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34-153-21199

Well Details

Well ID: 34-153-21199
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Country: United States
State: Ohio
County: Summit
Municipality: Sagamore Hills Township
Operator Name: D & D ENERGY COMPANY
Well Pad ID:
Farm/Lease Name: POLCEN
License Status: Plugged and Abandoned
License Date: 2005-09-09
Spud Date: 1983-06-05
Spud Drilling Contractor: CVAS DRLG
Final Drill Date: 1983-06-11
Well Total Depth: 3536.00 ft
Configuration: Vertical
Latitude: 41.320000
Longitude: -81.570000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1982-08-20 140 KST OIL & GAS CO INC GeoDate 8/20/82
Oil and Gas 1982-08-20 Issued Date 8/20/82 Expired Date 2/15/83 Acres 0020000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000
CO 1983-01-24 140 KST OIL & GAS CO INC GeoDate 1/24/83
Oil and Gas 1983-01-24 Issued Date 1/24/83 Expired Date 7/23/83 Acres 0020000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 03536 Proposed Drill Depth 03536
Original Spud 1983-06-05 R.I. 1-29-83
Completed 1983-06-11 R.I. 1-29-83
Reached Total Depth 1983-06-11 R.I. 1-29-83
Completion Report Received 1983-06-28 R.I. 1-29-83
CO 1995-12-12 182 BELDEN & BLAKE CO GeoDate 1/24/83
Change of Owner 1999-04-19 Operator changed from 182, BELDEN & BLAKE CORPORATION to 6401, OIL & GAS SOLUTIONS, LTD
APP 2001-07-05 Proposed Formations:CLINTON, Issued Date:7/5/2001, Expired Date:7/5/2002 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Change of Owner 2004-01-06 Operator changed from 6401, OIL & GAS SOLUTIONS, LTD to 5569, D & D ENERGY COMPANY
Plugged/Abandoned 2005-08-12 R.I. 1-29-83
APP 2005-09-09 Proposed Formations:CLINTON, Issued Date:9/9/2005, Expired Date:9/9/2006 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
Construction Permit Expires 2006-09-09 R.I. 1-29-83
Record Last Modified 2017-02-15 R.I. 1-29-83

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 3148 3252 0
3148 3252 0
2006-09-11 3184 3234 100
3184 3234 100
3148 3252 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 115000 Gal 0 FRAC;115MG H2O

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 KST OIL & GAS CO INC 19319.00 405.00 365
1985 KST OIL & GAS CO INC 9020.00 130.00 365
1986 KST OIL & GAS CO INC 5468.00 141.00 365
1987 KST OIL & GAS CO INC 3975.00 76.00 365
1988 KST OIL & GAS CO INC 2977.00 125.00 365
1989 KST OIL & GAS CO INC 2711.00 74.00 365
1990 KST OIL & GAS CO INC 1993.00 59.00 365
1991 KST OIL & GAS CO INC 1933.00 0.00 365
1992 KST OIL & GAS CO INC 1310.00 81.00 365
1993 KST OIL & GAS CO INC 985.00 51.00 365
1994 KST OIL & GAS CO INC 62.00 0.00 365
1995 KST OIL & GAS CO INC 57.00 0.00 365
1996 BELDEN & BLAKE CORPORATION 6.00 0.00 366
1997 BELDEN & BLAKE CORPORATION 137.00 0.00 366
1998 BELDEN & BLAKE CORPORATION 57.00 0.00 365
1999 BELDEN & BLAKE CORPORATION 33.00 0.00 14
2000 OIL & GAS SOLUTIONS LTD 0.00 0.00 365
2001 OIL & GAS SOLUTIONS LTD 0.00 0.00 0
2002 OIL & GAS SOLUTIONS LTD 0.00 0.00 0
2003 OIL & GAS SOLUTIONS LTD 0.00 0.00 0
2004 D & D ENERGY COMPANY 0.00 0.00 365
2005 D & D ENERGY COMPANY 0.00 0.00 240

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 KST OIL & GAS CO INC Brine 0 365
1985 KST OIL & GAS CO INC Brine 260 365
1986 KST OIL & GAS CO INC Brine 164 365
1987 KST OIL & GAS CO INC Brine 251 365
1988 KST OIL & GAS CO INC Brine 111 365
1989 KST OIL & GAS CO INC Brine 155 365
1990 KST OIL & GAS CO INC Brine 85 365
1991 KST OIL & GAS CO INC Brine 293 365
1992 KST OIL & GAS CO INC Brine 133 365
1993 KST OIL & GAS CO INC Brine 217 365
1994 KST OIL & GAS CO INC Brine 210 365
1995 KST OIL & GAS CO INC Brine 0 365
1996 BELDEN & BLAKE CORPORATION Brine 0 366
1997 BELDEN & BLAKE CORPORATION Brine 0 366
1998 BELDEN & BLAKE CORPORATION Brine 0 365
1999 OIL & GAS SOLUTIONS LTD Brine 245
2000 OIL & GAS SOLUTIONS LTD Brine 0 365
2001 OIL & GAS SOLUTIONS LTD Brine 0 0
2002 OIL & GAS SOLUTIONS LTD Brine 0 0
2003 OIL & GAS SOLUTIONS LTD Brine 0 0
2004 D & D ENERGY COMPANY Brine 0 365
2005 D & D ENERGY COMPANY Brine 365 240

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1291640485 2003-3-26 0:00: PW No Violations
-1675310609 2003-6-30 0:00: PW No Violations
-799795546 2004-10-22 0:00 PW No Violations
0000PL4773 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0236188736 2005-07-26 Production Wells Violations Noted Cable Well Service is on site to swab test the well. According to Bob Ditty, he intends to swab the well through tubing to try and build pressure. If this is not successful, he will pull tubing and swab 4-1/2.
0459683636 2003-09-12 Production Wells Violations Noted The well is still idle. According to Steve Swain, the well is being sold to D&D Energy. The transfer should occur this month.
0799795546 2004-10-22 Production Wells Violations Noted Still idle.
0832403279 2005-01-26 Production Wells Violations Noted The well is still idle. Bob Ditty stated that he will be working on getting a meter set for this well and the two Arapaho wells this spring and the wells will be put back into production.
1124737022 2005-08-12 Production Wells Violations Noted The well has been plugged and the violation has been corrected.
1274677928 2005-07-14 Production Wells Violations Noted The service rig has moved on site. Bob Ditty intends to swab the well through the tubing to see if the pressure will build enough to place the well into production. If pressure does not build, he said that he will plug and abandon the well.
1291640485 2003-03-26 Production Wells Violations Noted CASE 03-007 The Uniontown office received an idle well complaint from Mr. Ed Calvert at 1367 Nesbitt Road in Sagamore Hills (330-468-6856). The well is operated by Oil & Gas Solutions. The last reported significant production from this well was 1994. The last reported production of any kind was 1999. Steve Swain with Oil & Gas Solutions was notified by phone, that the well needs to be plugged or placed back into production. The tank battery identification is also incorrect.
1439712573 2005-08-02 Production Wells Violations Noted D&D Energy and Cable Well Service were still on site and had started swabbing 4-1/2 casing as part of determining whether to plug or produce the well. A decision should be made by the end of the week.
1675310609 2003-06-30 Production Wells Violations Noted CASE 03-007 recent correspondence from Steve Swain indicated that he will be selling this well by the end of August. If the transfer occurs, the new operator will be given the opportunity to place the well back into production. If the sale does not occur, Mr. Swain will be ordered to plug and abandon the well as soon as possible.
1856405680 2005-03-31 Production Wells Violations Noted No activity to date on this well. It is noted that Bob Ditty is working on the Silver well (P-1278) east of the Polcen. Perhaps he will move west when the Silver is completed. If he does not, a Chiefs order will be requested.
236188736 2005-7-26 0:00: PW No Violations
459683636 2003-9-12 0:00: PW No Violations
832403279 2005-1-26 0:00: PW No Violations
PL4773 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0236188736 US-OH-122352 2003-03-27 Failure to legibly identify well
0236188736 US-OH-122353 2003-03-27 Well shall be plugged
0459683636 US-OH-124974 2003-03-27 Failure to legibly identify well
0459683636 US-OH-124975 2003-03-27 Well shall be plugged
0799795546 US-OH-129092 2003-03-27 Failure to legibly identify well
0799795546 US-OH-129093 2003-03-27 Well shall be plugged
0832403279 US-OH-129486 2003-03-27 Failure to legibly identify well
0832403279 US-OH-129487 2003-03-27 Well shall be plugged
1124737022 US-OH-103147 2003-03-27 Failure to legibly identify well
1124737022 US-OH-103148 2003-03-27 Well shall be plugged
1274677928 US-OH-107629 2003-03-27 Failure to legibly identify well
1274677928 US-OH-107630 2003-03-27 Well shall be plugged
1291640485 US-OH-108224 2003-03-27 Failure to legibly identify well
1291640485 US-OH-108225 2003-03-27 Well shall be plugged
1439712573 US-OH-112802 2003-03-27 Failure to legibly identify well
1439712573 US-OH-112803 2003-03-27 Well shall be plugged
1675310609 US-OH-116568 2003-03-27 Failure to legibly identify well
1675310609 US-OH-116569 2003-03-27 Well shall be plugged
1856405680 US-OH-118583 2003-03-27 Failure to legibly identify well
1856405680 US-OH-118584 2003-03-27 Well shall be plugged

For data sources see[9]

References