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Well ID: 34-151-25189 | Loading map...
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Country: United States | |
State: Ohio | |
County: Stark | |
Municipality: Marlboro Township | |
Operator Name: RANGE RESOURCES-APPALACHIA LLC | |
Well Pad ID: | |
Farm/Lease Name: HAGAN UNIT | |
License Status: Final Restoration | |
License Date: 2010-03-08 | |
Spud Date: 2000-10-18 | |
Spud Drilling Contractor: UNION DRLG | |
Final Drill Date: 2000-10-28 | |
Well Total Depth: 7638.00 ft | |
Configuration: Vertical | |
Latitude: 40.930000 | |
Longitude: -81.210000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2000-08-23 | 6674 GREAT LAKES ENERGY PTNSHP LLC Proposed Formation CLINTON-COPPER RIDGE Issued Date 8/23/00 Expired Date 8/23/01 6:00:00 AM |
Original Spud | 2000-10-18 | RBDMS Rec |
Completed | 2000-10-28 | RBDMS Rec |
Reached Total Depth | 2000-10-28 | RBDMS Rec |
Completion Report Received | 2001-02-05 | RBDMS Rec |
APP | 2001-11-05 | Proposed Formations:ROSE RUN, Issued Date:11/5/2001, Expired Date:11/5/2002 6:00:00 AM, Drilling unit acres:285.95, Proposed Well Type:OG, Proposed Well Class: |
APP | 2010-03-08 | Proposed Formations:TREMPEALEAU, Issued Date:3/8/2010, Expired Date:3/8/2011 6:00:00 AM, Drilling unit acres:285.93, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2010-03-18 | RBDMS Rec |
Construction Permit Expires | 2011-03-08 | RBDMS Rec |
Record Last Modified | 2017-02-15 | RBDMS Rec |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2001-04-24 | 7434 | 7474 | 0 |
7434 | 7474 | 0 | |
7434 | 7474 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 64674 Gal | 33000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2000 | RANGE RESOURCES-APPALACHIA LLC | 139.00 | 0.00 | 31 |
2001 | RANGE RESOURCES-APPALACHIA LLC | 5250.00 | 0.00 | 334 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2000 | RANGE RESOURCES-APPALACHIA LLC | Brine | 80 | 31 |
2001 | RANGE RESOURCES-APPALACHIA LLC | Brine | 4070 | 334 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0533162192 | 2010-04-28 | Final Restoration | No Violations | All production equipment has been removed. The former well site and tank battery site are rough graded. The access road is still in place. I did not pass the Final Restoration at this time. |
1174855972 | 2013-06-06 | Final Restoration | No Violations | Site in middle of a field with crops growing on it. No signs of anything left on site. |
1225733682 | 2008-10-31 | Production Wells | Violations Noted | The Uniontown office received an anonymous phone call on 10-16-2008 regarding a blocked access road and a possible idle well. I inspected the site on 10-31-2008 and found the access road blocked by a downed tree. The tank battery and wellhead were overgrown with weeds. The well appears to be idle. The State database shows that the last reported production for this well was in 2001. Remove the downed tree in the access road, cut down the high weeds, and PLUG or PRODUCE the well. |
1268682068 | 2010-03-15 | Plug / Plug Back | No Violations | Whipstocks service rig is on the location and the plugging pit has been dug. I met with Mark Moody on the location to discuss the recommended plugs. |
1268939788 | 2010-03-16 | Plug / Plug Back | No Violations | Pulled tubing. Appalachian Well Services shot the 4-1/2 casing at 4988. The service rig was unable to pull the casing. |
1268961125 | 2010-03-18 | Plug / Plug Back | No Violations | This well was plugged and abandoned on 3-18-2010. The idle well violation has been RESOLVED. |
1282872545 | 2010-08-26 | Final Restoration | No Violations | This well was plugged and abandoned on 3-18-2010. The former well site and tank battery are growing in soybeans. The access road is still in place. I will need a landowner waiver for the access road and the flow line before I can pass the Final Restoration. |
533162192 | 2010-4-28 0:00: | FR | No Violations | |
iDIAN00610 | 2001-05-14 | Preliminary Restoration | No Violations | |
iDIAN006100 | 2001-5-14 0:00: | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1225733682 | US-OH-106077 | 2008-11-03 | Well shall be plugged |
For data sources see[9]