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Well ID: 34-157-21840 | Loading map...
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Country: United States | |
State: Ohio | |
County: Tuscarawas | |
Municipality: Sugar Creek Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: TROYER M & E UNIT | |
License Status: Final Restoration | |
License Date: 2016-02-19 | |
Spud Date: 1973-06-17 | |
Spud Drilling Contractor: | |
Final Drill Date: 1973-11-08 | |
Well Total Depth: 4401.00 ft | |
Configuration: Vertical | |
Latitude: 40.520000 | |
Longitude: -81.610000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1973-06-01 | 139 MB OPERATING CO INC GeoDate 6/1/73 |
Original Spud | 1973-06-17 | REV. LOC. 6-6-73 |
Completed | 1973-11-08 | REV. LOC. 6-6-73 |
Reached Total Depth | 1973-11-08 | REV. LOC. 6-6-73 |
Change of Owner | 2000-06-30 | Operator changed from 139, MB OPERATING CO INC to 6674, GREAT LAKES ENERGY PTNSHP LLC |
Change of Owner | 2010-04-08 | Operator changed from 6674, RANGE RESOURCES-APPALACHIA LLC to 7578, ENERVEST OPERATING LLC |
APP | 2016-02-19 | Proposed Formations:CLINOTN, Issued Date:2/19/2016, Expired Date:2/18/2018 12:00:00 PM, Drilling unit acres:94, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2017-03-28 | REV. LOC. 6-6-73 |
Record Last Modified | 2017-10-20 | REV. LOC. 6-6-73 |
Construction Permit Expires | 2018-02-18 | REV. LOC. 6-6-73 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4275 | 4363 | 0 |
4275 | 4363 | 0 | |
4275 | 4363 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 2200 Bbl | 0 | AVG. PUMP RATE 61 BPM; AVG. PRESS. W/SD. 2100#; HHP USED 3140. |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | RESOURCE AMERICA INC | 0.00 | 0.00 | 365 |
1985 | RESOURCE AMERICA INC | 711.00 | 0.00 | 365 |
1987 | RESOURCE AMERICA INC | 1074.00 | 0.00 | 365 |
1988 | MB OPERATING CO INC | 873.00 | 0.00 | 366 |
1989 | MB OPERATING CO INC | 732.00 | 0.00 | 365 |
1990 | MB OPERATING CO INC | 653.00 | 0.00 | 365 |
1991 | MB OPERATING CO INC | 497.00 | 0.00 | 365 |
1992 | MB OPERATING CO INC | 332.00 | 0.00 | 366 |
1993 | MB OPERATING CO INC | 41.00 | 0.00 | 365 |
1994 | MB OPERATING CO INC | 0.00 | 0.00 | 365 |
1995 | MB OPERATING CO INC | 21.00 | 0.00 | 365 |
1996 | MB OPERATING CO INC | 26.00 | 0.00 | 366 |
1997 | MB OPERATING CO INC | 114.00 | 0.00 | 365 |
1999 | MB OPERATING CO INC | 0.00 | 0.00 | 273 |
2010 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2011 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2012 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 366 |
2013 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 365 |
2014 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2015 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2016 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 2 |
2017 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | RESOURCE AMERICA INC | Brine | 0 | 365 |
1985 | RESOURCE AMERICA INC | Brine | 0 | 365 |
1987 | RESOURCE AMERICA INC | Brine | 0 | 365 |
1988 | MB OPERATING CO INC | Brine | 0 | 366 |
1989 | MB OPERATING CO INC | Brine | 0 | 365 |
1990 | MB OPERATING CO INC | Brine | 0 | 365 |
1991 | MB OPERATING CO INC | Brine | 0 | 365 |
1992 | MB OPERATING CO INC | Brine | 0 | 366 |
1993 | MB OPERATING CO INC | Brine | 0 | 365 |
1994 | MB OPERATING CO INC | Brine | 0 | 365 |
1995 | MB OPERATING CO INC | Brine | 0 | 365 |
1996 | MB OPERATING CO INC | Brine | 0 | 366 |
1997 | MB OPERATING CO INC | Brine | 0 | 365 |
1999 | MB OPERATING CO INC | Brine | 0 | 273 |
2010 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
2011 | ENERVEST OPERATING LLC | Brine | 0 | |
2012 | ENERVEST OPERATING LLC | Brine | 0 | 366 |
2013 | ENERVEST OPERATING LLC | Brine | 0 | 365 |
2014 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
2015 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
2016 | ENERVEST OPERATING LLC | Brine | 0 | 2 |
2017 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0112212900 | 2017-07-11 | Final Restoration | No Violations | On the day of my inspection, I found that the final restoration has been completed. The site passed final restoration per ORC 1509.072 (B). |
112212900 | 2017-7-11 0:00: | FR | No Violations | 0.50 |
1426598324 | 2015-03-17 | Production Wells | No Violations | On the day of my inspection I found a 8 X 4 inch wellhead and a 4 X 1.5 inch wellhead. Operated by a plunger lift system. The well is idle, the valves are in the off position. The tank battery is made up of a vertical separator, and one 210 bbl tank. The tank has no identification on it. The last year of reported production was 1997. I will call about the ID. The property owner has requested that the well be plugged and abandon. The owner shall secure a plug and abandon permit, and the well shall be plug within 180 days. |
1452107666 | 2016-01-06 | Production Wells | Violations Noted | On the day of my inspection I found a 8 X 4 wellhead and a 4 X 1 1/2 inch wellhead operated by a plunger lift system. The outlet valve was in the off position, the well was idle. The tank battery is made up of one 210 bbl tank. A vertical separator. The last production was in the year of 1997. The owner/operator shall submit a written plugging schedule to Inspector Randy Akins at 2207 Reiser Ave. New Philadelphia, Ohio, 44663 within 30 day, per OAC 1501:9-11-05(B), and plug the well within 180 days. The owner/operator will be notified if the plugging schedule is approved or denied. This is a follow up to complaint ID # 4965. |
1457529290 | 2016-03-09 | Production Wells | No Violations | This is a follow up inspection to NOV-issued on 01/06/2016 and complaint #4965. As of this date EnerVest has not responded to the issued NOV. A plugging plan was to be submitted to this inspector on 02/062016. The status of the well has not changed. |
1467039011 | 2016-06-27 | Production Wells | No Violations | This is a follow up inspection to NOV-issued on 01/06/2016 and complaint #4965. As of this date EnerVest has not responded to the issued NOV. A plugging plan was to be submitted to this inspector on 02/062016. The status of the well has not changed. |
1490207067 | 2017-03-22 | Plug / Plug Back | No Violations | Upon arrival on location I found the rig crew is moving in equipment to start plugging the well. |
1490288736 | 2017-03-23 | Plug / Plug Back | No Violations | |
1490366467 | 2017-03-24 | Plug / Plug Back | No Violations | |
1490626269 | 2017-03-27 | Plug / Plug Back | No Violations | |
1490713284 | 2017-03-28 | Plug / Plug Back | No Violations | |
2091114635 | 2016-10-24 | Production Wells | No Violations | This is a follow up inspection to NOV-issued on 01/06/2016 and complaint #4965. As of this date EnerVest has not responded to the issued NOV. A plugging plan was to be submitted to this inspector on 02/062016. The status of the well has not changed. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1452107666 | US-OH-113085 | 2017-10-23 | Well shall be plugged |
For data sources see[9]