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34-157-20454

Well Details

Well ID: 34-157-20454
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Country: United States
State: Ohio
County: Tuscarawas
Municipality: Warren Township
Operator Name: ENERVEST OPERATING LLC
Well Pad ID:
Farm/Lease Name: GOODERDING AL
License Status: Final Restoration
License Date: 2014-08-11
Spud Date: 1952-06-05
Spud Drilling Contractor:
Final Drill Date: 1952-09-29
Well Total Depth: 5136.00 ft
Configuration: Vertical
Latitude: 40.520000
Longitude: -81.330000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1952-06-05
Completed 1952-09-29
Reached Total Depth 1952-09-29
Completion Report Received 1952-10-06
Change of Owner 2007-04-27 Operator changed from 182, BELDEN & BLAKE CORPORATION to 7578, ENERVEST OPERATING LLC
APP 2012-06-08 Proposed Formations:CLINTON, Issued Date:6/8/2012, Expired Date:6/8/2014 12:00:00 PM, Drilling unit acres:159.75, Proposed Well Type:OG, Proposed Well Class:
APP 2014-08-11 Proposed Formations:CLINTON, Issued Date:8/11/2014, Expired Date:8/10/2016 12:00:00 PM, Drilling unit acres:159.75, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2015-03-06
Construction Permit Expires 2016-08-10
Record Last Modified 2017-02-15

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 KST OIL & GAS CO INC 4682.00 0.00 365
1986 KST OIL & GAS CO INC 4528.00 0.00 365
1987 KST OIL & GAS CO INC 3365.00 0.00 365
1988 KST OIL & GAS CO INC 6684.00 0.00 365
1989 KST OIL & GAS CO INC 6837.00 0.00 365
1990 KST OIL & GAS CO INC 9418.00 0.00 365
1991 KST OIL & GAS CO INC 6502.00 0.00 365
1992 KST OIL & GAS CO INC 5471.00 0.00 365
1993 KST OIL & GAS CO INC 5219.00 0.00 365
1994 KST OIL & GAS CO INC 4291.00 0.00 365
1995 KST OIL & GAS CO INC 1589.00 0.00 365
1996 BELDEN & BLAKE CORPORATION 1082.00 0.00 380
1997 BELDEN & BLAKE CORPORATION 3075.00 0.00 365
1998 BELDEN & BLAKE CORPORATION 1056.00 0.00 358
1999 BELDEN & BLAKE CORPORATION 710.00 0.00 363
2000 BELDEN & BLAKE CORPORATION 423.00 0.00 340
2001 BELDEN & BLAKE CORPORATION 637.00 0.00 364
2002 BELDEN & BLAKE CORPORATION 1799.00 0.00 229
2003 BELDEN & BLAKE CORPORATION 2272.00 41.00 259
2004 BELDEN & BLAKE CORPORATION 800.00 0.00 366
2005 BELDEN & BLAKE CORPORATION 0.00 0.00 365
2007 ENERVEST OPERATING LLC 0.00 0.00 0
2008 ENERVEST OPERATING LLC 0.00 0.00 0
2009 ENERVEST OPERATING LLC 0.00 0.00 0
2010 ENERVEST OPERATING LLC 0.00 0.00 0
2011 ENERVEST OPERATING LLC 0.00 0.00 0
2012 ENERVEST OPERATING LLC 0.00 0.00 0
2013 ENERVEST OPERATING LLC 0.00 0.00 365
2014 ENERVEST OPERATING LLC 0.00 0.00 0
2015 ENERVEST OPERATING LLC 0.00 0.00 0

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 KST OIL & GAS CO INC Brine 0 365
1986 KST OIL & GAS CO INC Brine 0 365
1987 KST OIL & GAS CO INC Brine 0 365
1988 KST OIL & GAS CO INC Brine 0 365
1989 KST OIL & GAS CO INC Brine 0 365
1990 KST OIL & GAS CO INC Brine 0 365
1991 KST OIL & GAS CO INC Brine 0 365
1992 KST OIL & GAS CO INC Brine 0 365
1993 KST OIL & GAS CO INC Brine 0 365
1994 KST OIL & GAS CO INC Brine 0 365
1995 KST OIL & GAS CO INC Brine 0 365
1996 BELDEN & BLAKE CORPORATION Brine 0 380
1997 BELDEN & BLAKE CORPORATION Brine 0 365
1998 BELDEN & BLAKE CORPORATION Brine 0 358
1999 BELDEN & BLAKE CORPORATION Brine 0 363
2000 BELDEN & BLAKE CORPORATION Brine 0 340
2001 BELDEN & BLAKE CORPORATION Brine 0 364
2002 BELDEN & BLAKE CORPORATION Brine 43 229
2003 BELDEN & BLAKE CORPORATION Brine 12 259
2004 BELDEN & BLAKE CORPORATION Brine 0 366
2005 BELDEN & BLAKE CORPORATION Brine 0 365
2007 ENERVEST OPERATING LLC Brine 0 0
2008 ENERVEST OPERATING LLC Brine 0 0
2009 ENERVEST OPERATING LLC Brine 0 0
2010 ENERVEST OPERATING LLC Brine 0 0
2011 ENERVEST OPERATING LLC Brine 0
2012 ENERVEST OPERATING LLC Brine 0 0
2013 ENERVEST OPERATING LLC Brine 0 365
2014 ENERVEST OPERATING LLC Brine 0 0
2015 ENERVEST OPERATING LLC Brine 0 0

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1242314795 2015-2-27 0:00: PB No Violations 9.00
-172887733 2015-3-6 0:00:0 PB No Violations 5.00
0172887733 2015-03-06 Plug / Plug Back No Violations
0700156476 2015-03-05 Plug / Plug Back No Violations
1242314795 2015-02-27 Plug / Plug Back No Violations Upon arrival on location I found the crew preparing to set the bottom plug. 1 joint of 1.5 tubing was picked up and run in the wellbore to a depth of 5080 feet, leaving 1/2 of joint up in the air. That joint was laid down and a 400 foot plug was set at 5070 feet. The 1 1/2 inch tubing was pulled from the well bore
1303867364 2015-08-19 Final Restoration No Violations On the day of my inspection I found that the final restoration has been completed. The site passed final restoration according to ORC 1509.072 (B).
1424880214 2015-02-24 Plug / Plug Back No Violations Received a phone call from ChipCo that they were moving in on the well and going to plug the well. Upon arrival on location I found the rigging up and preparing to plug the well.
1425047460 2015-02-26 Plug / Plug Back No Violations Upon arrival on location I found the crew preparing to pull the 3.5 inch tubing. The tubing would not move. 1.5 tubing was then run to the depth of 5066 feet and shut-in for the night.
1425322855 2015-03-02 Plug / Plug Back No Violations Upon arrival on location I found the crew ready to continue plugging. The crew ran 1.5 inch tubing in the wellbore on Saturday to a depth of 5066 feet. It was determined this morning that the 1.5 inch tubing was hung in the well and could not be pulled. We pumped on the tubing and was able to circulate the well, but was still unable to pull the tubing. We attempted to shoot off the tubing at 4600 feet and it still would not pull. We then shot off tubing at 3103 feet, and was able to pull the 1.5 inch tubing.
1425406226 2015-03-03 Plug / Plug Back No Violations Upon arrival on location I found the crew ready to shoot off the 3.5 inch tubing. Shot off the tubing at 3075 feet and are removing the tubing from the wellbore.
1425478099 2015-03-04 Plug / Plug Back No Violations Upon arrival I found that the rig crew has ripped the 5.5 casing at 3038 feet. Will pull 1 joint and set lime plug. Set plug at 3018 feet to 2668 feet. Pulled casing up to 1115 feet and set a plug to 915 feet at the bottom of the surface casing. Pulled 5.5 casing out of well.
1425568737 2015-03-05 Plug / Plug Back No Violations Upon arrival on location I was accompanied by Pat Shreve. We ran a slick line into the well bore to tag the top of the cement plug and found the top at 930 feet. Rig shut down do to weather.
1425651048 2015-03-06 Plug / Plug Back No Violations Upon arrival on location I found the rig crew ready to continue plugging . They had 600 feet of 1.5 tubing in the wellbore. We circulated the well to clean up well. Ran in with a casing ripper to rip the 8 inch casing. Ripped casing at 300 feet, pulled out 6 feet and the casing pulled a part. 8 inch casing was full of hole and unable to pull any more. Ran in with 1.5 tubing to cement to surface, starting at a depth of 340 feet. Established circulation and pumped cement to surface. We had good returns to surface. Cement dropped two feet. Job complete.
1503083838 2015-02-26 Plug / Plug Back No Violations On the date of inspection I accompanied Randy Akins to the well that was currently being plugged. We had expected to set a plug but the cementers were cancelled. Chipco was in the process of running 1.5 inch tubing.
700156476 2015-3-5 0:00:0 PB No Violations 4.00

For data sources see[7]

References