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37-005-01591

Well Details

Well ID: 37-005-01591
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Country: United States
State: Pennsylvania
County: Armstrong
Municipality: Kiskiminetas Township
Operator Name: ALLIANCE PETRO CO LLC
Well Pad ID:
Farm/Lease Name: R MCLAUGHLIN 3
License Status: Plugged and Abandoned
Spud Date: 1925-02-09
Permit Date:
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.557132
Longitude: -79.538615

For data sources see[1][2][3]

Well History

Date Event
1925-05-02 Drilling Completion
1985-01-01 Newly Drilled
2016-12-01 Begin Plugging
2016-12-19 Finished Plugging
2019-01-25 Fully Plugged

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 922.00 335 0.00 0 0.00 0
1996 997 365 0.00 0 0.00 0
1998 1371 365 0.00 0 0.00 0
1999 CONSOL GAS CO 1166 365 0.00 0 0.00 0
2000 CONSOL GAS CO 535 365 0.00 0 0.00 0
2002 CONSOL GAS CO 506 365 0.00 0 0.00 0
2003 CONSOL GAS CO 326 365 0.00 0 0.00 0
2005 CONSOL GAS CO 84 365 0.00 0 0.00 0
2006 CONSOL GAS CO 39.00 365 0.00 0 0.00 0
2007 CONSOL GAS CO 1104.00 365 0.00 0 0.00 0
2008 CONSOL GAS CO 95.00 365 0.00 0 0.00 0
2009 CONSOL GAS CO 79.00 365 0.00 0 0.00 0
2010 CONSOL GAS CO 0.00 0 0.00 0 0.00 0
2011 CONSOL GAS CO 1.00 365 0.00 0 0.00 0
2012 CONSOL GAS CO 1.00 366 0.00 0 0.00 0
2013 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2014 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2015 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2016 CNX GAS CO LLC 84.00 61 0.00 0 0.00 0
2017 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2006 CONSOL GAS CO Brine 0.00 Bbl Other

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2544635 Primary Facility 2016-12-14 Plugging(Includes Plugged/Mined Through) No Violations Noted Crew had perfed 7" from 1360' to surface every 100' and was tripping out to displace cement in 700' lifts at time of inspection. All equipment on site looked ok.

For data sources see[7]

References