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Well ID: 34-153-20417 | Loading map...
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Country: United States | |
State: Ohio | |
County: <County> | |
Municipality: | |
Operator Name: CITY OF CUYAHOGA FALLS | |
Well Pad ID: | |
Farm/Lease Name: CITY OF CUYAHOGA FALLS | |
License Status: Active Injection | |
License Date: 1966-09-17 | |
Spud Date: 1966-11-15 | |
Spud Drilling Contractor: MASON DRILLING | |
Final Drill Date: 1966-12-15 | |
Well Total Depth: 3003.00 ft | |
Configuration: Vertical | |
Latitude: 41.130000 | |
Longitude: -81.450000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1966-11-15 | |
Completed | 1966-12-15 | |
Reached Total Depth | 1966-12-15 | |
Completion Report Received | 1966-12-23 | |
Last Compliance Report | 2015-03-23 | |
Record Last Modified | 2015-06-26 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1999-10-20 | 2775 | 3003 | 0 |
2775 | 3003 | 0 | |
2775 | 3003 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
0 | 0 | 0 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1134131424 | 2010-1-12 0:00: | SM | No Violations | |
-1192659126 | 2009-2-2 0:00:0 | SM | No Violations | |
-1435441880 | 2015-4-23 0:00: | SM | No Violations | |
-1544334726 | 2011-12-28 0:00 | SM | No Violations | |
-1817416591 | 2016-8-11 0:00: | SM | No Violations | |
-2071468511 | 2004-2-6 0:00:0 | SM | No Violations | |
-851761336 | 2010-3-22 0:00: | SM | No Violations | |
0253529591 | 2004-04-08 | Solution Mining Project | No Violations | Run 2-3/8 tubing back into the hole, pressure up and start circulating. |
0621302873 | 2010-03-24 | Solution Mining Project | No Violations | on site for MIT test of well casing 51/2. Ran a Baker #81 Packer on 23/8 tubing set at 2680.ran pressure up to 380PSI shut in waited 10 minutes no leaks. Then bleed off pressure then ran MIT test pressure up to 525PSI shut in started time at 5min press |
0851761336 | 2010-03-22 | Solution Mining Project | No Violations | Moore Well Service is on site to initiate the five year MIT requirement. The 2-3/8 tubing has been removed and the plan is to run a scraper in the morning before attempting to run the packer necessary for the MIT. |
1081340000 | 2004-04-06 | Solution Mining Project | No Violations | Completed the Mechanical Integrity Test on the 5-1/2 casing in this solution mining well. Ran a Halliburton RTTS retrievable packer on 2-3/8 tubing. Set packer at 2663. Pressure up to 150# and found a leak at the tubing head. Tighten and retest to 500#. Had a small leak in the packing of one the old valves. The test had to be done through the old valves because of the connection sizes. This leak probably accounted for the 3% pressure loss (500 psi to 485 psi) after the 15 minute test. All of the valves will be replaced before the system is placed back into operation.
Initial - 500 psi 5 Minute - 500 psi 10 Minute - 495 psi 15 Minute - 485 psi TEST PASSED. |
1134131424 | 2010-01-12 | Solution Mining Project | No Violations | The required 5 year MIT is still on hold at the request of the City. They are waiting for the Moore Well service rig to pull the tubing and set a packer to conduct the test. On this date they were producing some brine which was being discharged into their containment pit. |
1192659126 | 2009-02-02 | Solution Mining Project | No Violations | Status check inspection found no violations at this time. The injection pressure will be checked at a later date. The ID is posted on the perimeter fence and the system was placing brine in the holding pit. The five year MIT is due this year. |
1269266382 | 2010-03-19 | Solution Mining Project | No Violations | The well is scheduled for a 5 year mechanical integrity test. Moore Well Service is bringing a service rig on Monday 3/22 to start the project which will include removing the tubing, running a retrievable packer and completing the MIT. |
1270502005 | 2010-03-23 | Solution Mining Project | No Violations | Met on site with Keith Moore representing Moore Well Service and discussed the planned activity. The MIT is scheduled for 3/24. |
1435441880 | 2015-04-23 | Solution Mining Project | No Violations | I was on the City of Cuyahoga Falls # 1 for the five ( 5) year Mechanical Integrity Test. Moore Well Services ( MWS ) set a Baker Model 81 packer at 2701 ( mid element ) on 2.375 tubing and began the pressure test using a triplex pump. Allowable injection pressure for the well is 400 psi. A test manifold isolated the well from any possible bled off back through the pump and plumbing. A Barton chart recorder and a digital gauge monitored and recorded pressures at timed intervals. The annular space between the 5.5 casing and 2.375 tubing was monitored for any pressure leakage. The initial pressure was 527 psi ( @ 0838 hrs. ) followed by 525 psi ( @ 0843 hrs. ), 520 psi ( @ 0848 hrs. ), 518 psi ( @ 0853 hrs. ) and 513 psi ( @ 0858 hrs. ). Test duration was fifteen minutes, during which a 9 psi decline ( 1.7 % ) occurred. The well passed the five (5) year Mechanical Integrity Test. |
1510836137 | 2017-11-15 | Solution Mining Project | No Violations | |
1544334726 | 2011-12-28 | Solution Mining Project | No Violations | The City of Cuyahoga Falls continues to use this well to generate brine for use in the adjacent water treatment plant and for snow and ice control. During this inspection, brine was being pumped into the holding pond and City trucks were loading for road application. |
1599747542 | 2020-9-3 0:00:0 | SM | No Violations | |
1739716426 | 2004-02-04 | Solution Mining Project | No Violations | Status check inspection prior to conducting MIT. |
1817416591 | 2016-08-11 | Solution Mining Project | No Violations | Moore Well Services (MWS) was on location to change out the 2.375 injection string after the salt density had dropped. MWS removed the tubing badly corroded which was being crushed where the power tongs bite into the tubing. The bottom two (2) joints of tubing had been sheared off, possibly due to cavern collapse. Moore Well Services ran a used string of 2.375 tubing consisting of 89 joints and one (1 ) mud anchor. No violations observed during this inspection. |
2071468511 | 2004-02-06 | Solution Mining Project | No Violations | Status check inspection of solution project prior to meeting with John Christman regarding MIT test. No violations at this time. |
253529591 | 2004-4-8 0:00:0 | SM | No Violations | |
621302873 | 2010-3-24 0:00: | SM | No Violations |
For data sources see[5]