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Well ID: 34-157-21712 | Loading map...
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Country: United States | |
State: Ohio | |
County: Tuscarawas | |
Municipality: Mill Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: MURPHY UNIT | |
License Status: Final Restoration | |
License Date: 2018-09-27 | |
Spud Date: 1972-09-20 | |
Spud Drilling Contractor: | |
Final Drill Date: 1972-10-11 | |
Well Total Depth: 5444.00 ft | |
Configuration: Vertical | |
Latitude: 40.340000 | |
Longitude: -81.320000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1972-08-25 | 311 STOCKER & SITLER INC GeoDate 8/25/72 |
Original Spud | 1972-09-20 | GMM CJHANED PLUG STATUS PER PLUG REPORT. UPDATED LOCATION PER DOGRM SURVEYOR 1/3/19 ALE. |
Completed | 1972-10-11 | GMM CJHANED PLUG STATUS PER PLUG REPORT. UPDATED LOCATION PER DOGRM SURVEYOR 1/3/19 ALE. |
Reached Total Depth | 1972-10-11 | GMM CJHANED PLUG STATUS PER PLUG REPORT. UPDATED LOCATION PER DOGRM SURVEYOR 1/3/19 ALE. |
Change of Owner | 2003-08-11 | Operator changed from 311, STOCKER & SITLER INC to 28, CGAS EXPLORATION |
Change of Owner | 2007-04-27 | Operator changed from 28, CGAS EXPLORATION to 7578, ENERVEST OPERATING LLC |
APP | 2018-09-27 | Proposed Formations:CLINTON SAND, Issued Date:9/27/2018, Expired Date:9/26/2020 12:00:00 PM, Drilling unit acres:468, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2018-10-18 | GMM CJHANED PLUG STATUS PER PLUG REPORT. UPDATED LOCATION PER DOGRM SURVEYOR 1/3/19 ALE. |
Record Last Modified | 2019-01-03 | GMM CJHANED PLUG STATUS PER PLUG REPORT. UPDATED LOCATION PER DOGRM SURVEYOR 1/3/19 ALE. |
Construction Permit Expires | 2020-09-26 | GMM CJHANED PLUG STATUS PER PLUG REPORT. UPDATED LOCATION PER DOGRM SURVEYOR 1/3/19 ALE. |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5246 | 5315 | 0 |
5246 | 5315 | 0 | |
5246 | 5315 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 2100 Bbl | 70000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | STOCKER & SITLER INC | 4570.00 | 52.00 | 365 |
1985 | STOCKER & SITLER INC | 6023.00 | 0.00 | 0 |
1986 | STOCKER & SITLER INC | 2412.00 | 0.00 | 365 |
1987 | STOCKER & SITLER INC | 2303.00 | 43.00 | 365 |
1988 | STOCKER & SITLER INC | 6958.00 | 0.00 | 0 |
1989 | STOCKER & SITLER INC | 5081.00 | 0.00 | 365 |
1990 | STOCKER & SITLER INC | 9311.00 | 0.00 | 365 |
1991 | STOCKER & SITLER INC | 5497.00 | 0.00 | 365 |
1992 | STOCKER & SITLER INC | 4197.00 | 37.00 | 365 |
1993 | STOCKER & SITLER INC | 4507.00 | 0.00 | 365 |
1994 | STOCKER & SITLER INC | 4071.00 | 0.00 | 0 |
1995 | STOCKER & SITLER INC | 1577.00 | 0.00 | 0 |
1996 | STOCKER & SITLER INC | 0.00 | 0.00 | 0 |
1997 | STOCKER & SITLER INC | 0.00 | 0.00 | 365 |
1998 | STOCKER & SITLER INC | 3969.00 | 0.00 | 365 |
1999 | STOCKER & SITLER INC | 4761.00 | 0.00 | 365 |
2000 | STOCKER & SITLER INC | 4262.00 | 0.00 | 365 |
2001 | STOCKER & SITLER INC | 1859.00 | 0.00 | 365 |
2002 | STOCKER & SITLER INC | 1574.00 | 0.00 | 365 |
2003 | CGAS EXPLORATION | 2438.00 | 0.00 | 365 |
2004 | CGAS EXPLORATION | 3637.00 | 0.00 | 365 |
2005 | CGAS EXPLORATION | 2553.00 | 0.00 | 365 |
2006 | CGAS EXPLORATION | 2222.00 | 0.00 | 365 |
2007 | ENERVEST OPERATING LLC | 2338.00 | 0.00 | 365 |
2008 | ENERVEST OPERATING LLC | 2221.00 | 0.00 | 365 |
2009 | ENERVEST OPERATING LLC | 2750.00 | 36.00 | 365 |
2010 | ENERVEST OPERATING LLC | 1997.00 | 0.00 | 365 |
2011 | ENERVEST OPERATING LLC | 3951.00 | 0.00 | 365 |
2012 | ENERVEST OPERATING LLC | 3360.00 | 0.00 | 366 |
2013 | ENERVEST OPERATING LLC | 1321.00 | 0.00 | 365 |
2014 | ENERVEST OPERATING LLC | 76.00 | 0.00 | 365 |
2015 | ENERVEST OPERATING LLC | 5.00 | 0.00 | 31 |
2016 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2017 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2018 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1567690009 | 2018-10-18 0:00 | PB | No Violations | 5.70 |
-1570824948 | 2018-5-11 0:00: | PW | No Violations | 0.50 |
-545226434 | 2018-10-16 0:00 | PB | No Violations | 6.40 |
-744505200 | 2019-8-7 0:00:0 | FR | No Violations | 0.50 |
0545226434 | 2018-10-16 | Plug / Plug Back | No Violations | Upon my arrival on location, accompanied by ODNR Inspector Bob Roush and ODNR Senior Legal Counsel Eric Vendel, I witnessed the rig attempting to circulate the 1.5 inch diameter tubing out of the well, the attempt failed. Appalachian Well Surveyors showed up on location to shoot the tubing off. They started down 1.5 inch tubing and stopped at 4065 feet by an obstruction. They tripped out of the well. The rig crew sent their 1.5 inch tools back down into the well. They moved the obstruction to the depth of 4318 feet. They had Appalachian Well Surveyors go back down into the well and shoot the tubing off at the depth of 4303 feet. The rig crew will now trip the 1.5 inch tubing out of the well. |
1492432418 | 2017-04-17 | Production Wells | No Violations | |
1539801425 | 2018-10-15 | Plug / Plug Back | No Violations | Upon my arrival on location, I witnessed the rig crew rigging up the service rig. They started to blow down the well. They finished rigging up and dug a pit with the dozer. They spotted the 5 axle on location to lay the tubing on. They attempted to pull the 1.5 inch diameter tubing. The tubing would not move. They will try to circulate the tubing out of the well, in the morning. |
1539867710 | 2018-10-17 | Plug / Plug Back | No Violations | Upon my arrival on location, accompanied by ODNR Inspector Bob Roush and ODNR District Supervisor Mike Moreland, I witnessed the rig crew was rigging up the 4.5 inch diameter casing ripping tool. They lower ripping tool into the well to the depth of 3825 feet. They proceeded to rip the 4.5 inch diameter casing off at that depth. They tripped the tools out of the well and pulled one joint of casing. Putting the bottom of the casing at the depth of 3791 feet. They circulated the well till it cleaned up, with 280 barrels of fresh water. The well stayed equalized. The cement crew set a 400 foot (115 sks), Class A cement plug. The cement was scaled at 15.2 weight. The water they used for the cement, tested at 50 degrees, with the pH of 10, and the chlorides were at 70 ppm. The footage of the cement plug was 3791 feet to 3391 feet. The rig crew started to pull 84 joints of 4.5 inch diameter casing out of the well, to the depth of 1132 feet. The cement crew established circulation on the well. They started to set a 200 foot, Class A cement plug, when the circulation water started to cloud up with cement returns. Bob and I stopped cementing and circulated all the cement out of the well, till the circulation water cleaned back up. The rig crew started to pull the remaining 4.5 inch casing out of the well. They pulled 7 joints and we found the hole in the casing. The rig crew will tag the Lime plug in the morning, before we continue plugging the well. |
1567690009 | 2018-10-18 | Plug / Plug Back | No Violations | Upon my arrival on location, accompanied by ODNR Inspector Bob Roush, I witnessed the rig crew rigging up the tools to go down into the well. They tagged the top of the bottom cement plug at the depth of 3106 feet. Bob and I called ODNR District Supervisor Mike Moreland about the information we had obtained from the rig operator. We all were all right with the placement of the existing plug they set yesterday. We are going to make Enervest set a larger cement plug at the bottom of the 8.625 inch diameter casing and a larger cement plug at the surface. The rig crew started to run 1.5 inch diameter tubing back into the well. They will run the tubing to the depth of 1232 feet. The cement crew established circulation on the well, then set a 300 foot (95 sks), Class A cement plug. The cement was scaled at the weight of 15.3. The water used for mixing cement tested at 48 degrees, chlorides at 98 ppm, and pH of 6. They displaced the cement with 2.3 barrels of fresh water. The rig crew pulled 32 joints of tubing out of the well to the depth of 200 feet. The cement crew established circulation on the well, then set a 200 foot (60 sks), Class A cement plug. They pumped until we seen good cement returns. The rig crew pulled the remaining 6 joints of tubing out of the well. The rig crew rigged the service rig down and moved all equipment off location. They filled the pit in with the dozer and dug around the well. They cut the 8.625 inch diameter casing off 30 inches below the ground level. They put a steel plate on top of the well, with the permit number inscribe on it. They then backfilled around the well and graded the whole location. The location will not have to be seeded, because the location is in the middle of a bean field. A roustabout crew will come in on a later date to remove the production equipment at the edge of the field. |
1570824948 | 2018-05-11 | Production Wells | No Violations | Upon arrival on location, I witnessed the well was equipped 4.5 inch diameter casing, 1.5 inch diameter tubing, and a plunger lift system. The valves were closed on tubing and one of two valves were open on the casing. The sale line valve was closed going towards production equipment. The well was idle at the time of the inspection. Production equipment included a steel 210 barrel tank, a steel 50 barrel tank, a horizonal separator, and a chart recorder with an 2 inch by .875 inch orifice plate within an earthen dike. The production report was up to date but showed no production since 2016. Proper identification was present at this time. |
For data sources see[9]