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34-155-21042

Well Details

Well ID: 34-155-21042
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Country: United States
State: Ohio
County: Trumbull
Municipality: Braceville Township
Operator Name: ATWOOD ENERGY INC
Well Pad ID:
Farm/Lease Name: MCGARRY
License Status: Orphan Well - Ready
License Date: 1987-10-28
Spud Date: 1978-10-25
Spud Drilling Contractor: CUBBY DRLG
Final Drill Date: 1978-10-30
Well Total Depth: 4546.00 ft
Configuration: Vertical
Latitude: 41.210000
Longitude: -80.930000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Completion Report Received 1978-02-08 WELL REPORTED TO BE LEAKING BY AREA REALTOR. CHANGE STATUS TO NF PER INSPECTIONS ON FILE 3/31/16 ALE.

Per Richard Skmore Well was located on 12/22/2016 and Inspection report completed. Change Well Status from NF to PR.. Mkb 2/21/2017

CO 1978-10-03 277 ATWOOD ENERGY INC GeoDate 10/3/78
Original Spud 1978-10-25 WELL REPORTED TO BE LEAKING BY AREA REALTOR. CHANGE STATUS TO NF PER INSPECTIONS ON FILE 3/31/16 ALE.

Per Richard Skmore Well was located on 12/22/2016 and Inspection report completed. Change Well Status from NF to PR.. Mkb 2/21/2017

Completed 1978-10-30 WELL REPORTED TO BE LEAKING BY AREA REALTOR. CHANGE STATUS TO NF PER INSPECTIONS ON FILE 3/31/16 ALE.

Per Richard Skmore Well was located on 12/22/2016 and Inspection report completed. Change Well Status from NF to PR.. Mkb 2/21/2017

Reached Total Depth 1978-10-30 WELL REPORTED TO BE LEAKING BY AREA REALTOR. CHANGE STATUS TO NF PER INSPECTIONS ON FILE 3/31/16 ALE.

Per Richard Skmore Well was located on 12/22/2016 and Inspection report completed. Change Well Status from NF to PR.. Mkb 2/21/2017

CO 1987-10-28 277 ATWOOD ENERGY INC GeoDate 10/28/87
Unknown 1987-10-28 Issued Date 10/28/87 Expired Date 10/27/88 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date
Construction Permit Expires 1988-10-27 WELL REPORTED TO BE LEAKING BY AREA REALTOR. CHANGE STATUS TO NF PER INSPECTIONS ON FILE 3/31/16 ALE.

Per Richard Skmore Well was located on 12/22/2016 and Inspection report completed. Change Well Status from NF to PR.. Mkb 2/21/2017

Record Last Modified 2017-02-21 WELL REPORTED TO BE LEAKING BY AREA REALTOR. CHANGE STATUS TO NF PER INSPECTIONS ON FILE 3/31/16 ALE.

Per Richard Skmore Well was located on 12/22/2016 and Inspection report completed. Change Well Status from NF to PR.. Mkb 2/21/2017

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2002-11-25 4376 4440 18
4376 4440 18
4376 4440 18

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 79000 Gal 60000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 ATWOOD ENERGY INC 2097.00 95.00 0
1985 ATWOOD ENERGY INC 1891.00 0.00 0
1986 ATWOOD ENERGY INC 1387.00 87.00 365
1987 ATWOOD ENERGY INC 702.00 77.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 ATWOOD ENERGY INC Brine 0 0
1985 ATWOOD ENERGY INC Brine 60 0
1986 ATWOOD ENERGY INC Brine 140 365
1987 ATWOOD ENERGY INC Brine 70 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0951791127 2017-01-17 Administrative Inspection No Violations I received a call from Terry Alberini (330-717-0113) from Tara Development in response to the letter I mailed concerning the well on their property. Mr. Alberini stated

Tara Development does own the property (Parcel 54-091401) where the tank battery and well are located. Mr. Alberini is unaware if the well is supplying domestic gas. Tara Development may be interested in taking ownership of the well and plans to contact Jim Adams from J Well to inspect the condition of the well and tank battery.

I informed Mr. Alberini that the well is currently leaking gas. Further investigations will be conducted.

1147369567 2016-12-22 Production Wells No Violations
1337605912 2012-05-18 Production Wells No Violations On 5/18/2012, I conducted a production well inspection status check. I was unable to locate the lease road, tank battery, or well head. My review of the well file revealed one previous inspection on 10/24/2000 that stated: no well, tanks, or lease road was found and listed the well as a NOV under statute 1509.14 as a report of abandonment. However, the inspection report was followed by a complaint form dated 11/27/2002 revealing the well was owned by the landower for domestic use.
1484841053 2017-01-19 Production Wells No Violations
1565268209 2019-8-8 0:00:0 OR No Violations
951791127 2017-1-17 0:00: AM No Violations 0.20

For data sources see[9]

References