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34-155-20690

Well Details

Well ID: 34-155-20690
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Country: United States
State: Ohio
County: Trumbull
Municipality: Bristol Township
Operator Name: PETROX, INC
Well Pad ID:
Farm/Lease Name: OWEN ALVA & MARGARET
License Status: Final Restoration
License Date: 1995-10-26
Spud Date: 1977-09-23
Spud Drilling Contractor:
Final Drill Date: 1977-09-29
Well Total Depth: 4366.00 ft
Configuration: Vertical
Latitude: 41.350000
Longitude: -80.860000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1977-09-23
Completed 1977-09-29
Reached Total Depth 1977-09-29
CO 1981-06-30 271 TGX CORP GeoDate 6/30/81
CO 1994-03-29 182 BELDEN & BLAKE CO GeoDate 6/30/81
CO 1995-10-11 1966 PETROX INC GeoDate 6/30/81
CO 1995-10-26 1966 PETROX INC GeoDate 10/26/95
COMBINATION WELL 1995-10-26 Issued Date 10/26/95 Expired Date 10/25/96 Proposed Purpose OG Was Plug Supervised Y Who Superivsed JERRY KOHLPlug and Abandon Date 7/17/96
Plugged/Abandoned 1996-07-17
Construction Permit Expires 1996-10-25
Record Last Modified 2013-03-14

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4077 4131 12
4077 4131 12
4077 4131 12

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1350 Bbl 28500 CASING PRESSURE 1275#

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 TGX CORP 4094.00 0.00 0
1985 TGX CORP 3869.00 0.00 365
1986 TGX CORP 5312.00 21.00 365
1987 TGX CORP 3645.00 0.00 365
1988 TGX CORP 2060.00 41.00 365
1989 TGX CORP 2267.00 0.00 365
1990 TGX CORP 1899.00 0.00 365
1991 TGX CORP 1322.00 0.00 365
1992 TGX CORP 1139.00 0.00 365
1993 TGX CORP 629.00 0.00 181
1994 BELDEN & BLAKE CORPORATION 0.00 0.00 7
2010 GAS ACQUISITION COMPANY LTD 933.00 159.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 TGX CORP Brine 280 0
1985 TGX CORP Brine 154 365
1986 TGX CORP Brine 147 365
1987 TGX CORP Brine 35 365
1988 TGX CORP Brine 0 365
1989 TGX CORP Brine 0 365
1990 TGX CORP Brine 0 365
1991 TGX CORP Brine 35 365
1992 TGX CORP Brine 10 365
1993 TGX CORP Brine 382 181
1994 BELDEN & BLAKE CORPORATION Brine 6 7
2010 GAS ACQUISITION COMPANY LTD Brine 242 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-2116705365 2014-9-10 0:00: PB No Violations
2116705365 2014-09-10 Plug / Plug Back No Violations I was on site to with Inspector Jerry Kohl to respond to a gas leak complaint. The well was plugged and abandoned on 7/17/1964. The land owner waived the removal of the production piping so the pipeline was still lying on top of the ground intact. Final restoration was passed on 11/16/1996. The landowner hit the pipe coming from the supply line to the old tank battery with a brush hog, causing small gas leak at a pipe elbow. Petrox was on site to locate the leak and fix the problem. It was decided that they would dig down below the surface and cut off the pipe and cap it to prevent similar problems in the future.
iDIAN00125 1998-11-16 Final Restoration No Violations
iDIAN001257 1998-11-16 0:00 FR No Violations

For data sources see[9]

References