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34-151-22692

Well Details

Well ID: 34-151-22692
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Country: United States
State: Ohio
County: Stark
Municipality: Washington Township
Operator Name: CARPENTER GREGGORY C SR
Well Pad ID:
Farm/Lease Name: UNRUH-HOFFMAN
License Status: Domestic Well
License Date: 1977-09-08
Spud Date: 1977-11-18
Spud Drilling Contractor:
Final Drill Date: 1977-12-04
Well Total Depth: 5400.00 ft
Configuration: Vertical
Latitude: 40.820000
Longitude: -81.110000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1977-09-08 133 QUAKER STATE OIL REF CORP GeoDate 9/8/77
Unknown 1977-09-08 Issued Date 9/8/77 Expired Date 9/8/78 Acres 0000000 Tool Type Proposed Formation Proposed Depth 00000 Proposed Drill Depth 00000
Original Spud 1977-11-18 RI 9-14-77
Completed 1977-12-04 RI 9-14-77
Reached Total Depth 1977-12-04 RI 9-14-77
Construction Permit Expires 1978-09-08 RI 9-14-77
CO 1995-10-18 182 BELDEN & BLAKE CO GeoDate 9/8/77
Change of Owner 2001-04-05 Operator changed from 457, ALSID OIL & GAS to 6970, VANGUARD OIL & GAS LLC
Change of Owner 2011-10-18 Operator changed from 6970, VANGUARD OIL & GAS LLC to 8867, CARPENTER GREGGORY C SR
Record Last Modified 2013-05-10 RI 9-14-77

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 5255 5311 2
5255 5311 2
5255 5311 2

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 3619 Bbl 65000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 QUAKER STATE OIL REF CORP 4238.00 424.00 0
1985 QUAKER STATE OIL REF CORP 3479.00 307.00 365
1986 QUAKER STATE OIL REF CORP 3559.00 381.00 365
1987 QUAKER STATE OIL REF CORP 2814.00 367.00 365
1988 QUAKER STATE OIL REF CORP 3974.00 301.00 365
1989 QUAKER STATE OIL REF CORP 2613.00 330.00 365
1990 QUAKER STATE OIL REF CORP 2066.00 133.00 365
1991 QUAKER STATE OIL REF CORP 2858.00 225.00 365
1992 QUAKER STATE OIL REF CORP 2343.00 188.00 365
1993 QUAKER STATE OIL REF CORP 892.00 82.00 365
1997 ALSID OIL & GAS 0.00 0.00 0
2002 VANGUARD OIL & GAS LLC 0.00 0.00 0
2003 VANGUARD OIL & GAS LLC 0.00 0.00 0
2005 VANGUARD OIL & GAS LLC 0.00 0.00 0
2006 VANGUARD OIL & GAS LLC 0.00 0.00 0
2007 VANGUARD OIL & GAS LLC 0.00 0.00 0
2009 VANGUARD OIL & GAS LLC 9889.00 105.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 QUAKER STATE OIL REF CORP Brine 0 0
1985 QUAKER STATE OIL REF CORP Brine 0 365
1986 QUAKER STATE OIL REF CORP Brine 160 365
1987 QUAKER STATE OIL REF CORP Brine 185 365
1988 QUAKER STATE OIL REF CORP Brine 140 365
1989 QUAKER STATE OIL REF CORP Brine 160 365
1990 QUAKER STATE OIL REF CORP Brine 170 365
1991 QUAKER STATE OIL REF CORP Brine 80 365
1992 QUAKER STATE OIL REF CORP Brine 45 365
1993 QUAKER STATE OIL REF CORP Brine 0 365
1997 ALSID OIL & GAS Brine 0 0
2002 VANGUARD OIL & GAS LLC Brine 0 0
2003 VANGUARD OIL & GAS LLC Brine 0 0
2005 VANGUARD OIL & GAS LLC Brine 0 0
2006 VANGUARD OIL & GAS LLC Brine 0 0
2007 VANGUARD OIL & GAS LLC Brine 0 0
2009 VANGUARD OIL & GAS LLC Brine 115 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1543049798 2011-7-11 0:00: PW No Violations
-2011161339 2014-12-30 0:00 AM No Violations
-845923159 2014-6-18 0:00: PW No Violations 3.00
-867073976 2014-4-3 0:00:0 PW No Violations
0189529873 2014-07-07 Production Wells No Violations I was on location to follow up to NOV #1311354705 and complaint #3217. I checked the remedial work that Moore Well Services has performed on this well. On 6/11 Moore Well Services dug of the 8 5/8 surface casing and saw that both ports were open. They installed a bull plug into one of the holes and a 2 riser with a 2 ball valve above ground. They found very little pressure on the 8 5/8 casing and do not think there are any issues with the 4.5 casing. I contacted the operator and Moore Well Services have them put a pressure relief valve on the 8 5/8 2 riser so that the annulus does not continually vent or build excessive pressure. At this time the leaking casing has been fixed and the compliance notice can be closed. The complaint on this well also can be closed at this time.
0260553249 2011-07-11 Production Wells No Violations FOLLOW UP TO NOV # 1311354705 See Complaint #11-007. The Uniontown office received a phone call on 7-8-11 from Jan Williams (330-248-3080) regarding an idle well located on her property at 3510 Anderson Ave., Minerva, OH 44657. She also e-mailed me photographs of the wellhead and the tank battery. I inspected the site on 7-11-2011 and found the well to be idle. The pumping unit is overgrown with vegetation. There are no rods and no tubing in the well. The 4-1/2 is swedged down to 2 and then down to what appears to be a house gas hook-up that goes nowhere and is shut in. Gas is bubbling up around the submerged 4-1/2. There is no I.D. sign posted. PLUG or PRODUCE this well. I called Russell Miller (330-506-8152) and discussed the status of this well.
0792591323 2014-03-07 Production Wells No Violations I was on location to follow up NOV #1311354705 and complaint #3217. My inspection found the well to be idle. The pumping unit is overgrown with vegetation. There are no rods and no tubing in the well. The 4-1/2 is swedged down to 2 and then down to what appears to be a house gas hook-up that goes nowhere and is shut in. Gas is bubbling up around the submerged 4-1/2. There is no I.D. sign posted. The tank battery is overgrown and is not piped into the well at this time. A former NOV was issued on 7/22/2011. On 10/3/2011 this well was transferred from Vanguard Oil & Gas LTD to Carpenter Greggory C Sr as a Exempt Domestic Well. The outstanding NOV has not been closed out and the failed wellhead leaking and bubbling gas also has not been addressed at this time.
0845923159 2014-06-18 Production Wells No Violations I was on location to follow up to NOV #1311354705 and complaint #3217. I checked the remedial work that Moore Well Services has performed on this well. On 6/11 Moore Well Services dug of the 8 5/8 surface casing and saw that both ports were open. They installed a bull plug into one of the holes and a 2 riser with a 2 ball valve above ground. They found very little pressure on the 8 5/8 casing and do not think there are any issues with the 4.5 casing. I contacted the operator and Moore Well Services to have them put a pressure releif valve on the 8 5/8 2 riser so that the annullus does not continually vent or build excessive pressure. When this work is done the compliance notice and complaint for this well can be closed.
0867073976 2014-04-03 Production Wells No Violations I was on location with Supervisor Tom Hill, Rick Anderson and Inspector Jim Bucksar to follow up to NOV #1311354705 and complaint #3217. The pumping unit is overgrown with vegetation. There are no rods and no tubing in the well. The 4-1/2 is swedged down to 2 and then down to what appears to be a house gas hook-up that goes nowhere and is shut in. Gas is bubbling up around the submerged 4-1/2. There is no I.D. sign posted. The tank battery is overgrown and is not piped into the well at this time. A former NOV was issued on 7/22/2011. On 10/3/2011 this well was transferred from Vanguard Oil & Gas LTD to Carpenter Greggory C Sr as a Exempt Domestic Well. The outstanding NOV has not been closed out and the failed wellhead leaking and bubbling gas also has not been addressed at this time. I have given the operator a list of contractors to contact to have the leak fixed and the well put back into compliance.
1311354705 2011-07-11 Production Wells Violations Noted See Complaint #11-007. The Uniontown office received a phone call on 7-8-11 from Jan Williams (330-248-3080) regarding an idle well located on her property at 3510 Anderson Ave., Minerva, OH 44657. She also e-mailed me photographs of the wellhead and the tank battery. I inspected the site on 7-11-2011 and found the well to be idle. The pumping unit is overgrown with vegetation. There are no rods and no tubing in the well. The 4-1/2 is swedged down to 2 and then down to what appears to be a house gas hook-up that goes nowhere and is shut in. Gas is bubbling up around the submerged 4-1/2. There is no I.D. sign posted. PLUG or PRODUCE this well. I called Russell Miller (330-506-8152) and discussed the status of this well.
1543049798 2011-07-11 Production Wells No Violations FOLLOW UP TO NOV # 1311354705 See Complaint #11-007. The Uniontown office received a phone call on 7-8-11 from Jan Williams (330-248-3080) regarding an idle well located on her property at 3510 Anderson Ave., Minerva, OH 44657. She also e-mailed me photographs of the wellhead and the tank battery. I inspected the site on 7-11-2011 and found the well to be idle. The pumping unit is overgrown with vegetation. There are no rods and no tubing in the well. The 4-1/2 is swedged down to 2 and then down to what appears to be a house gas hook-up that goes nowhere and is shut in. Gas is bubbling up around the submerged 4-1/2. There is no I.D. sign posted. PLUG or PRODUCE this well. I called Russell Miller (330-506-8152) and discussed the status of this well.
189529873 2014-7-7 0:00:0 PW No Violations 2.50
1971719937 2011-07-11 Production Wells No Violations FOLLOW UP TO NOV # 260553249 FOLLOW UP TO NOV # 1311354705 See Complaint #11-007. The Uniontown office received a phone call on 7-8-11 from Jan Williams (330-248-3080) regarding an idle well located on her property at 3510 Anderson Ave., Minerva, OH 44657. She also e-mailed me photographs of the wellhead and the tank battery. I inspected the site on 7-11-2011 and found the well to be idle. The pumping unit is overgrown with vegetation. There are no rods and no tubing in the well. The 4-1/2 is swedged down to 2 and then down to what appears to be a house gas hook-up that goes nowhere and is shut in. Gas is bubbling up around the submerged 4-1/2. There is no I.D. sign posted. PLUG or PRODUCE this well. I called Russell Miller (330-506-8152) and discussed the status of this well.
2011161339 2014-12-30 Administrative Inspection Violations Noted Faliure to pay $60 fee for 2014.

1509.50 Oil and gas regulatory cost recovery assessment. (2) The oil and gas regulatory cost recovery assessment for a well that becomes an exempt domestic well on and after June 30, 2010, shall be sixty dollars to be paid to the division of oil and gas resources management on the first day of July of each year. TOTAL AMOUNT OWED $60.00.

260553249 2011-7-11 0:00: PW No Violations
792591323 2014-3-7 0:00:0 PW No Violations 2.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1311354705 US-OH-108637 2011-07-22 General Safety
1311354705 US-OH-108638 2011-07-22 Well insufficiently equipped to prevent escape of oil and gas
1311354705 US-OH-108639 2011-07-22 Failure to legibly identify well
1311354705 US-OH-108640 2011-07-22 Nonproduction; well shall be plugged or placed in temporary inactive status
2011161339 US-OH-120415 2015-01-16 $60 cost recovery fee not paid for 2014

For data sources see[9]

References