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37-027-21427

Well Details

Well ID: 37-027-21427
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Country: United States
State: Pennsylvania
County: Centre
Municipality: Burnside Township
Operator Name: DIVERSIFIED OIL & GAS LLC
Well Pad ID:
Farm/Lease Name: GULF USA 176-CEN
License Status: ACTIVE
Spud Date:
Permit Date: 2007-06-05
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 41.070426
Longitude: -77.972941

For data sources see[1][2][3]

Well History

Date Event
2007-06-05 New Permit Application
2007-07-17 Drilling Completion
2007-07-24 Perforation
2007-10-26 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2007 TEXAS KEYSTONE INC 119.00 22 0.00 0 0.00 0
2008 TEXAS KEYSTONE INC 171.00 61 0.00 0 0.00 0
2009 TEXAS KEYSTONE INC 60.00 16 0.00 0 0.00 0
2010 TEXAS KEYSTONE INC 130.00 27 0.00 0 0.00 0
2011 TEXAS KEYSTONE INC 0.00 0 0.00 0 0.00 0
2012 TEXAS KEYSTONE INC 3.00 2 0.00 0 0.00 0
2013 TEXAS KEYSTONE INC 63.00 18 0.00 0 0.00 0
2014 TEXAS KEYSTONE INC 25.00 9 0.00 0 0.00 0
2015 TEXAS KEYSTONE INC 3.00 1 0.00 0 0.00 0
2016 DIVERSIFIED OIL & GAS LLC 57.00 7 0.00 0 0.00 0
2017 DIVERSIFIED OIL & GAS LLC 53.00 4 0.00 0 0.00 0
2018 DIVERSIFIED OIL & GAS LLC 53.00 365 0.00 0 0.00 0
2019 DIVERSIFIED OIL & GAS LLC 1,002.00 276 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2016 DIVERSIFIED OIL & GAS LLC Produced Fluid 25 Bbl CENT WASTE TRT FAC NPDES PA0095273
2016 DIVERSIFIED OIL & GAS LLC Produced Fluid 25.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095273

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2488533 Primary Facility 2016-05-25 Routine/Complete Inspection No Violations Noted
2493386 Primary Facility 2016-06-09 Routine/Complete Inspection No Violations Noted Evidence of a brine leak from dump line at the brine tank- staining on tank under line, distressed (or no) vegetation around tank, straw placed around tank, and a small puddle of water (< 1 gallon) tested for conductance showed 1866µS/cm. Pending inspection result awaiting response from Diversified. Update: 1.29 tons of soil removed, disposed of at Greentree Landfill on 8/23/2016.

For data sources see[7]

References