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34-167-27018

Well Details

Well ID: 34-167-27018
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Country: United States
State: Ohio
County: Washington
Municipality: Dunham Township
Operator Name: DECKER WELL SERVICE LLC
Well Pad ID:
Farm/Lease Name: HART KENNETH
License Status: Final Restoration
License Date: 2015-04-13
Spud Date: 1981-12-30
Spud Drilling Contractor:
Final Drill Date: 1982-01-15
Well Total Depth: 2366.00 ft
Configuration: Vertical
Latitude: 39.340000
Longitude: -81.670000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1981-12-10 2202 DECKER WELL SERVICE GeoDate 12/10/81
Original Spud 1981-12-30
Completed 1982-01-15
Reached Total Depth 1982-01-15
APP 2015-04-13 Proposed Formations:BEREA, Issued Date:4/13/2015, Expired Date:4/12/2017 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2015-08-12
Record Last Modified 2017-02-10
Construction Permit Expires 2017-04-12

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 2148 2154 4
2148 2154 4
2148 2154 4

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 50000 Gal 50000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 COLUMBIA GAS TRANSMISSION LLC 18.00 0.00 0
1985 DECKER WELL SERVICE LLC 31.00 0.00 60
1986 DECKER WELL SERVICE LLC 0.00 0.00 0
1987 DECKER WELL SERVICE LLC 0.00 0.00 365
1988 DECKER WELL SERVICE LLC 0.00 0.00 0
1989 DECKER WELL SERVICE LLC 0.00 0.00 0
1990 DECKER WELL SERVICE LLC 0.00 0.00 0
1991 DECKER WELL SERVICE LLC 0.00 0.00 0
1992 DECKER WELL SERVICE LLC 0.00 0.00 0
1993 DECKER WELL SERVICE LLC 0.00 0.00 0
1994 DECKER WELL SERVICE LLC 0.00 0.00 0
1995 DECKER WELL SERVICE LLC 0.00 0.00 0
1996 DECKER WELL SERVICE LLC 0.00 0.00 0
1997 DECKER WELL SERVICE LLC 0.00 0.00 0
1998 DECKER WELL SERVICE LLC 0.00 0.00 0
1999 DECKER WELL SERVICE LLC 0.00 0.00 0
2000 DECKER WELL SERVICE LLC 0.00 0.00 0
2001 DECKER WELL SERVICE LLC 0.00 0.00 0
2002 DECKER WELL SERVICE LLC 0.00 0.00 0
2003 DECKER WELL SERVICE LLC 0.00 0.00 0
2004 DECKER WELL SERVICE LLC 0.00 0.00 0
2005 DECKER WELL SERVICE LLC 0.00 0.00 0
2006 DECKER WELL SERVICE LLC 0.00 0.00 0
2007 DECKER WELL SERVICE LLC 0.00 0.00 0
2008 DECKER WELL SERVICE LLC 0.00 0.00 0
2009 DECKER WELL SERVICE LLC 0.00 0.00 0
2010 DECKER WELL SERVICE LLC 0.00 0.00 0
2011 DECKER WELL SERVICE LLC 0.00 0.00 0
2014 DECKER WELL SERVICE LLC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 COLUMBIA GAS TRANSMISSION LLC Brine 0 0
1985 DECKER WELL SERVICE LLC Brine 0 60
1986 DECKER WELL SERVICE LLC Brine 0 0
1987 DECKER WELL SERVICE LLC Brine 0 365
1988 DECKER WELL SERVICE LLC Brine 0 0
1989 DECKER WELL SERVICE LLC Brine 0 0
1990 DECKER WELL SERVICE LLC Brine 0 0
1991 DECKER WELL SERVICE LLC Brine 0 0
1992 DECKER WELL SERVICE LLC Brine 0 0
1993 DECKER WELL SERVICE LLC Brine 0 0
1994 DECKER WELL SERVICE LLC Brine 0 0
1995 DECKER WELL SERVICE LLC Brine 0 0
1996 DECKER WELL SERVICE LLC Brine 0 0
1997 DECKER WELL SERVICE LLC Brine 0 0
1998 DECKER WELL SERVICE LLC Brine 0 0
1999 DECKER WELL SERVICE LLC Brine 0 0
2000 DECKER WELL SERVICE LLC Brine 0 0
2001 DECKER WELL SERVICE LLC Brine 0 0
2002 DECKER WELL SERVICE LLC Brine 0 0
2003 DECKER WELL SERVICE LLC Brine 0 0
2004 DECKER WELL SERVICE LLC Brine 0 0
2005 DECKER WELL SERVICE LLC Brine 0 0
2006 DECKER WELL SERVICE LLC Brine 0 0
2007 DECKER WELL SERVICE LLC Brine 0 0
2008 DECKER WELL SERVICE LLC Brine 0 0
2009 DECKER WELL SERVICE LLC Brine 0 0
2010 DECKER WELL SERVICE LLC Brine 0 0
2011 DECKER WELL SERVICE LLC Brine 0 0
2014 DECKER WELL SERVICE LLC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0689246005 2015-08-12 Plug / Plug Back No Violations On location to witness plugging operations for this well and to train newly hired Inspector Brian Sefcik. Knox Energy was the plugging contractor for the well. After running in tools to total depth, it was observed the well was dry down to 100 off bottom. The decision was made to bullhead the bottom plug through the 4.5 casing. Cemenco pumped a 400 bottom plug from 2150-1750 using 30 sks class A cement and 28.2 bbls of freshwater displacement. Knox Energy then ran in with ripping tools and was able to rip the 4.5 casing at 625. Cemenco tried to establish a pumping rate at that depth, but was unsuccessful due to red rock cave in on the annulus of the 4.5 casing. The casing was pulled to a depth of 500 and 300 plug was set from 500-200 using 75 sks 2% gel cement and 3.2 bbls of freshwater displacement. Casing was then pulled to 150 and a plug was circulated to surface using 40 sks 2% gel cement. The cement did not drop below 30 down.
1439317694 2015-08-11 Administrative Inspection No Violations Received call from Bill Mitten of Knox Energy stating they are moving a service rig onto this well to commence plugging operations. 1.5 tubing will be pulled from the well today. The bottom plug will be set tomorrrow.
1465322000 2016-06-07 Final Restoration No Violations The purpose of my inspection today is a status check on a final restoration. During my inspection I witnessed no evidence of an oil and gas well and the site has been restored. Location has met 1509.072 B requirements.
689246005 2015-8-12 0:00: PB No Violations 8.00

For data sources see[9]

References