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34-157-20937

Well Details

Well ID: 34-157-20937
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Country: United States
State: Ohio
County: Tuscarawas
Municipality: Dover Township
Operator Name: MAINSPRING LLC
Well Pad ID:
Farm/Lease Name: WIDDER BEN F
License Status: Producing
License Date: 1964-11-06
Spud Date: 1964-11-02
Spud Drilling Contractor:
Final Drill Date: 1964-11-30
Well Total Depth: 998.00 ft
Configuration: Vertical
Latitude: 40.480000
Longitude: -81.550000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1964-11-02
Completed 1964-11-30
Reached Total Depth 1964-11-30
CO 1993-08-17 3214 ECHO DRILLING INC
Change of Owner 2016-09-23 Operator changed from 3214, ECHO DRILLING INC to 9781, MAINSPRING LLC
Record Last Modified 2016-09-23

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 954 990 0
954 990 0
954 990 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
NITR 0 90 Qts 0 12-2-64

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 ECHO DRILLING INC 0.00 41.00 365
1985 ECHO DRILLING INC 0.00 38.00 365
1986 ECHO DRILLING INC 0.00 49.00 365
1987 ECHO DRILLING INC 0.00 43.00 365
1988 ECHO DRILLING INC 0.00 54.00 365
1989 ECHO DRILLING INC 0.00 22.00 365
1990 ECHO DRILLING INC 0.00 20.00 365
1991 ECHO OIL & GAS CO 0.00 47.00 365
1992 ECHO DRILLING INC 0.00 29.00 365
1993 ECHO DRILLING INC 0.00 26.00 365
1994 ECHO DRILLING INC 0.00 34.00 349
1995 ECHO DRILLING INC 0.00 18.00 355
1996 ECHO DRILLING INC 0.00 33.00 365
1997 ECHO DRILLING INC 0.00 26.00 365
1998 ECHO DRILLING INC 0.00 20.00 365
1999 ECHO DRILLING INC 0.00 17.00 365
2000 ECHO DRILLING INC 0.00 44.00 354
2001 ECHO DRILLING INC 0.00 24.00 363
2002 ECHO DRILLING INC 0.00 18.00 365
2003 ECHO DRILLING INC 0.00 20.00 365
2004 ECHO DRILLING INC 0.00 18.00 365
2005 ECHO DRILLING INC 0.00 18.00 365
2006 ECHO DRILLING INC 0.00 0.00 365
2007 ECHO DRILLING INC 0.00 0.00 365
2008 ECHO DRILLING INC 0.00 16.00 365
2009 ECHO DRILLING INC 0.00 37.00 365
2010 ECHO DRILLING INC 0.00 18.00 357
2011 ECHO DRILLING INC 0.00 18.00 357
2012 ECHO DRILLING INC 0.00 24.00 366
2013 ECHO DRILLING INC 0.00 12.00 353
2014 ECHO DRILLING INC 0.00 0.00 25
2016 ECHO DRILLING INC 0.00 0.00 0
2017 MAINSPRING LLC 0.00 74.00 205
2018 MAINSPRING LLC 0.00 74.00 205

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 ECHO DRILLING INC Brine 0 365
1985 ECHO DRILLING INC Brine 60 365
1986 ECHO DRILLING INC Brine 60 365
1987 ECHO DRILLING INC Brine 40 365
1988 ECHO DRILLING INC Brine 20 365
1989 ECHO DRILLING INC Brine 40 365
1990 ECHO DRILLING INC Brine 20 365
1991 ECHO OIL & GAS CO Brine 40 365
1992 ECHO DRILLING INC Brine 20 365
1993 ECHO DRILLING INC Brine 20 365
1994 ECHO DRILLING INC Brine 60 349
1995 ECHO DRILLING INC Brine 80 355
1996 ECHO DRILLING INC Brine 80 365
1997 ECHO DRILLING INC Brine 140 365
1998 ECHO DRILLING INC Brine 80 365
1999 ECHO DRILLING INC Brine 60 365
2000 ECHO DRILLING INC Brine 80 354
2001 ECHO DRILLING INC Brine 20 363
2002 ECHO DRILLING INC Brine 20 365
2003 ECHO DRILLING INC Brine 40 365
2004 ECHO DRILLING INC Brine 220 365
2005 ECHO DRILLING INC Brine 240 365
2006 ECHO DRILLING INC Brine 240 365
2007 ECHO DRILLING INC Brine 220 365
2008 ECHO DRILLING INC Brine 312 365
2009 ECHO DRILLING INC Brine 306 365
2010 ECHO DRILLING INC Brine 391 357
2011 ECHO DRILLING INC Brine 391 357
2012 ECHO DRILLING INC Brine 400 366
2013 ECHO DRILLING INC Brine 363 353
2014 ECHO DRILLING INC Brine 0 25
2016 ECHO DRILLING INC Brine 0 0
2017 MAINSPRING LLC Brine 225 205
2018 MAINSPRING LLC Brine 70 205

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-2039531856 2017-8-28 0:00: PW No Violations
0570972057 2018-09-13 Production Wells No Violations This inspection was a follow up to a compliance notice number 2026805155, issued on 8/21/17 by ODNR Inspector Todd Miller. Upon arrival on location, I witnessed the contaminated area around the pumping was cleaned up. There was vegetation growing all around the pumping unit. This compliance notice can be closed out. The well was equipped with 3 inch diameter casing, 1.5 inch tubing, rods, and a pumping unit ran with an electric motor. The valves on the wellhead were open. The production equipment included two steel 210 barrel tanks, a water knockout, and a plastic 100 barrel tank within an earthen dike. The production equipment was being shared with the Widder 2 (0712) and the Widder 1 (0703). The production report was up to date and proper identification was present.
2026805155 2017-08-21 Production Wells Violations Noted This is a producing pump jack well. The stuffing box is leaking and there is free oil on the ground at the wellhead. There is oil contaminated soil where the hill breaks over. There is no identification at the well. There were no other problems noted at the time of the inspection. The oil needs cleaned up and the oil contaminated soil removed.
2039531856 2017-08-28 Production Wells No Violations The operator was in the process of cleaning up the oil contaminated soil around the well when I was there. Will check back later.
570972057 2018-9-13 0:00: PW No Violations 0.30

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
2026805155 US-OH-120611 2017-10-18 9-1-07 Well operation causing pollution and contamination
2026805155 US-OH-120612 2017-10-18 9-9-05(A)1 Well insufficiently equipped to prevent escape of oil and gas
2026805155 US-OH-120613 2017-10-18 9-9-05(A)10 Failure to legibly identify well

For data sources see[9]

References