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37-005-30345

Well Details

Well ID: 37-005-30345
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Country: United States
State: Pennsylvania
County: Armstrong
Municipality: Kittanning Township
Operator Name: ALLIANCE PETRO CO LLC
Well Pad ID:
Farm/Lease Name: DANIEL MILLER 4
License Status:
Spud Date:
Permit Date: 2009-04-28
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.740850
Longitude: -79.481414

For data sources see[1][2][3]

Well History

Date Event
2009-04-28 New Permit Application
2009-05-27 Drilling Completion
2009-07-21 Performed Spud Operation
2009-08-03 Perforation
2009-10-30 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2009 PHILLIPS EXPLORATION INC 5868.00 365 0.00 0 0.00 0
2010 PHILLIPS EXPLORATION INC 9,284.00 356 0.00 0 0.00 0
2011 PHILLIPS EXPLORATION INC 13,658.00 364 0.00 0 0.00 0
2012 XTO ENERGY INC 10,881.00 366 0.00 0 0.00 0
2013 XTO ENERGY INC 13,300.00 365 0.00 0 0.00 0
2014 XTO ENERGY INC 7,029.00 309 0.00 0 0.00 0
2015 XTO ENERGY INC 10,817.01 365 0.00 0 0.00 0
2016 XTO ENERGY INC 6,355.00 366 0.00 0 0.00 0
2017 ALLIANCE PETRO CO LLC 6,253.00 334 0.00 0 0.00 0
2018 ALLIANCE PETRO CO LLC 11,816.00 365 0.00 0 0.00 0
2019 ALLIANCE PETRO CO LLC 4,671.00 334 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2013 XTO ENERGY INC Produced Fluid 55.00 Bbl PUBLIC SEWAGE TREATMENT PLANT PA0020346
2018 ALLIANCE PETRO CO LLC Produced Fluid 36.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095273

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1816001 Primary Facility 2009-07-21 Drilling/Alteration No Violations Noted spud notif. 7-2-09 - well not drilled/site made - E&S ok
1817843 Primary Facility 2009-07-28 Routine/Complete Inspection No Violations Noted Drilling was completed at the time of the inspection. Below grade pit located onsite had more than the two feet of required freeboard. Observed no accelerated erosion & sedimentation in relation to the access road or well-site. It was noted that the culverts and associated erosion control BMP's had not been compromised. The culvert inlets had been clogged with sediment and would not function properly.
1836020 Primary Facility 2009-10-15 Routine/Complete Inspection No Violations Noted Drilling had been completed and the well appeared to be equipped for production at the time of the inspection. Fill slope had been stabilized with rock, and the filter fabric fence appeared to be holding in place and continuing to function properly. Cut slope had not been stabilized, and the site had not been regraded. In addition the below grade pit was located onsite. The pit had more than the required two feet of lined freeboard, but it appeared surface runoff had been flowing into the pit. The Department recommends that the operator dispose of the cuttings contained in the pit in accodance with the regulations set forth in Chapter 78, regrade the site and implement temporary BMP's to minimize accelerated erosion & sedimentation until final restoration activities can be completed.
2818896 Primary Facility 2018-12-17 Routine/Complete Inspection No Violations Noted This well is tagged and in production with the annulus open. The well head casing, piping, equipment and 100 bbl plastic fluid collection tank look ok.

For data sources see[7]

References