X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

37-007-20297

Well Details

Well ID: 37-007-20297
Loading map...
Country: United States
State: Pennsylvania
County: Beaver
Municipality: Franklin Township
Operator Name: EQT PROD CO
Well Pad ID: 149612
Farm/Lease Name: YMCA 590433
License Status:
Spud Date:
Permit Date: 2010-02-02
Well Type: GAS
Unconventional Well: Y
Configuration: Vertical Well
Conservation: Yes
Latitude: 40.813922
Longitude: -80.208025

For data sources see[1][2][3]

Well History

Date Event
2010-02-02 New Permit Application
2010-03-03 Performed Spud Operation
2010-03-15 Drilling Completion
2010-08-09 DEVIATED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2010 EQT PROD CO 0.00 0 0.00 0 0.00 0
2011 EQT PROD CO 0.00 0 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2010 EQT PROD CO Drilling Fluid Waste 1,410.00 Bbl IDENTIFY METHOD IN COMMENTS
2010 EQT PROD CO Drilling Fluid Waste 20.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0091472
2010 EQT PROD CO Drilling Fluid Waste 870.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE 301353

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1869545 Primary Facility 2010-03-10 Drilling/Alteration No Violations Noted HIGHLANDS RIG 4 DRILLING TOP HOLE FOR THIS MARCELLUS WELL.
1869551 Primary Facility 2010-03-04 Drilling/Alteration No Violations Noted SUPERIOR CEMENTING 133/8" CASING. MARCELLUS WELL.
1882760 Primary Facility 2010-03-29 Drilling/Alteration No Violations Noted TOP HOLE COMPLETE. RIG AND SUPPORT EQUIPTMENT GONE. SITE, E&S, & ACCESS, OK.
1882772 Primary Facility 2010-04-05 Drilling/Alteration No Violations Noted SERVICE RIG IS UP. WELL WILL BE PERFED AT 5160'. HORIZONTAL PART OF WELL WILL NOT BE DRILLED.
1882798 Primary Facility 2010-04-21 Drilling/Alteration No Violations Noted DRILLING COMPLETE. WELL WILL REMAIN VERTICAL. PIT WAS DRAINED, SOLIDIFIED, AND BURIED.
1883284 Primary Facility 2010-04-29 Routine/Complete Inspection No Violations Noted On April 29, 2010 I visited this site as a routine inspection. The well was drilled but not yet in production. The well site appeared to be in compliance. A site ID sign and E&S plan were posted on site. The access road was in good condition. E&S controls were in place according to the plan on site. There was no evidence of spills or leaks and no accelerated erosion was observed at the time of inspection. The operator should continue to inspect the E&S controls routinely and after each runoff event until the site has reached uniform 70% vegetative cover.
1913145 Primary Facility 2010-08-10 Routine/Complete Inspection No Violations Noted THIS MARCELLUS SITE IS RESTORED, VEGETATED, AND FENCED. THE ACCESS IS STONED.
1928579 Primary Facility 2010-10-06 Routine/Complete Inspection No Violations Noted On October 6th, 2010 I visited this site as a routine inspection. The well was drilled but not yet in production. The well site appeared to be in compliance. A site ID sign and E&S plan were posted on site. The access road was in good condition. E&S controls were in place according to the plan on site. There was no evidence of spills or leaks and no accelerated erosion was observed at the time of inspection. The operator should continue to inspect the E&S controls routinely and after each runoff event until the site has reached uniform 70% vegetative cover. The site was well vegetated and surrounded by security fence.
2016831 Primary Facility 2011-10-28 Plugging(Includes Plugged/Mined Through) No Violations Noted SERVICE RIG AND SUPPORT EQUIPTMENT SET UP, BUT THERE IS NO ACTIVITY.
2016862 Primary Facility 2011-10-18 Plugging(Includes Plugged/Mined Through) No Violations Noted WELL IS TO BE PLUGGED. NO RIG OR EQUIPTMENT ON THE PAD.
2018674 Primary Facility 2011-11-08 Plugging(Includes Plugged/Mined Through) No Violations Noted HYDROCARBON WELL SERVICES RUNNING TUBING TO SET CEMENT PLUGS.
2023015 Primary Facility 2011-11-15 Plugging(Includes Plugged/Mined Through) No Violations Noted HYDROCARBON JACKING 4080' OF 5.5" CASING. THIS IS A VERTICLE MARCELLUS WELL.
2064338 Primary Facility 2012-04-17 Plugging(Includes Plugged/Mined Through) No Violations Noted EXCAVATION AROUND WELL WAS FILLED WITH WATER AND NO BUBBLES CAN BE SEEN.
2064347 Primary Facility 2012-04-25 Plugging(Includes Plugged/Mined Through) No Violations Noted WELL IS PLUGGED. MEETING WITH EQT AND YMCA TO DISCUSS THE FUTURE OF THE VENT .
2064364 Primary Facility 2012-04-16 Plugging(Includes Plugged/Mined Through) No Violations Noted AT WELL WITH HYDROCARBON STEVE JONES TO TRY AND FIND SOURCE OF BUBBLES.THE WELL HEAD IS EXCAVATED TO HELP.
2121625 Primary Facility 2012-12-05 Routine/Complete Inspection No Violations Noted John Ley WQS, SWRO was on site to conduct a routine inspection. At the time of this inspection, the well sign was onsite. The well was drilled and there was a vent pipe on site. Bmp's installed were functioning. No accelerated erosion or sedimentation issues were noted on site or the access road. The hillsides had been stabilized and had good growth with at least 70% vegetation.
2169316 Primary Facility 2013-05-20 Plugging(Includes Plugged/Mined Through) No Violations Noted WHEN WEL WAS PLUGGED IN 2011 GAS WAS DETECTED IN THE GROUND AROUND THE WELL. THE VENT WAS CHECKED FOR GAS FROM 5/4/12 TILL 7/20/12. % OF LEL RANGED FROM 6.0% TO 20.0%. ON THIS DAY THE % OF LEL WAS 9.0. THE SOURCE OF THE GAS HAS NOT BEEN DETERMINED.

For data sources see[7]

References