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34-157-25484

Well Details

Well ID: 34-157-25484
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Country: United States
State: Ohio
County: Tuscarawas
Municipality: Rush Township
Operator Name: DIVERSIFIED PRODUCTION LLC
Well Pad ID:
Farm/Lease Name: TATMAN
License Status: Producing
License Date: 2011-08-12
Spud Date: 2011-12-08
Spud Drilling Contractor: POULSON DRILLING
Final Drill Date: 2011-12-13
Well Total Depth: 3850.00 ft
Configuration: Vertical
Latitude: 40.320000
Longitude: -81.320000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2011-08-12 Proposed Formations:ORISKANY, Issued Date:8/12/2011, Expired Date:8/11/2013 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:POOL
Reached Total Depth 2011-12-13
Correction to Well 2012-04-06 CORRECTION TO PROPOSED GEOLOGICAL FORMATION.
Construction Permit Expires 2013-08-11
Completion Report Received 2013-09-17
Change of Owner 2017-10-17 Operator changed from 6866, ATLAS NOBLE LLC to 8685, M & R INVESTMENTS OHIO LLC
Record Last Modified 2017-10-24

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2013-09-17 3410 3478 30
2013-09-17 3762 3772 60
3410 3478 30
3762 3772 60
3410 3478 30

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2013-03-15 H2O 8 1200 Gal 67400 Producers Service Corporation STAGE 2
2012-03-14 H2O 8 72723 Gal 20000 Producers Service Corporation STAGE 1

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2012 ATLAS NOBLE LLC 1852.00 1219.00 266
2013 ATLAS NOBLE LLC 2161.00 665.00 365
2014 ATLAS NOBLE LLC 1352.00 254.00 365
2015 ATLAS NOBLE LLC 1251.00 342.00 365
2016 ATLAS NOBLE LLC 1507.00 459.00 366
2017 ATLAS NOBLE LLC 845.00 493.00 182
2018 M & R INVESTMENTS OHIO LLC 1440.00 455.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2012 ATLAS NOBLE LLC Brine 4260 266
2013 ATLAS NOBLE LLC Brine 1054 365
2014 ATLAS NOBLE LLC Brine 1127 365
2015 ATLAS NOBLE LLC Brine 727 365
2016 ATLAS NOBLE LLC Brine 1402 366
2017 M & R INVESTMENTS OHIO LLC Brine 0 182
2018 M & R INVESTMENTS OHIO LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1390723141 2016-4-15 0:00: PW No Violations 1.00
0084907848 2016-04-14 Production Wells No Violations I received a phone call from Chris Belch with Atlas Energy requesting a inspect of the tank battery where the oil spill accrued. There is no indication of any free oil on the water in the dike. The gravel still needs some bio-sorb or lime used to complete the cleanup on the stone. The cleanup has come along very nicely.
0494580975 2014-09-22 Production Wells No Violations I received a call at 11:00am from Lisa Raffle with Atlas Energy stating that a spill had occurred at he Tatman # 6 well. The amount of the spill was approximately 3 bbls of crude oil and brine. The well pump jack controller was left on manual, causing the tank to overflow. All fluids were contained in the dike system. When I arrived on location I found that a crew of Atlas employees was already cleaning up the spill. A vacuum truck was used to clean up all free fluids. There was no off site exposure to the fluids. Remediation in place shall be done.
1390723141 2016-04-15 Production Wells No Violations Upon arrival on location I found that the cleanup has been completed. There are no signs of free oil in the dike. A coating of Bio-sorb is in place in the dike.
1411487551 2014-09-23 Production Wells No Violations On the day of my inspection I found the employees of Atlas Energy completing the clean up and the remediation of the spill that had occurred. Will re-inspect in 3 to 4 days.
1414083371 2014-10-23 Production Wells No Violations On the day of my inspection, this is a follow up to the reported spill. The dike is still in need of some remediation. Most of the clean up has been effective. The dike has rain water in the dike at this time and there is a small amount of oil scum on the northwest Connor of the dike. I placed a phone call to Chuck with Atlas and discussed the need to use a vacuum truck to remove the water and the oil scum. Chuck agreed to get it done.
1460485139 2016-04-12 Production Wells No Violations I received a phone call from Lisa Raffle with Atlas Energy, at 12:30 pm reporting that they had an oil release in the tank battery. The dump valve on the separator failed in the open position allowing oil to flow out the top of the tank. The release amount is about 10 to 15 gallon of oil. The oil is contained within the dike area. A crew with Atlas Energy is on site and is doing the cleanup. A vacuum truck is removing the fluid in the dike and they are using a power washer to wash down the tanks and the gravel in the dike area. Chris Belch with Atlas Energy is in charge of the cleanup. I placed a phone call to Scott King as he was the Emergency Response Duty Office of the day.
1460635853 2016-04-13 Production Wells No Violations Upon arriving on location I found The Atlas Energy crew continuing cleanup. Absorbent pads are being used and they are still using the power washer. Most of the oil has been recovered and will need to continue monitoring.
1976421429 2011-12-10 Production Wells No Violations On location for surface job. Pits ok.
2080799710 2013-08-06 Preliminary Restoration No Violations Everything passed according to 1509.072A.
494580975 2014-9-22 0:00: PW No Violations
84907848 2016-4-14 0:00: PW No Violations

For data sources see[9]

References