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37-005-30535

Well Details

Well ID: 37-005-30535
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Country: United States
State: Pennsylvania
County: Armstrong
Municipality: Redbank Township
Operator Name: DANNIC ENERGY CORP
Well Pad ID:
Farm/Lease Name: ROCCO 1
License Status:
Spud Date:
Permit Date: 2010-01-11
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.928489
Longitude: -79.223638

For data sources see[1][2][3]

Well History

Date Event
2010-01-11 New Permit Application
2010-11-17 Performed Spud Operation

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2008 DANNIC ENERGY CORP 0.00 0 0.00 0 0.00 0
2009 DANNIC ENERGY CORP 0.00 0 0.00 0 0.00 0
2010 DANNIC ENERGY CORP 0.00 0 0.00 0 0.00 0
2011 DANNIC ENERGY CORP 0.00 0 0.00 0 0.00 0
2012 DANNIC ENERGY CORP 0.00 0 0.00 0 0.00 0
2013 DANNIC ENERGY CORP 8.1 273 0.00 0 0.00 0
2014 DANNIC ENERGY CORP 7,345.00 273 0.00 0 0.00 0
2015 DANNIC ENERGY CORP 4,414.44 365 0.00 0 0.00 0
2016 DANNIC ENERGY CORP 3,371.00 366 0.00 0 0.00 0
2017 DANNIC ENERGY CORP 921.00 365 0.00 0 0.00 0
2018 DANNIC ENERGY CORP 405.38 365 0.00 0 0.00 0
2019 DANNIC ENERGY CORP 78.08 61 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2014 DANNIC ENERGY CORP Produced Fluid 1,690.00 Bbl PUBLIC SEWAGE TREATMENT PLANT PA0028428
2014 DANNIC ENERGY CORP Produced Fluid 475.00 Bbl PUBLIC SEWAGE TREATMENT PLANT PA0020346
2015 DANNIC ENERGY CORP Produced Fluid 3,360.00 Bbl PUBLIC SEWAGE TREATMENT PLANT PA0028428

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1929226 Primary Facility 2010-11-22 Routine/Complete Inspection No Violations Noted Drilling was ongoing at the time of the inspection. Below grade drill pit located onsite and it had more than the required two feet of lined freeboard. Noted that a large portion of the access road was located on disturbed acreage associated with an ongoing mining operation. Observed no accelerated erosion & sedimentation in relation to the access road related solely to the well and the site. All erosion controls had been implemented as outlined in the E&S plan.
2483347 Primary Facility 2016-05-09 Routine/Complete Inspection No Violations Noted Well tagged-in production. Well head casing-equipment-100 bbl plastic tank look ok.
2717082 Primary Facility 2018-04-11 Routine/Complete Inspection No Violations Noted This well is tagged and in production. The annulus is shut. The well head casing, piping, production equipment and 100 bbl plastic fluid collection tank look ok.

For data sources see[7]

References