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34-155-21553

Well Details

Well ID: 34-155-21553
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Country: United States
State: Ohio
County: Trumbull
Municipality: Bristol Township
Operator Name: VORTEX ENERGY LLC
Well Pad ID:
Farm/Lease Name: STROM
License Status: Producing
License Date: 1981-06-24
Spud Date: 1981-10-01
Spud Drilling Contractor: MOBILE AIR DRLG
Final Drill Date: 1981-10-05
Well Total Depth: 4145.00 ft
Configuration: Vertical
Latitude: 41.410000
Longitude: -80.870000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1981-06-24 130 LESLIE OIL & GAS CO INC GeoDate 6/24/81
Oil and Gas 1981-06-24 Issued Date 6/24/81 Expired Date 6/24/82 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 04145 Proposed Drill Depth 04145
Original Spud 1981-10-01 PERMIT EXPIRED.
Completed 1981-10-05 PERMIT EXPIRED.
Reached Total Depth 1981-10-05 PERMIT EXPIRED.
Construction Permit Expires 1982-06-24 PERMIT EXPIRED.
Completion Report Received 1993-11-02 PERMIT EXPIRED.
CO 1993-12-15 54 TITAN ENERGY CORP GeoDate 6/24/81
Change of Owner 1998-01-26 Operator changed from 54, TITAN ENERGY CORP to 1333, BARR ROBT/dba BIG SKY PET
Change of Owner 2018-09-11 Operator changed from 1333, BIG SKY ENERGY INC to 9841, VORTEX ENERGY LLC
Record Last Modified 2018-09-11 PERMIT EXPIRED.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 3890 4061 0
3890 4061 0
2006-09-11 3898 4061 15
3898 4061 15
3890 4061 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 0 0 FRAC'D

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 LESLIE OIL & GAS CO INC 1479.00 696.00 365
1986 LESLIE OIL & GAS CO INC 1538.00 526.00 365
1989 LESLIE OIL & GAS CO INC 76.00 664.00 365
1990 LESLIE OIL & GAS CO INC 365.00 521.00 365
1991 LESLIE OIL & GAS CO INC 367.00 496.00 365
1992 TITAN ENERGY CORP 366.00 431.00 365
1993 TITAN ENERGY CORP 407.00 370.00 365
1994 TITAN ENERGY CORP 373.00 411.00 365
1996 EASTERN STATES OIL & GAS INC 4320.00 0.00 365
1997 EASTERN STATES OIL & GAS INC 4052.00 0.00 365
1998 EASTERN STATES OIL & GAS INC 4134.00 56.00 365
1999 EASTERN STATES OIL & GAS INC 0.00 0.00 0
2000 BIG SKY ENERGY INC 66.00 269.00 365
2001 BIG SKY ENERGY INC 380.00 137.00 365
2002 BIG SKY ENERGY INC 797.00 244.00 365
2003 BIG SKY ENERGY INC 341.00 164.00 365
2004 BIG SKY ENERGY INC 1247.00 188.00 365
2005 BIG SKY ENERGY INC 1177.00 125.00 365
2006 BIG SKY ENERGY INC 1800.00 211.00 365
2007 BIG SKY ENERGY INC 1336.00 0.00 365
2008 BIG SKY ENERGY INC 436.00 89.00 365
2009 BIG SKY ENERGY INC 2112.00 128.00 365
2010 BIG SKY ENERGY INC 2800.00 0.00 365
2011 BIG SKY ENERGY INC 778.00 146.00 365
2012 BIG SKY ENERGY INC 965.00 154.00 366
2013 BIG SKY ENERGY INC 303.00 64.00 280
2014 BIG SKY ENERGY INC 522.00 70.00 365
2016 BIG SKY ENERGY INC 118.00 0.00 98
2017 BIG SKY ENERGY INC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 LESLIE OIL & GAS CO INC Brine 300 365
1986 LESLIE OIL & GAS CO INC Brine 310 365
1989 LESLIE OIL & GAS CO INC Brine 0 365
1990 LESLIE OIL & GAS CO INC Brine 0 365
1991 LESLIE OIL & GAS CO INC Brine 0 365
1992 TITAN ENERGY CORP Brine 0 365
1993 TITAN ENERGY CORP Brine 100 365
1994 TITAN ENERGY CORP Brine 119 365
1996 EASTERN STATES OIL & GAS INC Brine 0 365
1997 EASTERN STATES OIL & GAS INC Brine 365
1998 EASTERN STATES OIL & GAS INC Brine 365
1999 EASTERN STATES OIL & GAS INC Brine
2000 BIG SKY ENERGY INC Brine 0 365
2001 BIG SKY ENERGY INC Brine 0 365
2002 BIG SKY ENERGY INC Brine 0 365
2003 BIG SKY ENERGY INC Brine 0 365
2004 BIG SKY ENERGY INC Brine 0 365
2005 BIG SKY ENERGY INC Brine 0 365
2006 BIG SKY ENERGY INC Brine 0 365
2007 BIG SKY ENERGY INC Brine 0 365
2008 BIG SKY ENERGY INC Brine 0 365
2009 BIG SKY ENERGY INC Brine 0 365
2010 BIG SKY ENERGY INC Brine 0 365
2011 BIG SKY ENERGY INC Brine 0 365
2012 BIG SKY ENERGY INC Brine 0 366
2013 BIG SKY ENERGY INC Brine 255 280
2014 BIG SKY ENERGY INC Brine 77 365
2016 BIG SKY ENERGY INC Brine 0 98
2017 BIG SKY ENERGY INC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1280386752 2008-8-18 0:00: PW No Violations
-1302781606 2017-12-7 0:00: PW No Violations 0.70
-1405226355 2017-3-21 0:00: PW No Violations 0.60
-1725869349 2018-3-6 0:00:0 PW No Violations 1.00
-227464710 2019-2-8 0:00:0 PW No Violations 0.70
0079868289 2016-04-29 Production Wells Violations Noted I was on location in reference to compliance to Chiefs Order 2016-

Big Sky needs to: Shut in the well immediately per the temporary restraining order issued by the Trumbull County Court of Common Pleas dated 4-11-2016 Remove and dispose of all impacted soil and vegetation at the well. Repair surface area affected by the oil leakage from the well. Post the proper identification.

The equipment on the site consists of the following:


1 Mechanical separator 1 Production well

0227464710 2019-02-08 Production Wells No Violations I conducted a compliance notice follow-up for compliance notice 79868289, regarding the removal of the impacted soil at the well location and identification updated and installed at tank battery. At the time of my inspection, the well was equipped with a pumping unit and not in production. The 2 inch line off the tubing and 2 inch flow line valves were closed. There was a domestic line plumbed off the 4.5 inch casing with an open valve. The previously impacted area around and in front of the well, was still oil stained but no active leak was observed at the wellhead. The oil stained soil previously around the north side of the two 100 BBL tanks has been removed. Valves on the separator were open. The diked tank battery still needs updated identification installed. Lease access to the well and tank battery was stable. I contacted Vortex Energy, LLC and left a messsage at the phone number listed on the state database (740-270-4100) for Vortex, regarding the installation of identification and cleanup at the well location.
0692391677 2016-08-26 Production Wells No Violations
0870441862 2014-03-06 Production Wells Violations Noted I was on location to check compliance to Chiefs Order 2014-43. My inspection found the well was equipped with a pumping unit. Two valves leading to the flow line from the well were open. The tank battery consisted of two 100 barrel production tank, a 50 barrel brine tank, and a heat, treated separator. The separator had the correct spacing. There was a stenciled identification sign posted on the production tank. The dike meets containment requirements. The flow line valves leading to and exiting the separator were open. The lease road was in stable condition. Photos were taken of all the production equipment. The well was in production which was in non-compliance of Chiefs order #2014-43. The well needs to be shut-in immediately.
1280386752 2008-08-18 Production Wells No Violations no violations .
1302781606 2017-12-07 Production Wells No Violations I was on location to assess compliance notice #79868289. I found the oil impacted soil at the base of the middle storage tank and in front of the wellhead has not been cleaned up. The stenciled identification sign is still blank. The separator doors are still off the hinges. Photos have been taken and are available upon request.

Big Sky still needs to:

Remove and dispose of all impacted soil and vegetation at the well and tank battery. Repair surface area affected by the oil leakage from the well. Post the proper identification.

1405226355 2017-03-21 Production Wells No Violations I was on location to assess compliance notice #79868289. I found the well not in production on the day of my inspection. The 2 flow line ball valve coming off of the wellhead is closed. The oil impacted soil in front of the pumping unit and at the base of the storage tanks has not been cleaned up. There is a bee hive inside of the separator with one door lying on the ground and the other leaning against the separator. A stenciled identification sign is posted.
1417700099 2014-12-04 Administrative Inspection No Violations I performed an administrative inspection for Compliance Notice #870441862, which has been closed at this time. Operator was granted a stay in reference to Chiefs Order 2014-43.
1505756607 2017-09-18 Production Wells No Violations

--up lines are secure with plugs. The doors on the separator are off their hinges with one lying on the ground and the other is leaning against the separator. The access road is in good repair. Photos have been taken and are available upon request.

Big Sky still needs to:

Remove and dispose of all impacted soil and vegetation at the well and tank battery. Repair surface area affected by the oil leakage from the well. Post the proper identification.

1580137058 2020-1-27 0:00: PW No Violations 0.80
1611175334 2007-06-06 Production Wells No Violations no violations .
1665647198 2014-12-15 Production Wells No Violations I was on location for a status check. During my inspection, I found the well in production. The well was equipped with a pumpjack. The tank battery consisted of two, 100 barrel production tanks, a 50 barrel brine tank and a separator. A dike surrounded the production equipment. The load lines had bull plugs. There was a stenciled identification sign on a production tank. The lease road was in good, stable condition.
1725869349 2018-03-06 Production Wells No Violations DOGRM Steve Ochs and my self performed a follow-up inspection (Chiefs Order 2016-105 ) on the above location the tank battery is equipped with 2-100 barrel tanks an 1-50 barrel and 1-vertical separator. . The well is equipped with a pump jack with an electric motor. All values are shut at the well head no gas sales recorded on the chart. No ID signs posted. Well not in production
1944488199 2016-06-03 Production Wells No Violations
692391677 2016-8-26 0:00: PW No Violations 0.50
79868289 2016-4-29 0:00: PW No Violations 0.50
870441862 2014-3-6 0:00:0 PW No Violations 1.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0079868289 US-OH-129079 2016-05-27 Well operation causing pollution and contamination
0079868289 US-OH-129080 2016-05-27 Failure to legibly identify well
0870441862 US-OH-129906 2015-01-07 Failure to register/obtain or maintain bond/insurance

For data sources see[9]

References