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37-003-00892

Well Details

Well ID: 37-003-00892
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Country: United States
State: Pennsylvania
County: Allegheny
Municipality: Moon Township
Operator Name: WHARTON C C JR
Well Pad ID:
Farm/Lease Name: MILLER 1
License Status:
Spud Date:
Permit Date:
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.527770
Longitude: -80.218439

For data sources see[1][2][3]

Well History

Date Event
1900-01-01 Drilling Completion
1915-01-01 NEWLY DRILLED

For data sources see[4]



Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1779470 Primary Facility 2009-03-27 Routine/Complete Inspection No Violations Noted not producing, opereator deceased, leaking, placed on ad, well list
1866972 Primary Facility 2010-02-23 Routine/Complete Inspection No Violations Noted inspect abd well, leaking more gas recommend emergency plugging
1866975 Primary Facility 2010-02-25 Routine/Complete Inspection No Violations Noted mobilize backhoe/ dozer monitor ground for gas
1866979 Primary Facility 2010-02-26 Plugging(Includes Plugged/Mined Through) No Violations Noted site prep 3 loads gravel
1866981 Primary Facility 2010-02-27 Plugging(Includes Plugged/Mined Through) No Violations Noted install containment dam install containment around well
1866984 Primary Facility 2010-02-28 Plugging(Includes Plugged/Mined Through) No Violations Noted complete E&S controls, mobilize eqipment...very large snowstorm over past 3 days
1866992 Primary Facility 2010-03-01 Plugging(Includes Plugged/Mined Through) No Violations Noted complete mob and site preprig in place will start pulling rods in am
1866997 Primary Facility 2010-03-02 Plugging(Includes Plugged/Mined Through) No Violations Noted pull rods attempt to blow down well
1866999 Primary Facility 2010-03-03 Plugging(Includes Plugged/Mined Through) No Violations Noted pulled all tubing well approx 1500' deep will log in am
1867000 Primary Facility 2010-02-22 Routine/Complete Inspection No Violations Noted well inspected conditions have deteriorated since last inspection
1868035 Primary Facility 2010-03-04 Plugging(Includes Plugged/Mined Through) No Violations Noted ran collar locator prep to run 25 sk cement plug
1868043 Primary Facility 2010-03-05 Plugging(Includes Plugged/Mined Through) No Violations Noted tagged top of plug at 1700' 0% gas at well head
1869611 Primary Facility 2010-03-10 Plugging(Includes Plugged/Mined Through) No Violations Noted cemented back to 500'
1869615 Primary Facility 2010-03-08 Plugging(Includes Plugged/Mined Through) No Violations Noted ran caliper log, ran plug 1700'-1490'
1869636 Primary Facility 2010-03-11 Plugging(Includes Plugged/Mined Through) No Violations Noted use spear to hook into 3 1/2" would not come
1869637 Primary Facility 2010-03-11 Plugging(Includes Plugged/Mined Through) No Violations Noted cement from 500' to surface
1871991 Primary Facility 2010-03-01 Plugging(Includes Plugged/Mined Through) No Violations Noted HYDROCARBON WELL SERVICES PULLING RODS.
1871993 Primary Facility 2010-03-10 Plugging(Includes Plugged/Mined Through) No Violations Noted SOLID CEMENT FROM 1850' TO 1000'. 3.5" CASING PERFORATED EVERY 100'.
1871995 Primary Facility 2010-03-09 Plugging(Includes Plugged/Mined Through) No Violations Noted BOTTOM HOLE CEMENTED. 3.5" CASING WILL NOT PULL.
1893473 Primary Facility 2010-04-27 Plugging(Includes Plugged/Mined Through) No Violations Noted address complaints from landowner
1893476 Primary Facility 2010-05-30 Plugging(Includes Plugged/Mined Through) No Violations Noted completed site restoration
1893481 Primary Facility 2010-05-06 Plugging(Includes Plugged/Mined Through) No Violations Noted LANDSCAPING IN GOOD SHAPE
1893483 Primary Facility 2010-05-08 Plugging(Includes Plugged/Mined Through) No Violations Noted meet to sign daily logs
1893490 Primary Facility 2010-03-18 Plugging(Includes Plugged/Mined Through) No Violations Noted demob, finish site restoration
215831 Primary Facility 1994-02-17 Routine/Complete Inspection Violation(s) Noted NO ID;ABANDONED;E&S OK
216973 Primary Facility 1994-09-26 Routine/Complete Inspection No Violations Noted E&S OK
217957 Primary Facility 1996-07-01 Routine/Complete Inspection Violation(s) Noted ABANDONED & UNPLUGGED

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
215831 102077 02/17/1994 1994-02-17 203TAG - Failure to affix, in a permanent manner, a registration number on a well within 60 days of registration Administrative NO ID
217957 107525 07/01/1996 1996-07-01 210A - Failure to adequately plug or schedule plugging of a well upon abandonment Administrative ABANDONED & UNPLUGGED

For data sources see[5]

References