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Well ID: 34-157-25535 | Loading map...
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Country: United States | |
State: Ohio | |
County: Tuscarawas | |
Municipality: Oxford Township | |
Operator Name: PRODUCED WATER TRANSFER1 LLC | |
Well Pad ID: | |
Farm/Lease Name: MARK & DAISY MOZENA 2 (SWIW #16) | |
License Status: Active Injection | |
License Date: 2018-06-05 | |
Spud Date: 2018-06-22 | |
Spud Drilling Contractor: | |
Final Drill Date: 2018-10-25 | |
Well Total Depth: 8348.00 ft | |
Configuration: Vertical | |
Latitude: 40.280000 | |
Longitude: -81.570000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2018-06-05 | Proposed Formations:KNOX THROUGH ROME, Issued Date:6/5/2018, Expired Date:6/4/2020 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:SWD, Proposed Well Class:SWIW |
Reached Total Depth | 2018-10-25 | BASED ON CHIEFS ORDER 2018-401 AUTHORIZATION TO INJECT ON 12/6/2018 |
Record Last Modified | 2019-01-03 | BASED ON CHIEFS ORDER 2018-401 AUTHORIZATION TO INJECT ON 12/6/2018 |
Construction Permit Expires | 2020-06-04 | BASED ON CHIEFS ORDER 2018-401 AUTHORIZATION TO INJECT ON 12/6/2018 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2018-09-25 | ACID | 15 | 23523 Gal | 0 | Producers Service Corporation |
For data sources see[3]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-106922622 | 2020-4-9 0:00:0 | SW | No Violations | |
-109223693 | 2019-10-7 0:00: | SW | No Violations | |
-128133605 | 2019-7-24 0:00: | SW | No Violations | |
-1291087164 | 2019-11-27 0:00 | SW | No Violations | |
-1338576724 | 2018-7-30 0:00: | DD | No Violations | |
-1368022502 | 2018-8-23 0:00: | DD | No Violations | |
-146816751 | 2018-7-5 0:00:0 | DD | No Violations | |
-1511787575 | 2018-8-30 0:00: | DD | No Violations | |
-1538712751 | 2019-4-24 0:00: | SW | No Violations | |
-1575283942 | 2019-12-31 0:00 | SW | No Violations | |
-1772514518 | 2018-8-16 0:00: | DD | No Violations | |
-1846426413 | 2018-10-30 0:00 | SW | No Violations | |
-1959666022 | 2019-11-15 0:00 | SW | No Violations | |
-1983374884 | 2019-12-4 0:00: | SW | No Violations | |
-2008676653 | 2018-10-10 0:00 | DD | No Violations | |
-2113688035 | 2019-8-21 0:00: | SW | No Violations | |
-2116388940 | 2018-11-2 0:00: | SW | No Violations | |
-2129558524 | 2020-3-31 0:00: | SW | No Violations | |
-316019607 | 2018-10-25 0:00 | SW | No Violations | |
-328455886 | 2018-6-14 0:00: | DD | No Violations | |
-469959991 | 2018-9-25 0:00: | SW | No Violations | |
-778086779 | 2018-9-6 0:00:0 | CS | No Violations | 12.00 |
-804159782 | 2019-2-26 0:00: | SW | No Violations | |
-811037472 | 2019-6-19 0:00: | SW | No Violations | |
-868618761 | 2018-6-22 0:00: | DD | No Violations | |
-915311161 | 2019-5-10 0:00: | SW | No Violations | |
-939845402 | 2020-1-30 0:00: | SW | No Violations | |
0100290207 | 2018-08-17 | Drill / Deepen / Reopen | No Violations | 3100 deep dusting in the shale today, should be drilling lime at next reporting time. |
0146816751 | 2018-07-05 | Drill / Deepen / Reopen | No Violations | Site construction still being done informed construction crew that pit would need to be started 80 from the well bore. |
0275052026 | 2018-08-27 | Drill / Deepen / Reopen | No Violations | Site inspection revealed that Mitchell Drilling was at a depth of 6570 at the time of my inspection. |
0316019607 | 2018-10-25 | Salt Water Injection Well | No Violations | Site check today to verify that owner is preparing too have pits closed once they are emptied of all free standing fluid. |
0328455886 | 2018-06-14 | Drill / Deepen / Reopen | No Violations | Inspection today revealed that equipment has been moved in on site to begin site construction. |
0469959991 | 2018-09-25 | Salt Water Injection Well | No Violations | On site to witness Producers Services perform 3500 gallon acid treatment on open section of well bore. |
0698040343 | 2018-06-20 | Drill / Deepen / Reopen | No Violations | Inspection revealed that drill site is nearly complete, Express Energy will possibly move conductor rig in on site tomorrow. |
0778086779 | 2018-09-06 | Casing String Witnessed | No Violations | On site today to witness running of 26#-7 casing string, pipe is equipped with 1-shoe and 20 centralizers and Petro Set will cement in place tomorrow morning. |
0804159782 | 2019-02-26 | Salt Water Injection Well | No Violations | Inspection revealed that injection pumps were in operation today(4) pumps in operation and there was several brine haulers on site waiting to offload.
|
0868618761 | 2018-06-22 | Drill / Deepen / Reopen | No Violations | Express Energy on site today and they set a 6x6 cellar and were 40 foot deep when I stopped at the site they will drill a 26 hole and run 100 of 20 conductor pipe and they will cement it in place tomorrow. |
0915311161 | 2019-05-10 | Salt Water Injection Well | No Violations | On site to witness MIT testing on said well they applied 1790 psi and we monitored pressure for 15 minutes with no decline in pressure(TEST PASSED).
|
0935001765 | 2019-04-02 | Salt Water Injection Well | No Violations | Inspection revealed that injection pump was in operation during my inspection.
Noted four Myers trucks offloading during my inspection. |
100290207 | 2018-8-17 0:00: | DD | No Violations | |
1018042461 | 2018-11-20 | Salt Water Injection Well | No Violations | Currently waiting on Chiefs Order to be issued for authorization to inject. |
1038012474 | 2018-09-04 | Drill / Deepen / Reopen | No Violations | On site today to witness Producers Services try and pump drill string free they were stuck in hole at 7494 free point was 7190 suspect hung in the Beekmantown formation on unstuck rig pulled above tight spot and started to mix gel and once mixed they plan on going to bottom and condition wellbore and then run E-Logs and then run and cement 7 casing in place. |
1194238140 | 2018-08-13 | Casing String Witnessed | No Violations | On site to witness running and cementing of 9.625 casing driller drilled to a depth of 1384 and ran 1315 of casing and Halliburton cemented in place with 430 sacks of Class A cement and they had 30 bbl. of good cement returns. |
1211013000 | 2020-4-28 0:00: | SW | No Violations | |
1260883431 | 2019-12-26 0:00 | SW | No Violations | |
1313262402 | 2019-9-16 0:00: | SW | No Violations | |
1322954743 | 2018-06-27 | Drill / Deepen / Reopen | No Violations | Mitchell Drilling still working on location today. |
1338576724 | 2018-07-30 | Drill / Deepen / Reopen | No Violations | Mitchell Drilling rigging up on well site preparing to drill surface hole. |
1368022502 | 2018-08-23 | Drill / Deepen / Reopen | No Violations | Morning drilling report 5680 drilling a head. |
138256604 | 2019-9-9 0:00:0 | SW | No Violations | |
1450815460 | 2019-03-20 | Salt Water Injection Well | No Violations | Inspection today revealed that injection pumps were in operation during our inspection.
|
1511787575 | 2018-08-30 | Drill / Deepen / Reopen | No Violations | 7272 deep preparing to trip bit. |
1529779364 | 2018-06-23 | Casing String Witnessed | No Violations | On site to witness cementing of conductor pipe, Express Energy drilled a 26 hole to 100 and they ran 100 of new 20 casing and Cemenco cemented it in place with 230 sacks of Class A cement. |
1533488145 | 2018-08-02 | Drill / Deepen / Reopen | No Violations | Inspection today indicated that Mitchell Drilling was at a depth of 147 deep at 7:00 am and when I arrived on they were unloading 13 3/8 casing they received 18 pieces and one shoe and three centralizers should be ready to run casing Friday night or early Saturday morning. |
1533586462 | 2018-08-06 | Drill / Deepen / Reopen | No Violations | Drilling at 850 soaping deviation survey indicated hole was out 7 degrees. |
1533930317 | 2018-08-07 | Drill / Deepen / Reopen | No Violations | Stopped and checked on status of rig they were preparing to go back in hole with reamers and 12.250 bit if they could find enough personnel to run rig. |
1535213411 | 2018-08-21 | Drill / Deepen / Reopen | No Violations | Morning report tripping bit@4853. |
1536504711 | 2018-09-07 | Casing String Witnessed | No Violations | On site to witness casing being run and cementing of casing string.
7388 of pipe ran and Petro Set cemented it in place with 165 sacks Class cement calculated cement top@6388 will confirm with bod log on Monday. |
1536953686 | 2018-09-12 | Drill / Deepen / Reopen | No Violations | On site today to witness bond logging of well to confirm good cement top on backside of 7 casing string cement top was noted at 6000. |
1537211218 | 2018-09-17 | Drill / Deepen / Reopen | No Violations | On site to witness setting of 7casing slips in wellhead rig had to pull 200K to get rotary slips from bowl and then they relaxed pipe and then unbolted Blowout Preventer and picked up assembly and set slips in wellhead and then reassembled stack. |
1538164035 | 2018-09-26 | Drill / Deepen / Reopen | No Violations | Rig check, rig still being repaired once they make repairs they will lay down drill string and then prepare to run injection string and packer. |
1538712751 | 2019-04-24 | Salt Water Injection Well | No Violations | Inspection revealed that injection pumps were not in operation during my inspection.
Truck audits today. |
1539286126 | 2018-10-09 | Drill / Deepen / Reopen | No Violations | On site today to witness Halliburton packer and 4.5 tubing run in well to prepare for injection, ran 7370 0f casing and setting depth of packer is currently 7374 unhooked from packer and circulated freshwater and inhibitor attached back onto packer and will pressure test tomorrow. |
1539313185 | 2018-09-19 | Drill / Deepen / Reopen | No Violations | Drilling 6 1/8 hole on fluid. |
1540134350 | 2018-10-18 | Salt Water Injection Well | No Violations | On site today to witness Halliburton packer and 4.5 injection tubing run in hole, bottom of 7 production casing@7388 and they set packer at 7365 center of element and it was set in compression and on/off tool was released and they pumped fresh water and inhibitor and reattached to packer and pre-tested annulus we will complete official testing on Monday 10/22/18. |
1542408342 | 2018-11-13 | Salt Water Injection Well | No Violations | On site today to witness pressure testing of flowline to well, line consist of 6 outer steel line and 4 inner steel line (welded) and we tested line at 1750 psi and monitored pressure for 15 minutes with no pressure loss(TEST PASSED). |
1579446277 | 2020-1-14 0:00: | SW | No Violations | |
1597349089 | 2020-8-10 0:00: | SW | No Violations | |
1597594158 | 2020-8-13 0:00: | PL | No Violations | |
1618619165 | 2018-08-22 | Drill / Deepen / Reopen | No Violations | Morning report drilling at a depth of 4972.
Air/foam drilling. |
1705836449 | 2018-08-01 | Drill / Deepen / Reopen | No Violations | Still rigging up preparing to start drilling later today. |
1722627504 | 2018-08-10 | Drill / Deepen / Reopen | No Violations | Mitchell Drilling was running deviation survey while I was on site.
6 degrees out noted at this point. |
1772514518 | 2018-08-16 | Drill / Deepen / Reopen | No Violations | 7:00 am morning report 2200 drilling shale, survey indicated that hole was out 3/4 degree. |
1838073639 | 2018-10-04 | Salt Water Injection Well | No Violations | On site to witness packer and tubing run in well, Halliburton packer and 4.5 injection string ran to a setting depth of 7360 and packer was set and they released on/off tool and they circulated inhibitor and they will pressure test at later date(no pressure pump trucks available today). |
1846426413 | 2018-10-30 | Salt Water Injection Well | No Violations | On site today to witness MIT testing of well, they applied 1790 psi on annulus of tubing and we monitored pressure for 15 minutes with no decline in pressure(TEST PASSED).
Once test was completed we hooked up to tubing string and applied pressure to blow off plug on bottom of tubing it took 1400 psi to sheer pins on the plug. |
1883187298 | 2020-4-14 0:00: | SW | No Violations | |
1967882032 | 2019-12-10 0:00 | SW | No Violations | |
1984829481 | 2019-04-14 | Salt Water Injection Well | No Violations | Inspection revealed that injection pumps were not in operation during my inspection.
One Ryan Environmental truck on site during inspection. |
2008676653 | 2018-10-10 | Drill / Deepen / Reopen | No Violations | Attempted to pressure test annulus of tubing after several attempts it was determined that possible hole in production casing. |
2036524374 | 2018-07-16 | Salt Water Injection Well | No Violations | Met with drilling contractor to discuss upcoming drilling of well, we went over Rose Run drilling requirements. |
2090298474 | 2020-6-24 0:00: | SW | No Violations | |
2115181476 | 2018-12-26 | Salt Water Injection Well | No Violations | Inspection today indicated that injection pumps were in operation and injecting to both wells on the day of my inspection. |
2116388940 | 2018-11-02 | Salt Water Injection Well | No Violations | On site to witness spinner testing of said well. |
2130661526 | 2018-08-20 | Drill / Deepen / Reopen | No Violations | Drilling at 4840 soaping. |
275052026 | 2018-8-27 0:00: | DD | No Violations | |
453932366 | 2019-7-18 0:00: | SW | No Violations | |
531045862 | 2019-8-12 0:00: | SW | No Violations | |
612593335 | 2019-7-10 0:00: | SW | No Violations | |
698040343 | 2018-6-20 0:00: | DD | No Violations | |
760376750 | 2019-7-5 0:00:0 | SW | No Violations | |
771741669 | 2020-1-22 0:00: | SW | No Violations | |
779248512 | 2020-3-17 0:00: | SW | No Violations | |
809537598 | 2020-6-18 0:00: | SW | No Violations | |
810575835 | 2020-7-8 0:00:0 | SW | No Violations | |
935001765 | 2019-4-2 0:00:0 | SW | No Violations |
For data sources see[4]