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37-005-20720

Well Details

Well ID: 37-005-20720
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Country: United States
State: Pennsylvania
County: Armstrong
Municipality: Wayne Township
Operator Name: CNX GAS CO LLC
Well Pad ID:
Farm/Lease Name: NANNIE D MOORE 1
License Status: Plugged and Abandoned
Spud Date: 1964-09-17
Permit Date: 1964-09-16
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.870481
Longitude: -79.363267

For data sources see[1][2][3]

Well History

Date Event
1964-09-16 New Permit Application
1964-09-23 Drilling Completion
1964-12-30 Reworked
2016-12-28 Begin Plugging
2017-01-10 Finished Plugging
2018-10-19 Fully Plugged

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 2962.00 365 0.00 0 0.00 0
1996 2413 365 0.00 0 0.00 0
1998 2311 365 0.00 0 0.00 0
1999 CONSOL GAS CO 2284 365 0.00 0 0.00 0
2000 CONSOL GAS CO 774 365 0.00 0 0.00 0
2001 CONSOL GAS CO 2248 365 0.00 0 0.00 0
2002 CONSOL GAS CO 2063 365 0.00 0 0.00 0
2003 CONSOL GAS CO 1978 365 0.00 0 0.00 0
2005 CONSOL GAS CO 1496 365 0.00 0 0.00 0
2006 CONSOL GAS CO 1703.00 365 0.00 0 0.00 0
2007 CONSOL GAS CO 1546.00 365 0.00 0 0.00 0
2008 CONSOL GAS CO 1518.00 365 0.00 0 0.00 0
2009 CONSOL GAS CO 1487.00 365 0.00 0 0.00 0
2010 CONSOL GAS CO 1,490.00 365 0.00 0 0.00 0
2011 CONSOL GAS CO 0.00 0 0.00 0 0.00 0
2012 CNX GAS CO LLC 1,758.00 366 0.00 0 0.00 0
2013 CNX GAS CO LLC 1,490.00 365 0.00 0 0.00 0
2014 CNX GAS CO LLC 1,219.00 365 0.00 0 0.00 0
2015 CNX GAS CO LLC 482.00 365 0.00 0 0.00 0
2016 CNX GAS CO LLC 274.00 122 0.00 0 0.00 0
2017 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2006 CONSOL GAS CO Brine 0.00 Bbl Other
2017 CNX GAS CO LLC Produced Fluid 40.00 Bbl SURFACE IMPOUNDMENT 95-7-37312-10

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1030255 Primary Facility 2001-05-15 Routine/Complete Inspection No Violations Noted equipped/no tank/E&S ok/tag ok
209336 Primary Facility 1989-01-10 Routine/Complete Inspection No Violations Noted E&S OK; NO TANK
2514014 Primary Facility 2016-08-24 Routine/Complete Inspection Pending Well tagged-in production. 3" well head casing severely corroded and leaking steady gas. Contacted operator to inform them that the mechanical integrity of this well is severely compromised and will need corrected. Operator inspected this well and informed me that they will submit NOI to plug and will then plug this well shortly.
2548872 Primary Facility 2017-01-03 Plugging(Includes Plugged/Mined Through) No Violations Noted Running a CBL at the time of this inspection. Tagged cement top from last plug at 1797'. Getting ready to cut pipe at 1690' and will then either pull or perf every 100' and squeeze cement. All equipment on site looked ok.

For data sources see[7]

References