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Well ID: 34-155-20690 | Loading map...
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Country: United States | |
State: Ohio | |
County: Trumbull | |
Municipality: Bristol Township | |
Operator Name: PETROX, INC | |
Well Pad ID: | |
Farm/Lease Name: OWEN ALVA & MARGARET | |
License Status: Final Restoration | |
License Date: 1995-10-26 | |
Spud Date: 1977-09-23 | |
Spud Drilling Contractor: | |
Final Drill Date: 1977-09-29 | |
Well Total Depth: 4366.00 ft | |
Configuration: Vertical | |
Latitude: 41.350000 | |
Longitude: -80.860000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1977-09-23 | |
Completed | 1977-09-29 | |
Reached Total Depth | 1977-09-29 | |
CO | 1981-06-30 | 271 TGX CORP GeoDate 6/30/81 |
CO | 1994-03-29 | 182 BELDEN & BLAKE CO GeoDate 6/30/81 |
CO | 1995-10-11 | 1966 PETROX INC GeoDate 6/30/81 |
CO | 1995-10-26 | 1966 PETROX INC GeoDate 10/26/95 |
COMBINATION WELL | 1995-10-26 | Issued Date 10/26/95 Expired Date 10/25/96 Proposed Purpose OG Was Plug Supervised Y Who Superivsed JERRY KOHLPlug and Abandon Date 7/17/96 |
Plugged/Abandoned | 1996-07-17 | |
Construction Permit Expires | 1996-10-25 | |
Record Last Modified | 2013-03-14 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4077 | 4131 | 12 |
4077 | 4131 | 12 | |
4077 | 4131 | 12 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1350 Bbl | 28500 | CASING PRESSURE 1275# |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | TGX CORP | 4094.00 | 0.00 | 0 |
1985 | TGX CORP | 3869.00 | 0.00 | 365 |
1986 | TGX CORP | 5312.00 | 21.00 | 365 |
1987 | TGX CORP | 3645.00 | 0.00 | 365 |
1988 | TGX CORP | 2060.00 | 41.00 | 365 |
1989 | TGX CORP | 2267.00 | 0.00 | 365 |
1990 | TGX CORP | 1899.00 | 0.00 | 365 |
1991 | TGX CORP | 1322.00 | 0.00 | 365 |
1992 | TGX CORP | 1139.00 | 0.00 | 365 |
1993 | TGX CORP | 629.00 | 0.00 | 181 |
1994 | BELDEN & BLAKE CORPORATION | 0.00 | 0.00 | 7 |
2010 | GAS ACQUISITION COMPANY LTD | 933.00 | 159.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | TGX CORP | Brine | 280 | 0 |
1985 | TGX CORP | Brine | 154 | 365 |
1986 | TGX CORP | Brine | 147 | 365 |
1987 | TGX CORP | Brine | 35 | 365 |
1988 | TGX CORP | Brine | 0 | 365 |
1989 | TGX CORP | Brine | 0 | 365 |
1990 | TGX CORP | Brine | 0 | 365 |
1991 | TGX CORP | Brine | 35 | 365 |
1992 | TGX CORP | Brine | 10 | 365 |
1993 | TGX CORP | Brine | 382 | 181 |
1994 | BELDEN & BLAKE CORPORATION | Brine | 6 | 7 |
2010 | GAS ACQUISITION COMPANY LTD | Brine | 242 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-2116705365 | 2014-9-10 0:00: | PB | No Violations | |
2116705365 | 2014-09-10 | Plug / Plug Back | No Violations | I was on site to with Inspector Jerry Kohl to respond to a gas leak complaint. The well was plugged and abandoned on 7/17/1964. The land owner waived the removal of the production piping so the pipeline was still lying on top of the ground intact. Final restoration was passed on 11/16/1996. The landowner hit the pipe coming from the supply line to the old tank battery with a brush hog, causing small gas leak at a pipe elbow. Petrox was on site to locate the leak and fix the problem. It was decided that they would dig down below the surface and cut off the pipe and cap it to prevent similar problems in the future. |
iDIAN00125 | 1998-11-16 | Final Restoration | No Violations | |
iDIAN001257 | 1998-11-16 0:00 | FR | No Violations |
For data sources see[9]