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Well ID: 34-155-22107 | Loading map...
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Country: United States | |
State: Ohio | |
County: Trumbull | |
Municipality: Liberty Township | |
Operator Name: OHIO VALLEY ENERGY SYSTEMS COR | |
Well Pad ID: | |
Farm/Lease Name: NATIONAL NORTHERN INC | |
License Status: Producing | |
License Date: 1982-03-01 | |
Spud Date: 1982-03-02 | |
Spud Drilling Contractor: | |
Final Drill Date: 1982-03-08 | |
Well Total Depth: 5182.00 ft | |
Configuration: Vertical | |
Latitude: 41.200000 | |
Longitude: -80.650000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1982-03-01 | 2125 EASTERN PETROLEUM CO GeoDate 3/1/82 |
Oil and Gas | 1982-03-01 | Issued Date 12/31/81 Expired Date 6/29/82 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05182 Proposed Drill Depth 05182 |
Original Spud | 1982-03-02 | |
Completed | 1982-03-08 | |
Reached Total Depth | 1982-03-08 | |
Construction Permit Expires | 1982-06-29 | |
Completion Report Received | 1986-06-04 | |
CO | 1992-10-08 | 2456 SIMCO EXPLORATION CORP GeoDate 3/1/82 |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4979 | 5051 | 2 |
4979 | 5051 | 2 | |
4979 | 5051 | 2 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1830 Bbl | 60000 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0000PL4049 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
1481203706 | 2016-12-07 | UrbanProduction Wells | No Violations
| |
1714840391 | 2018-12-03 | UrbanProduction Wells | No Violations | Status check inspection of this Clinton Sandstone well. My inspection found the wellhead equipped with 1.5 tubing and operating with the aid of a plunger lift system. Gauges indicate 330psi on the 4.5 production casing and 260psi on the tubing. This well produces to a diked tank battery near the lease road entrance and contains one (1) 100 barrel tank. The horizontal separator is located just south of the battery and is outside containment. A gauge at the separator indicates a production pressure of 70psi. The valves on the tank and the separator doors are equipped with locks and the load lines are fitted with bull plugs. The required ID is posted on the tank. This well was drilled prior to HB278 and its location does not warrant urban compliance at this time. No violations. |
1881146025 | 2013-10-28 | UrbanProduction Wells | No Violations | My inspection found the well in production. The well was equipped with a plunger lift unit. The tank battery consisted of a 100 barrel production tank, a buried, concrete brine tank, and a separator. The dike met containment requirements. There was a plug on the load line. An identification sign was properly posted. The lease road was in good condition with a locked gate at the entrance. The well was placed into production prior to House Bill 278. |
PL4049 | PL | No Violations |
For data sources see[9]