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34-169-24058

Well Details

Well ID: 34-169-24058
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Country: United States
State: Ohio
County: Wayne
Municipality: Chippewa Township
Operator Name: S & S ENERGY CORP
Well Pad ID:
Farm/Lease Name: BARAT
License Status: Final Restoration
License Date: 2007-04-09
Spud Date: 1985-10-17
Spud Drilling Contractor:
Final Drill Date: 1985-10-22
Well Total Depth: 3840.00 ft
Configuration: Vertical
Latitude: 40.950000
Longitude: -81.710000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1985-01-04 Issued Date 12/31/84 Expired Date 6/29/85 Acres 0020000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000
CO 1985-07-25 432 BAKERWELL INC GeoDate 7/25/85
Oil and Gas 1985-07-25 Issued Date 7/25/85 Expired Date 7/25/86 Acres 0020000 Tool Type CRAF Proposed Formation CLINTON Proposed Depth 03840 Proposed Drill Depth 03840
Original Spud 1985-10-17 R.I. 7-27-85 PD. NAT. TR/GAS
Completed 1985-10-22 R.I. 7-27-85 PD. NAT. TR/GAS
Reached Total Depth 1985-10-22 R.I. 7-27-85 PD. NAT. TR/GAS
Plugged Back 1985-10-29 R.I. 7-27-85 PD. NAT. TR/GAS
CO 1986-08-01 70 WALDRON DAVID A & ASS INC GeoDate 1/4/85
Completion Report Received 1986-08-08 R.I. 7-27-85 PD. NAT. TR/GAS
Change of Owner 1997-12-26 Operator changed from 432, BAKERWELL INC to 5660, S & S ENERGY CORPORATION
APP 2007-04-09 Proposed Formations:CLINTON, Issued Date:4/9/2007, Expired Date:4/8/2008 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2008-01-17 R.I. 7-27-85 PD. NAT. TR/GAS
Construction Permit Expires 2008-04-08 R.I. 7-27-85 PD. NAT. TR/GAS
Record Last Modified 2017-02-15 R.I. 7-27-85 PD. NAT. TR/GAS

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 3792 3810 2
3792 3810 2
3792 3810 2

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
N2 0 180 Mscf 0
H2O 0 1800 Bbl 40000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1990 BAKERWELL INC 1769.00 0.00 365
1992 BAKERWELL INC 0.00 0.00 365
1993 BAKERWELL INC 0.00 0.00 365
1994 BAKERWELL INC 0.00 0.00 365
1995 BAKERWELL INC 0.00 0.00 365
1996 BAKERWELL INC 0.00 0.00 365
1997 BAKERWELL INC 0.00 0.00 365
1998 S & S ENERGY CORP 0.00 0.00 365
1999 S & S ENERGY CORP 0.00 0.00 0
2000 S & S ENERGY CORP 0.00 0.00 0
2001 S & S ENERGY CORP 0.00 0.00 0
2002 S & S ENERGY CORP 0.00 0.00 0
2003 S & S ENERGY CORP 0.00 0.00 0
2004 S & S ENERGY CORP 0.00 0.00 0
2005 S & S ENERGY CORP 0.00 0.00 0
2006 S & S ENERGY CORP 0.00 0.00 365
2007 S & S ENERGY CORP 0.00 0.00 0
2008 S & S ENERGY CORP 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1990 BAKERWELL INC Brine 0 365
1992 BAKERWELL INC Brine 0 365
1993 BAKERWELL INC Brine 0 365
1994 BAKERWELL INC Brine 0 365
1995 BAKERWELL INC Brine 0 365
1996 BAKERWELL INC Brine 0 365
1997 BAKERWELL INC Brine 0 365
1998 S & S ENERGY CORP Brine 0 365
1999 S & S ENERGY CORP Brine 0 0
2000 S & S ENERGY CORP Brine 0 0
2001 S & S ENERGY CORP Brine 0 0
2002 S & S ENERGY CORP Brine 0 0
2003 S & S ENERGY CORP Brine 0 0
2004 S & S ENERGY CORP Brine 0 0
2005 S & S ENERGY CORP Brine 0 0
2006 S & S ENERGY CORP Brine 0 365
2007 S & S ENERGY CORP Brine 0 0
2008 S & S ENERGY CORP Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1016731070 2008-2-5 0:00:0 PB No Violations 1.00
-1096255854 2008-1-3 0:00:0 PB No Violations 2.00
-1281055500 2008-1-8 0:00:0 PB No Violations 1.00
-1394927597 2007-12-18 0:00 PB No Violations 2.00
-1645832268 2008-2-25 0:00: FR No Violations
-1653941726 2008-1-15 0:00: PB No Violations 2.00
-1805998007 2008-1-7 0:00:0 PB No Violations 2.00
-2038980671 2006-9-11 0:00: PW No Violations 2.50
-2064285848 2007-10-26 0:00 FR No Violations 1.00
-329746541 2008-6-12 0:00: FR No Violations 1.00
-764948527 2010-11-19 0:00 FR No Violations 0.70
-814692966 2007-12-17 0:00 PB No Violations 1.50
00000PL538 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0008172648 2008-01-18 Plug / Plug Back No Violations Check for leaks and top of cement and found no leaks ,cement at surface .Looks like a great plug.Bishop well service moving rig off today.
0329746541 2008-06-12 Final Restoration No Violations Meets requirements for restoration final .
0391346591 2008-01-22 Plug / Plug Back No Violations Check again for leaks and found none.Pits pumped down ready to close.
0764948527 2010-11-19 Final Restoration No Violations Meets requirements for restoration final.
0814692966 2007-12-17 Plug / Plug Back No Violations Bishop well has moved mud pump in today so that they can circulate and drive 7 inch down well .
1016731070 2008-02-05 Plug / Plug Back No Violations Well cut off and area rough graded.Equipment needs removed .
1063730892 2008-01-04 Plug / Plug Back No Violations pull 7 inch out and go back in with 210 ft. of 7 inch with skirt on bottom and keep driving and rotating with power tongs.
1095403134 2008-04-10 Final Restoration No Violations Pits closed ,pipe cut .Area needs graded and seeded.
1096255854 2008-01-03 Plug / Plug Back No Violations Return and found that 7 inch did go back in hole then try and go below to find more stuff to fish out .All of the casing string has been turned to jello -from 190 ft to surface.8 Inch 4 inch 23/8 are all parted .
1106472046 2008-01-11 Plug / Plug Back No Violations Bishop is at 245 ft. on 1 1/2 tubing and may be able to set plug Monday.
1182815046 2007-12-26 Plug / Plug Back No Violations No plugging today , shut down for parts and repairs.
1205167972 2008-01-03 Plug / Plug Back No Violations Pull 8 inch casing out and go back in with 7 inch to about 190 ft. Return later in the day and found that the 7 inch casing did go back in hole and should stabalize hole to reach bottom for plug.
1210766453 2008-01-03 Plug / Plug Back No Violations Pull 8 inch out.190 ft. and ran same amount of 7 inch back in hole.Had trouble with the 7 inch going in.
1210779374 2008-01-04 Plug / Plug Back No Violations Pulling 7 inch back out and running more in today/after it arrives?
1211293183 2008-01-14 Plug / Plug Back No Violations Pulling 1 1/2 tubing out today and will not be ready to set plugs today.
1231347053 2008-01-16 Plug / Plug Back No Violations Arrive to find that Bishop well - Sqeak , has ran 2 3/8 tubing to 3682 ft. Petroset John set 200ft plug from 3682 to 3482 ft. Pull tubing to 2490 ft and wait on shooters.Shot line of holes from 2490 to 2460 ft. Set 350 ft plug .Pull up to 650ft and shot a
1281055500 2008-01-08 Plug / Plug Back No Violations Bishop Well able to pull out 4 inch and 1 1/2 to 245 ft. Now on something solid.
1394927597 2007-12-18 Plug / Plug Back No Violations On site today with Bishop well and they may be able to set bottom plug if they can get hold of the 1 1/2 tubing .Return later and found that they did not get it.
1426286448 2007-01-04 Production Wells No Violations Well remains shut in no leaks but needs plugged .Operator to plug well when plugging rig is back in area .
1453238393 2007-12-19 Plug / Plug Back No Violations Arrive today and they are still fishing for tubing and casing from the 4 inch 8 inch and 1 1/2 tubing.
1645832268 2008-02-25 Final Restoration No Violations Pipe not cut off .Pits pumped off ready to close but still need closed.Area needs more grade and seed.
1653941726 2008-01-15 Plug / Plug Back No Violations Running 2 3/8 tubing and try and set bottom plug later today.
1805998007 2008-01-07 Plug / Plug Back No Violations Bishop Well service milling on junk? Advise that a camera could find out what and returned after checking on camera and found mill in hole .
1900000290 2006-12-06 Production Wells No Violations Review site and found that service rig had been on location but has moved .Contact operator and find out plug schedule .It is on the list and should be plugged in a month or so .
2038980671 2006-09-11 Production Wells Violations Noted This well is idle and needs to be plugged or placed back into production . Contact operator and found that his contact number is no longer a working number .Met landowner on site and reviewed all of the info and found out he has not received any shut in f
2064285848 2007-10-26 Final Restoration No Violations Check on well which needs plugged and found that the tanks remain even though they were to be pulled.Area needs graded.Well needs plugged.
2077219980 2007-12-14 Plug / Plug Back No Violations Bishop well service is trying to pull out bad casing.They are pulling the collasped casing at the top section of the well.
2146097706 2008-01-17 Plug / Plug Back No Violations Arrive and tag cement at 195 ft. Next set gravel from 195 to 130 ft. Had Medina Supply set grout plug with 9 sack grout from 130ft. To surface.Used 3.5 yards and hole was full.
391346591 2008-1-22 0:00: PB No Violations 1.00
8172648 2008-1-18 0:00: PB No Violations 1.50
PL538 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
2038980671 US-OH-120744 2006-10-04 Well shall be plugged

For data sources see[9]

References