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Well ID: 34-157-24789 | Loading map...
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Country: United States | |
State: Ohio | |
County: Tuscarawas | |
Municipality: Auburn Township | |
Operator Name: RHDK OIL & GAS LLC/DBA RED HIL | |
Well Pad ID: | |
Farm/Lease Name: KIMBLE FLOYD | |
License Status: Producing | |
License Date: 1992-12-23 | |
Spud Date: 1990-10-28 | |
Spud Drilling Contractor: CUBBY DRLG | |
Final Drill Date: 1990-11-03 | |
Well Total Depth: 7259.00 ft | |
Configuration: Vertical | |
Latitude: 40.440000 | |
Longitude: -81.580000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1990-10-10 | 168 RED HILL DEVELOPMENT GeoDate 10/10/90 |
Oil and Gas | 1990-10-10 | Issued Date 10/10/90 Expired Date 10/10/91 Acres 0063785 Tool Type RTAF Proposed Formation CL/ROSE RUN Proposed Depth 07259 Proposed Drill Depth 07259 |
Original Spud | 1990-10-28 | |
Completed | 1990-11-03 | |
Reached Total Depth | 1990-11-03 | |
Completion Report Received | 1991-05-28 | |
CO | 1992-12-23 | 168 RED HILL DEVELOPMENT GeoDate 12/23/92 |
Unknown | 1992-12-23 | Issued Date 12/23/92 Expired Date 12/23/93 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date |
Construction Permit Expires | 1993-12-23 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 7039 | 7122 | 0 |
7039 | 7122 | 0 | |
2006-09-11 | 7044 | 7046 | 3 |
7044 | 7046 | 3 | |
7039 | 7122 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
ACID | 15 | 1500 Gal | 0 | ACIDIZED W/1500 GAL 15% HCL |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-163220585 | 2005-2-24 0:00: | PL | No Violations | |
-211832051 | 2017-8-2 0:00:0 | PW | No Violations | 0.50 |
0000013729 | Preliminary Restoration | No Violations | PASSED Y WITNESSED 8/5/96 INSPECTOR BARRY GRIMM DATE 08/0519/96 DATA FROM OLD VAX INFO | |
0163220585 | 2005-02-24 | Preliminary Restoration | No Violations | restoration ok |
0211832051 | 2017-08-02 | Production Wells | No Violations | On the day of my inspection I found the well equipped with 8 5/8 inch diameter casing 4 1/2 inch diameter casing, and 2 3/8 inch diameter tubing, operated by a plunger lift system. The production equipment is made up of one 100 bbl. fiberglass tank, one horizontal separator, and a recording gauge. The production reporting is up to date, and the tank is properly identified |
1237755310 | 2005-02-24 | Production Wells | No Violations | no violations dike ok |
13729 | PL | No Violations | ||
446196135 | 2020-3-23 0:00: | PW | No Violations | 0.30 |
For data sources see[9]