources Corp., D16-PHC-N Pad, Well # 8H on February 21, 2019. There is 1 active well on this pad.

This well is open and producing at the time of inspection. Annular vent (7-5/8" x 4-1/2") is open and plumed to the tank. 0% combustible gas was detected in the area immediately surrounding the well. Production tubing pressure is 217 PSI, backside casing pressure 252 PSI. Production processing equipment on location includes 1 production water tank, 1 gas processing unit, measurement equipment ¿ orifice meter stations. No obvious concerns or violations are noted at time of inspection. Wellsite looks neat and well organized. Seneca Resources Corp. Representative - Stephen Gus Simpson, Roustabout Foreman. DEP Representative - Ulyana Trynovich, Oil and Gas Inspector.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
1829048 571760 09/04/2009 2009-09-04 401 CSL - Discharge of pollultional material to waters of Commonwealth. Environmental Health & Safety Integrity issues at pit on-site most likely cause of release to Alex Branch the headwaters w/in 700 ft of well pad, elevated barium, strontium and chloride levels detected.
1836100 573592 10/14/2009 2009-10-14 301CSL - Stream discharge of IW, includes drill cuttings, oil, brine and/or silt Environmental Health & Safety
1836100 573593 10/14/2009 2009-10-14 401 CSL - Discharge of pollultional material to waters of Commonwealth. Environmental Health & Safety

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
571760 250279 NOV - Notice of Violation Comply/Closed 2010-08-31
571760 261736 CACP - Consent Assessment of Civil Penalty Comply/Closed 2010-08-31 2010-08-31 $30,000.00 $30,000.00
573592 251709 NOV - Notice of Violation Comply/Closed 2010-08-31
573592 261736 CACP - Consent Assessment of Civil Penalty Comply/Closed 2010-08-31 2010-08-31 $30,000.00 $30,000.00
573593 251709 NOV - Notice of Violation Comply/Closed 2010-08-31
573593 261736 CACP - Consent Assessment of Civil Penalty Comply/Closed 2010-08-31 2010-08-31 $30,000.00 $30,000.00

For data sources see[7]

References