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37-015-21126

Well Details

Well ID: 37-015-21126
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Country: United States
State: Pennsylvania
County: Bradford
Municipality: Ridgebury Township
Operator Name: EOG RESOURCES INC
Well Pad ID: 146312
Farm/Lease Name: MICCIO 1H
License Status:
Spud Date:
Permit Date: 2010-08-24
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: No
Latitude: 41.974058
Longitude: -76.735144

For data sources see[1][2][3]

Well History

Date Event
2010-08-24 New Permit Application
2011-01-29 Performed Spud Operation
2013-06-27 Perforation
2013-10-15 DEVIATED

For data sources see[4]

Fracking Activities

Fracking Jobs

Job Number Job Start Date Job End Date True Vertical Depth (ft) Total Water Volume (gal) Total Non-Water Volume (gal)
1 2011-08-04 2011-08-04 4,398 89,250
2 2013-07-12 2013-07-12 4,398 6,194,960 0

Fluid Composition Data

Job Number Trade Name Supplier Purpose Ingredient Name CAS Number Additive Percentage by Mass Job Percentage by Mass Mass Used (lb)
1 Interstate ICA-2 Iron Control
Ethylene glycol 107-21-1 60.00 0.00227000
D-Gluconic acid 526-95-4 10.00 0.00038000
Water 7732-18-5 60.00 0.00227000
Water EOG Resources Carrier/Base Fluid
Water 7732-18-5 100.00 90.94
Plexslick 921E Chemplex Friction Reducer for Water
Distillates, petroleum, hydrotreated light 64742-47-8 30.00 0.01
SCALE CLEAR SI 112 Weatherford Scale Inhibitor
Ethylene glycol 107-21-1 40.00 0.01
BioClear 1000 Biocide
2,2-Dibromo-3-nitrilopropionamide 10222-01-2 100.00 0.00260000
Sand EOG Resources Proppant
Quartz 14808-60-7 100.00 5.13
ENVIROHIB 2001 Corrosion Inhibitor Ethylene glycol 107-21-1 60.00 0.00236000
Cinnamaldehyde (3-phenyl-2-propenal) 104-55-2 40.00 0.00157000
Formic acid 64-18-6 40.00 0.00157000
2-Butoxyethanol 111-76-2 40.00 0.00157000
Hydrochloric Acid Basic Chemical Solutions Acid Hydrochloric acid 7647-01-0 7.50 0.28
2 Alpha 1427 Baker Hughes Biocide Didecyl dimethyl ammonium chloride 7173-51-5 10 0.0012 0
Glutaraldehyde 111-30-8 30 0.0036 0
Quaternary ammonium compound 68424-85-1 5 0.0006 0
Ethanol 64-17-5 5 0.0006 0
FERROTROL 300L Baker Hughes Iron Control Citric acid 77-92-9 60 0.00165 0
Water EOG Carrier/Base Fluid Water 7732-18-5 100 83.709 0
Hydrochloric Acid Baker Hughes Acid Hydrochloric Acid 7647-01-0 7.5 0.09501 0
Sand EOG Proppant Crystalline Silica 14808-60-7 100 14.9532 0
FRW-18 Baker Hughes Friction Reducer Petroleum distillates 64742-47-8 30 0.01198 0
CI-14 Baker Hughes Corrosion Inhibitor Olefin Trade Secret 5 0.0001 0
Polyoxyalkylenes Trade Secret 30 0.00057 0
Fatty acids Trade Secret 10 0.00019 0
Methanol 67-56-1 100 0.0019 0
Propargyl alchol 107-19-7 5 0.0001 0
SCALETROL 720 Baker Hughes Scale Inhibitor Ethylene Glycol 107-21-1 30 0.00432 0
Calcium Chloride (CaCl2) 10043-52-4 5 0.00072 0

For data sources see[5]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2010 EOG RESOURCES INC 0.00 0 0.00 0 0.00 0
2011 EOG RESOURCES INC 0.00 0 0.00 0 0.00 0
2012 EOG RESOURCES INC 0.00 0 0.00 0 0.00 0
2013 EOG RESOURCES INC 0.00 0 0.00 0 0.00 0
2014 EOG RESOURCES INC 0.00 0 0.00 0 0.00 0
2015 EOG RESOURCES INC 0.00 0 0.00 0 0.00 0
2016 EOG RESOURCES INC 0.00 0 0.00 0 0.00 0
2017 EOG RESOURCES INC 0.00 0 0.00 0 0.00 0
2019 EOG RESOURCES INC 0.00 0 0.00 0 0.00 0

For data sources see[6]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2011 EOG RESOURCES INC Drill Cuttings 1,182.55 Tons LANDFILL 31346244
2013 EOG RESOURCES INC Fracturing Fluid Waste 121.90 Tons LANDFILL 301358
2013 EOG RESOURCES INC Fracing Fluid Waste 237.00 Bbl STORAGE PENDING DISPOSAL OR REUSE
2013 EOG RESOURCES INC Fracing Fluid Waste 5,608.80 Bbl REUSE OTHER THAN ROAD SPREADING
2017 EOG RESOURCES INC Produced Fluid 50.00 Bbl STORAGE PENDING DISPOSAL OR REUSE

For data sources see[7]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1947309 Primary Facility 2011-02-03 Drilling/Alteration No Violations Noted
2039208 Primary Facility 2012-02-02 Complaint Inspection No Violations Noted
2153228 Primary Facility 2013-03-29 Routine/Complete Inspection No Violations Noted
2174334 Primary Facility 2013-06-11 Routine/Complete Inspection No Violations Noted
2180039 Primary Facility 2013-06-18 Routine/Complete Inspection No Violations Noted
2277896 Primary Facility 2014-05-22 Routine/Complete Inspection Violation(s) Noted VIOL 78.73(b) - failure to gas below casing seat from entering fresh gw; VIOL 78.81(a)(2) - failure to prevent gas migration to fresh gw; VIOL 78.81(a)(5) - failure to prevent gas flow in annulus.
2318802 Primary Facility 2014-11-03 Site Restoration No Violations Noted The Department inspected the Miccio A Well Pad, permit #ESX10-015-0297; well permit #37-015-21126 in Ridgebury Twp., Bradford Co. on 11/3/14 @ 1200 hours. The weather was 52° overcast. The Notice of Termination was received by the NCRO on 9/22/14; the well restoration report was received by the NCRO on 12/2/13. This inspection complies with 25 PA Code §102.22. No violations issued during this inspection. Approval of the Notice of Termination is recommended at this time. The Well Site Restoration Report for permit# 37-015-21126 is approved at this time.
2377510 Primary Facility 2015-04-22 Follow-up Inspection Outstanding Violations - No Viols Req'd
2404554 Primary Facility 2015-07-29 Routine/Complete Inspection Outstanding Violations - No Viols Req'd Annular vents separtely piped to polytank. Intermediate x production annulus 60% methane.
2645923 Primary Facility 2017-10-11 Routine/Complete Inspection No Violations Noted Inspection to assess overall site conditions. No issues noted and no violations cited.
2704337 Primary Facility 2018-01-10 Routine/Complete Inspection Outstanding Violations - Viols Req'd At time of inspection the annulus vents were vented to plastic barrels on location.

Collected gas samples from the production annulus and the surface annulus vents.


    • The violation code for 25 Pa. Code § 78.81(a)(2) was updated on May 6, 2019 because this violation code was not available in eFACTS when this inspection record was created. This violation was previously listed as §78.81D2, which was the closest violation code available in eFACTS to the actual violation at the time. Although this is an unconventional gas well currently subject to the Rules and Regulations of 25 Pa. Code §78a, the violation was originally cited in 2014 and the §78a regulations were not effective until October 2016. Therefore, to avoid confusion, the outstanding violation will remain as initially cited (§78.81(a)(2) instead of §78a.81(a)(2)) until it is either superseded or resolved. ** ~CMB~
    • The violation code for 25 Pa. Code § 78.85(a)(5) was updated on May 6, 2019 because this violation code was not available in eFACTS
2721607 Primary Facility 2018-04-23 Routine/Partial Inspection No Violations Noted I took electrical conductivity readings of standing liquid on site with an Oakton PCSTestr 35. A puddle on the pad gave a 0.51 mS/cm reading. I took combustible gas readings from the 3 annulus vents on the Marcellus well head: the vent pipe marked "prod" gave a 26% methane reading, the vents marked "inter" & "surf" gave 0% LEL & 0% methane readings. Air temp 67F. JLP
2735252 Primary Facility 2018-05-21 Routine/Complete Inspection Outstanding Violations - Viols Req'd Reason for inspection is to meet with EOG to collect gas samples from each of the annulus vent and perform A 72hour PBUT. On location with Caleb Woolever (PADEP), Clayton Schucker (Moody and associates), and Ed Sicora (EOG). PBUT VALVES CLOSED AT 13:18 pm. 2,220 psi production casing.
    • The violation code for 25 Pa. Code § 78.81(a)(2) was updated on May 6, 2019 because this violation code was not available in eFACTS when this inspection record was created. This violation was previously listed as §78.81D2, which was the closest violation code available in eFACTS to the actual violation at the time. Although this is an unconventional gas well currently subject to the Rules and Regulations of 25 Pa. Code §78a, the violation was originally cited in 2014 and the §78a regulations were not effective until October 2016. Therefore, to avoid confusion, the outstanding violation will remain as initially cited (§78.81(a)(2) instead of §78a.81(a)(2)) until it is either superseded or resolved. ** ~CMB~
    • The violatio
2743162 Primary Facility 2018-06-19 Routine/Partial Inspection No Violations Noted I got electrical conductivity readings from standing liquid on site. A puddle on the pad was 0.42 mS/cm today. JLP
2816475 Primary Facility 2018-12-12 Administrative/File Review Violation(s) Noted Administrative inspection created to cite violations and create an Enforcement Record (Enforcement ID 370481) for a December 12, 2018 NOV sent to EOG regarding impacts to five private water supplies in Ridgebury Township, Bradford County. A copy of the NOV is attached to this Admin Inspection record. See also Admin Inspection record #2816514.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
2277896 698018 05/22/2014 2014-05-22 78.73B - Excessive casing seat pressure Administrative
2277896 698019 05/22/2014 2014-05-22 78.81D2 - Failure to case and cement properly through storage reservoir or storage horizon Administrative
2277896 698020 05/22/2014 2014-05-22 78.85 - Inadequate, insufficient, and/or improperly installed cement Environmental Health & Safety
2704337 812051 2018-01-10 78.85(a)5 Environmental Health & Safety
2704337 812052 2018-01-10 78.81(a)2 Environmental Health & Safety
2704337 812053 2018-01-10 78.73(b) Environmental Health & Safety
2735252 819622 2018-05-21 78.73(b) Environmental Health & Safety
2735252 819623 2018-05-21 78.85(a)5 Environmental Health & Safety
2735252 819624 2018-05-21 78.81(a)2 Environmental Health & Safety
2816475 836559 2018-12-12 78a86 Environmental Health & Safety
2816475 836560 2018-12-12 78a91(a) Environmental Health & Safety

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
698018 313122 NOV - Notice of Violation
698019 313122 NOV - Notice of Violation
698020 313122 NOV - Notice of Violation
836559 370481 NOV - Notice of Violation
836560 370481 NOV - Notice of Violation

For data sources see[8]

References