X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-169-20414

Well Details

Well ID: 34-169-20414
Loading map...
Country: United States
State: Ohio
County: Wayne
Municipality: Milton Township
Operator Name: OXFORD OIL
Well Pad ID:
Farm/Lease Name: CONRAD-GRABER
License Status: Final Restoration
License Date: 2005-03-24
Spud Date: 1954-11-12
Spud Drilling Contractor:
Final Drill Date: 1954-11-12
Well Total Depth: 3330.00 ft
Configuration: Vertical
Latitude: 40.940000
Longitude: -81.840000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1801-01-02 79 OXFORD OIL CO
Unknown 1802-01-01
Completed 1954-11-12 GL=985.5 PF= 2ND CLINTON
Original Spud 1954-11-12 GL=985.5 PF= 2ND CLINTON
Reached Total Depth 1954-11-12 GL=985.5 PF= 2ND CLINTON
APP 2005-03-24 Proposed Formations:CLINTON, Issued Date:3/24/2005, Expired Date:3/24/2006 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2005-07-28 GL=985.5 PF= 2ND CLINTON
Construction Permit Expires 2006-03-24 GL=985.5 PF= 2ND CLINTON
Record Last Modified 2013-03-14 GL=985.5 PF= 2ND CLINTON

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
OIL 0 600 Bbl 15000

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 OXFORD OIL 0.00 206.00 0
1985 OXFORD OIL 0.00 63.00 365
1986 OXFORD OIL 0.00 0.00 365
1987 OXFORD OIL 0.00 0.00 365
1988 OXFORD OIL 932.00 377.00 365
1989 OXFORD OIL 1647.00 519.00 365
1990 OXFORD OIL 1859.00 392.00 365
1991 OXFORD OIL 1542.00 292.00 365
1992 OXFORD OIL 825.00 215.00 365
1993 OXFORD OIL 1098.00 227.00 365
1994 OXFORD OIL 921.00 208.00 365
1995 OXFORD OIL 1216.00 148.00 365
1996 OXFORD OIL 786.00 156.00 366
1997 OXFORD OIL 613.00 71.00 365
1998 OXFORD OIL 461.00 67.00 365
1999 OXFORD OIL 645.00 139.00 365
2000 OXFORD OIL 337.00 70.00 0
2001 OXFORD OIL 254.00 74.00 365
2002 OXFORD OIL 393.00 64.00 365
2003 OXFORD OIL 250.00 150.00 365
2004 OXFORD OIL 212.00 53.00 365
2005 OXFORD OIL 38.00 72.00 236
2006 OXFORD OIL 0.00 0.00 365
2007 OXFORD OIL 0.00 0.00 365
2008 OXFORD OIL 0.00 0.00 365

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 OXFORD OIL Brine 0 0
1985 OXFORD OIL Brine 0 365
1986 OXFORD OIL Brine 0 365
1987 OXFORD OIL Brine 786 365
1988 OXFORD OIL Brine 247 365
1989 OXFORD OIL Brine 107 365
1990 OXFORD OIL Brine 0 365
1991 OXFORD OIL Brine 46 365
1992 OXFORD OIL Brine 20 365
1993 OXFORD OIL Brine 20 365
1994 OXFORD OIL Brine 10 365
1995 OXFORD OIL Brine 0 365
1996 OXFORD OIL Brine 0 366
1997 OXFORD OIL Brine 0 365
1998 OXFORD OIL Brine 0 365
1999 OXFORD OIL Brine 0 365
2000 OXFORD OIL Brine 52
2001 OXFORD OIL Brine 0 365
2002 OXFORD OIL Brine 0 365
2003 OXFORD OIL Brine 76 365
2004 OXFORD OIL Brine 0 365
2005 OXFORD OIL Brine 60 236
2006 OXFORD OIL Brine 0 365
2007 OXFORD OIL Brine 0 365
2008 OXFORD OIL Brine 0 365

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1042750287 2005-8-5 0:00:0 PB No Violations 0.70
-1268534003 2006-2-7 0:00:0 FR No Violations 1.00
-1285039095 2005-9-6 0:00:0 FR No Violations 0.70
-1734709155 2006-3-22 0:00: FR No Violations 0.70
-244675243 2005-8-4 0:00:0 PB No Violations 1.50
-426940437 2005-8-26 0:00: PB No Violations 3.50
-512732206 2005-8-25 0:00: PB No Violations 9.50
001220i237 2002-07-31 Production Wells No Violations Returned to site to check status of water well being drilled at 12077 Miller Rd. Larry Maxwell ran bailor into well and gas pushed the bailor and fluid out of well and over top of rig mast. Well blew for 3 hours before dying down. Installed vent pipe 11 above ground. Well is venting at this time. Arrangments are being made to plug well. No evidence of P# 414 having caused this gas problem. Oxford Oil Co. uncovered well head for inspection. Sterling Fire department was called to assist. No injuries.
0023678885 2002-07-30 Production Wells No Violations Called Jack Green of Oxford Oil Co. to send a pumper to assist on the gas in a water well at 12077 Miller Rd. Needed to shut down the compreesor in the dike area. Gas was blowing from anew water well being drilled 300 west of this well. Pumper came and dug around 10 and 8 annulas. No gas pressure on the annular space. Gas diminished in water well and started compressor. No violations at this time. This well supplies gas to this home at 12077 Miller RD.
0244675243 2005-08-04 Plug / Plug Back No Violations Terry Rice is still trying to rip casing today and is still having problems with knife.
0426940437 2005-08-26 Plug / Plug Back No Violations Return today to finish plugging .The well had an obstruction at 250 ft. and that space to surface should have taken 6.5 tons to fill.After well was plugged it took 16 tons .That meant that the obstruction was open and did take material and should be full from 1500 ft. back to surface.
0498667928 2005-08-01 Plug / Plug Back No Violations Oxford Oil plugging well with Terry Rice and try and rip at 2392 ft. and has bad knife and could not rip casing.
0512732206 2005-08-25 Plug / Plug Back No Violations Arrive today after meeting in Uniontown for Down hole camera.Need to run camera in hole because of the fact that water can be heard running down hole .Next run camera down hole to 250 ft and found that water is filling up from below and not from above .Begin plug from 250 ft. to 0 ft. with clay.6.5 Tons should fill well and it took all of the clay and would need another load .
0564198828 2005-08-10 Plug / Plug Back No Violations Check on plug status and found that the rig is pulling 7 inch today and shouldbe ready in two days to finish up on plug.
0580448268 2005-10-05 Final Restoration No Violations found that there are no leaks at well and tanks remain and area needs graded and seeded.
0718965973 2005-10-05 Final Restoration No Violations Check for leaks and to see if pipe has been cut off and found no leaks .Pipe has been cut off and the tanks remain on site which also needs graded and seeded.
0771882970 2005-07-29 Plug / Plug Back No Violations Set another 500 shovels on bottom today becasuse top of plug was still almost to top of perfs.
0905471568 2005-08-29 Plug / Plug Back No Violations Return today and top off well which was only down 40 ft. after weekend.
1042750287 2005-08-05 Plug / Plug Back No Violations Working on knife repairs today and still have not ripped casing.
1126700799 2005-08-22 Plug / Plug Back No Violations Check on Plug operation and found that the 7 inch casing has been pulled and Terry Rice can not get back in hole past 250 ft. to set remaining plugs.Go over several options with Terry and leave final decision up to him.I advised that he pick up casing and try to use it to knock out obstruction and then use it to plug thru.Also contact Inspector Moravy and he advised the same .Try and contact Supr Cheslock and Simmers .
1126706692 2005-08-23 Plug / Plug Back No Violations Met with Supr Simmers on how to proceed with plug on well since operator can only get back in well to 250 ft. Then went and checked area for Berea production and found it to be over one mile away.Check computer and well maps also.
1220i237 2002-7-31 0:00: PW No Violations 0.00
1268534003 2006-02-07 Final Restoration No Violations Meets requirements for restoration final.
1285039095 2005-09-06 Final Restoration No Violations The well has plugged and the pits are close and the area needs graded and seeded .Tanks remain.
1416829788 2005-09-01 Plug / Plug Back No Violations Check to see if well has clay at surface and it does.The well has no leaks and appears to be ready to cut off below grade and the area graded and seeded.
1559275524 2005-08-17 Plug / Plug Back No Violations Rip casing at 2400 ft. on 5 1/2 casing .1700 ft. on 7 inch casing .
1734709155 2006-03-22 Final Restoration No Violations Tanks need removed and area needs seeded.
2086024430 2005-07-28 Plug / Plug Back No Violations Oxford Oil is having Terry Rice plug well today.Set bottom plug today with 500 shovels.
23678885 2002-7-30 0:00: PW No Violations 2.50
498667928 2005-8-1 0:00:0 PB No Violations 1.50
564198828 2005-8-10 0:00: PB No Violations 1.50
580448268 2005-10-5 0:00: FR No Violations 0.70
718965973 2005-10-5 0:00: FR No Violations 0.70
771882970 2005-7-29 0:00: PB No Violations 2.70
905471568 2005-8-29 0:00: PB No Violations 2.20

For data sources see[8]

References