X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

37-003-22314

Well Details

Well ID: 37-003-22314
Loading map...
Country: United States
State: Pennsylvania
County: Allegheny
Municipality: Findlay Township
Operator Name: CNX GAS CO LLC
Well Pad ID: 151158
Farm/Lease Name: ACAA 4A
License Status:
Spud Date:
Permit Date: 2014-11-03
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: No
Latitude: 40.479925
Longitude: -80.237208

For data sources see[1][2][3]

Well History

Date Event
2014-11-03 New Permit Application
2015-01-23 Performed Spud Operation
2017-09-21 MOD

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2015 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2016 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2017 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2019 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2015 CNX GAS CO LLC Drill Cuttings 62.38 Tons LANDFILL PAD059087072
2015 CNX GAS CO LLC Drilling Fluid Waste 474.32 Bbl LANDFILL 06-08438
2015 CNX GAS CO LLC Drill Cuttings 159.64 Tons LANDFILL 06-08438
2015 CNX GAS CO LLC Drill Cuttings 208.54 Tons LANDFILL 100620
2019 CNX GAS CO LLC Other Oil & Gas Wastes 19.33 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123SW019

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2332438 Primary Facility 2014-12-23 Preoperation Inspection No Violations Noted Our preoperation inspection of CNX ACAA 4 Well Pad for well 4A-4L
2337589 Primary Facility 2015-01-16 Follow-up Inspection No Violations Noted Follow up inspection to check on progress of E&S controls from 12/23/14.
2342057 Primary Facility 2015-01-29 Drilling/Alteration No Violations Noted THE CONDUCTOR IS IN AND COVERED WITH A STEEL PLATE. THE PAD IS IN GOOD CONDITION.
2356932 Primary Facility 2015-04-01 Administrative/File Review In Compliance with Policy On Monday March 31st 2015, Consol Energy representative Benjamin Leightner reported a Hammer Oil spill of one gallon that was immediately cleaned up and removed. This appears to be in compliance with department spill policy.
2362757 Primary Facility 2015-03-18 Drilling/Alteration No Violations Noted drilled to 612'; spud on 3/17/15; set 13 3/8" casing @ 549'; cemented to surface with 23 bbls of returns; plug down 3/18/15
2367305 Primary Facility 2015-05-04 Routine/Complete Inspection No Violations Noted
2367353 Primary Facility 2015-04-01 Drilling/Alteration No Violations Noted HAD 247 DRILLED TO A TOP HOLE TD OF 5,500'.
2665559 Primary Facility 2017-11-30 Complaint Inspection No Violations Noted Well appears to be drilled but not completed. Department records indicate the well was spud on 1/23/2015. No well apparatus observed. Cellar covered with a large steel plate. No production equipment observed. No gas production units on well pad.

For data sources see[7]

References