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34-157-21458

Well Details

Well ID: 34-157-21458
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Country: United States
State: Ohio
County: Tuscarawas
Municipality: Perry Township
Operator Name: ENERVEST OPERATING LLC
Well Pad ID:
Farm/Lease Name: GRAY J ETAL UNIT
License Status: Final Restoration
License Date: 2012-06-20
Spud Date: 1971-09-28
Spud Drilling Contractor:
Final Drill Date: 1971-10-20
Well Total Depth: 5600.00 ft
Configuration: Vertical
Latitude: 40.270000
Longitude: -81.410000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1971-09-08 311 STOCKER & SITLER INC GeoDate 9/8/71
Original Spud 1971-09-28
Completed 1971-10-20
Reached Total Depth 1971-10-20
CO 1995-04-20 182 BELDEN & BLAKE CO GeoDate 9/8/71
Change of Owner 2007-04-27 Operator changed from 182, BELDEN & BLAKE CORPORATION to 7578, ENERVEST OPERATING LLC
APP 2012-06-20 Proposed Formations:CLINTON, Issued Date:6/20/2012, Expired Date:6/20/2014 12:00:00 PM, Drilling unit acres:639.57, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2014-06-05
Construction Permit Expires 2014-06-20
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 5448 5512 1
5448 5512 1
5448 5512 1

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 2100 Bbl 70000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 DOMINION EAST OHIO 4674.00 46.00 0
1985 DOMINION EAST OHIO 4181.00 34.00 365
1986 DOMINION EAST OHIO 3448.00 41.00 365
1987 DOMINION EAST OHIO 0.00 0.00 358
1988 DOMINION EAST OHIO 0.00 0.00 336
1989 DOMINION EAST OHIO 0.00 0.00 363
1990 DOMINION EAST OHIO 3225.00 12.00 365
1991 DOMINION EAST OHIO 2737.00 0.00 365
1992 DOMINION EAST OHIO 2941.00 0.00 365
1993 DOMINION EAST OHIO 0.00 0.00 365
1994 DOMINION EAST OHIO 0.00 0.00 365
1995 BELDEN & BLAKE CORPORATION 124.00 0.00 365
2005 BELDEN & BLAKE CORPORATION 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 DOMINION EAST OHIO Brine 0 0
1985 DOMINION EAST OHIO Brine 0 365
1986 DOMINION EAST OHIO Brine 0 365
1987 DOMINION EAST OHIO Brine 0 358
1988 DOMINION EAST OHIO Brine 0 336
1989 DOMINION EAST OHIO Brine 0 363
1990 DOMINION EAST OHIO Brine 0 365
1991 DOMINION EAST OHIO Brine 0 365
1992 DOMINION EAST OHIO Brine 0 365
1993 DOMINION EAST OHIO Brine 0 365
1994 DOMINION EAST OHIO Brine 0 365
1995 BELDEN & BLAKE CORPORATION Brine 0 365
2005 BELDEN & BLAKE CORPORATION Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1330697557 2012-02-15 Production Wells Violations Noted Arrived on location and found well idle , checked production reports none reported since 1996. Within 30 days apply for a plug permit.
1365702099 2013-04-11 Final Restoration No Violations I arrived on location and found well plugged and final restoration complete and approved. Case closed 04/11/2013.
1383589999 2012-02-16 Production Wells No Violations I arrived on location and found well plugged .gas leak in 41/2casing repaired. Case closed 12/16/2013
1401801350 2014-06-03 Plug / Plug Back No Violations On my arrival on location ChipCo was prepairing to plug well. The 1 1/2 inch tubing was removed from the well and inspected. The tubing was tallied and made ready to run back in the well, and start plugging.
1401972699 2014-06-04 Plug / Plug Back No Violations On the day of my inspection Chipco ripped the 4.5 casing at 4060 They pulled one joint and set a 300 cement plug at the top of the Big Lime. The well started blowing gas when they were circulating prior to setting the plug. Chipco circulated approximately 70 barrels of oil out of the well and eventually got the gas blown down. They pulled 20 joints and circulated the hole again after setting the plug.
1567687552 2014-06-05 Plug / Plug Back No Violations On the day of my inspection Chipco pulled the 4.5 casing up to 1530, where they set a 200 cement plug at the base of the 8.625 surface casing. Good circulation was maintained while pumping the plug. They pulled the 4.5 casing up to approximately 200 and checked the fluid level. The fluid was at 200 so the pulled the rest of the casing and set a brush and stone bridge. Chipco filled the well to surface with class A cement. The surface casing was already cut off 36 below grade. Chipco had a steel plate inscribed with 1458 to place over the casing.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1330697557 US-OH-109478 2012-03-02 Well shall be plugged

For data sources see[9]

References