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37-033-26614

Well Details

Well ID: 37-033-26614
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Country: United States
State: Pennsylvania
County: Clearfield
Municipality: Brady Township
Operator Name: ALLIANCE PETRO CO LLC
Well Pad ID:
Farm/Lease Name: WILLIAM F MOORE 7
License Status: ACTIVE
Spud Date:
Permit Date: 2008-03-06
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 41.060022
Longitude: -78.729349

For data sources see[1][2][3]

Well History

Date Event
2008-03-06 New Permit Application
2008-05-08 Drilling Completion
2008-05-12 Perforation
2008-05-16 Performed Spud Operation
2009-10-22 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2008 CONSOL GAS CO 4135.69 365 0.00 0 0.00 0
2009 CONSOL GAS CO 3264.48 365 0.00 0 0.00 0
2010 CONSOL GAS CO 1,578.00 365 0.00 0 0.00 0
2011 CONSOL GAS CO 0.00 0 0.00 0 0.00 0
2012 CNX GAS CO LLC 387.00 366 0.00 0 0.00 0
2013 CNX GAS CO LLC 28.73 365 0.00 0 0.00 0
2014 CNX GAS CO LLC 18.54 365 0.00 0 0.00 0
2015 CNX GAS CO LLC 387.6 365 0.00 0 0.00 0
2016 CNX GAS CO LLC 280.7 366 0.00 0 0.00 0
2017 CNX GAS CO LLC 331.10 365 0.00 0 0.00 0
2018 CNX GAS CO LLC 100.00 365 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2008 CONSOL GAS CO Fracking Fluid 150.00 Bbl Brine or Industrial Waste Treatment Plt PA0095443
2008 CONSOL GAS CO Brine 271.04 Bbl Brine or Industrial Waste Treatment Plt PA0026034
2008 CONSOL GAS CO Brine 298.00 Bbl Brine or Industrial Waste Treatment Plt PA0091472
2009 CONSOL GAS CO Brine 255.00 Bbl Municipal Sewage Treatment Plant PA0026034
2009 CONSOL GAS CO Brine 95.00 Bbl Brine or Industrial Waste Treatment Plt PA0091472
2009 CONSOL GAS CO Brine 167.00 Bbl Injection Disposal Well PA101656
2010 CONSOL GAS CO Produced Fluid 61.15 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0020346
2010 CONSOL GAS CO Produced Fluid 96.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0028428
2011 CNX GAS CO LLC Produced Fluid 80.23 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0020346
2011 CNX GAS CO LLC Produced Fluid 57.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE 34-099-23127
2012 CNX GAS CO LLC Produced Fluid 43.00 Bbl Injection Disposal Well 34-007-22038
2013 CNX GAS CO LLC Produced Fluid 12.00 Bbl Injection Disposal Well 34-119-28776

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1706027 Primary Facility 2008-05-09 Drilling/Alteration No Violations Noted drilling complete, pit, e/s ok
1706028 Primary Facility 2008-05-07 Drilling/Alteration No Violations Noted waiting on cement
1709725 Primary Facility 2008-05-14 Drilling/Alteration No Violations Noted fracing with BJ well services
2787757 Primary Facility 2018-09-24 Routine/Complete Inspection No Violations Noted The weather is 65 Deg. F and cloudy at the time of inspection. Routine inspection of Diversified Oil & Gas, LLC., William F. Moore Pad, Well # 7 on September 24, 2018. There is 1 active well on this pad. Annular vent (7" x 4-1/2") was open and not vented. 0% combustible gas was detected at the annulus. Detected gas leak on the consumer meter line, 100% LEL and 10% combustible gas.

No violation noted at time of inspection, but will require follow up inspection after gas leak is fixed. DEP Representative - Ulyana Trynovich, Oil and Gas Inspector.

2803482 Primary Facility 2018-10-29 Follow-up Inspection No Violations Noted The weather is 50 Deg. F and cloudy at the time of inspection. Follow up inspection of CNX Gas Co. LLC. (Diversified O&G, LLC. is currently operating this well), William Moore Pad, Well # 7 on October 29, 2018. There is 1 active and producing well on this pad.

Annular vent (7" x 4-1/2") was closed at the time of inspection. 0% combustible gas was detected in the area immediately surrounding the well. Gas leak that was detected on the meter line on 09/24/2018 is fixed. No violation noted at time of inspection. DEP Representatives - Ulyana Trynovich, Oil and Gas Inspector; Sue Herzing ¿ Water Quality Specialist. Diversified O&G. LLC. (PA Production) ¿ Justin Ford, Well Tender.

For data sources see[7]

References