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34-169-20841

Well Details

Well ID: 34-169-20841
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Country: United States
State: Ohio
County: Wayne
Municipality: Wooster Township
Operator Name: KENOIL LLC
Well Pad ID:
Farm/Lease Name: WEARY
License Status: Final Restoration
License Date: 2009-09-18
Spud Date: 1958-11-01
Spud Drilling Contractor:
Final Drill Date: 1958-12-24
Well Total Depth: 3304.00 ft
Configuration: Vertical
Latitude: 40.780000
Longitude: -81.970000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1958-11-01 47.67 ACRES
Completed 1958-12-24 47.67 ACRES
Reached Total Depth 1958-12-24 47.67 ACRES
CO 1986-06-19 627 KENOIL
APP 2009-09-18 Proposed Formations:CLINTON, Issued Date:9/18/2009, Expired Date:9/18/2010 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2010-05-27 47.67 ACRES
Construction Permit Expires 2010-09-18 47.67 ACRES
Record Last Modified 2013-03-14 47.67 ACRES

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
OIL 0 575 Bbl 15000

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1987 KENOIL LLC 892.00 0.00 365
1988 KENOIL LLC 2356.00 0.00 365
1989 KENOIL LLC 580.00 0.00 365
1992 KENOIL LLC 250.00 0.00 365
1993 KENOIL LLC 200.00 0.00 365
1994 KENOIL LLC 100.00 0.00 0
1995 KENOIL LLC 0.00 0.00 0
1996 KENOIL LLC 398.00 0.00 0
1997 KENOIL LLC 498.00 0.00 365
1998 KENOIL LLC 410.00 0.00 365
1999 KENOIL LLC 550.00 0.00 0
2000 KENOIL LLC 370.00 0.00 365
2001 KENOIL LLC 270.00 0.00 365
2002 KENOIL LLC 219.00 0.00 365
2003 KENOIL LLC 365.00 0.00 365
2004 KENOIL LLC 294.00 0.00 365
2005 KENOIL LLC 313.00 0.00 365
2006 KENOIL LLC 211.00 0.00 365
2007 KENOIL LLC 259.00 0.00 365
2008 KENOIL LLC 91.00 0.00 365
2009 KENOIL LLC 15.00 0.00 365
2010 KENOIL LLC 0.00 0.00 365

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1987 KENOIL LLC Brine 50 365
1988 KENOIL LLC Brine 0 365
1989 KENOIL LLC Brine 0 365
1992 KENOIL LLC Brine 0 365
1993 KENOIL LLC Brine 0 365
1994 KENOIL LLC Brine 0 0
1995 KENOIL LLC Brine 40 0
1996 KENOIL LLC Brine 0 0
1997 KENOIL LLC Brine 0 365
1998 KENOIL LLC Brine 0 365
1999 KENOIL LLC Brine 0
2000 KENOIL LLC Brine 365
2001 KENOIL LLC Brine 0 365
2002 KENOIL LLC Brine 0 365
2003 KENOIL LLC Brine 0 365
2004 KENOIL LLC Brine 0 365
2005 KENOIL LLC Brine 0 365
2006 KENOIL LLC Brine 10 365
2007 KENOIL LLC Brine 0 365
2008 KENOIL LLC Brine 0 365
2009 KENOIL LLC Brine 0 365
2010 KENOIL LLC Brine 171 365

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1380089228 2010-5-24 0:00: PB No Violations 8.50
-2111202580 2010-11-3 0:00: FR No Violations 0.70
-451196537 2010-6-1 0:00:0 PB No Violations 1.00
-537297470 2010-5-14 0:00: PB No Violations 4.00
-559342367 2010-6-14 0:00: FR No Violations 1.00
-755349651 2010-7-21 0:00: FR No Violations 1.50
0451196537 2010-06-01 Plug / Plug Back No Violations Check for leaks and found cement down less than 10 ft and no leaks.
0537297470 2010-05-14 Plug / Plug Back No Violations Arrive today and found 5 inch out and hooked up to pull 8 inch. Pulled casing in two at 20 ft and could not screw back into casing. Went after inside spear and then could not pull casing. Rip at 690 ft then found out we could not get cement trucks today
0559342367 2010-06-14 Final Restoration No Violations Check on final and found that area has been graded but no vegetation has been established .
0646194789 2010-05-25 Plug / Plug Back No Violations Continue plugging well today. Had trouble pulling out of hole after getting rip at 2687 ft. Had to work pipe for hours before it came loose. Set Lime plug and then pull rest of casing out before trying to pull 8 inch.
0755349651 2010-07-21 Final Restoration No Violations Meets requirements for restoration final.
1371496896 2010-05-27 Plug / Plug Back No Violations Run tubing in to 745 ft and set plug. Finish plug to surface today.
1380089228 2010-05-24 Plug / Plug Back No Violations Plug well today with Jim Nalley and Petroset - Did not get it totally plugged today
2111202580 2010-11-03 Final Restoration No Violations Meets requirements for restoration final.
646194789 2010-5-25 0:00: PB No Violations 8.50

For data sources see[8]

References