X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-151-22459

Well Details

Well ID: 34-151-22459
Loading map...
Country: United States
State: Ohio
County: Stark
Municipality: Osnaburg Township
Operator Name: BRINEAWAY INC
Well Pad ID:
Farm/Lease Name: WALKER J& E
License Status: Active Injection
License Date: 1999-12-09
Spud Date: 1974-01-02
Spud Drilling Contractor: SERVICE RIG
Final Drill Date: 1974-01-10
Well Total Depth: 5290.00 ft
Configuration: Vertical
Latitude: 40.790000
Longitude: -81.230000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1974-01-02 ONLY INJECTING INTO THE CLINTON/ MEDINA. PB-12/11/99, CONV ERT 9-3-94,
Reached Total Depth 1974-01-10 ONLY INJECTING INTO THE CLINTON/ MEDINA. PB-12/11/99, CONV ERT 9-3-94,
CO 1994-08-31 2328 BRINEAWAY INC GeoDate 8/31/94
Conversion to Injector 1994-08-31
Salt Water Injection Well 1994-08-31 Issued Date 8/31/94 Expired Date 8/31/95 Acres 0071910 Tool Type NT Proposed Formation NEWBURG/CLINTON Proposed Depth 05290 Proposed Drill Depth 05290
Storage Well 1994-08-31 Issued Date 8/31/94 Expired Date 8/31/95 Acres 0071910 Tool Type NT Proposed Formation NEWBURG/CLINTON Proposed Depth 05290 Proposed Drill Depth 05290
CO 1994-11-14 139 MB OPERATING CO INC GeoDate 7/27/73
Completed 1994-11-15 ONLY INJECTING INTO THE CLINTON/ MEDINA. PB-12/11/99, CONV ERT 9-3-94,
First Injection 1994-11-24 ONLY INJECTING INTO THE CLINTON/ MEDINA. PB-12/11/99, CONV ERT 9-3-94,
Completion Report Received 1995-09-01 ONLY INJECTING INTO THE CLINTON/ MEDINA. PB-12/11/99, CONV ERT 9-3-94,
APP 1999-12-09 Proposed Formations:NEWBURG, Issued Date:12/9/99, Expired Date:12/8/00 6:00:00 AM, Drilling unit acres:71.91, Proposed Well Type:SWD, Proposed Well Class:SWIW
Plugged Back 1999-12-11 ONLY INJECTING INTO THE CLINTON/ MEDINA. PB-12/11/99, CONV ERT 9-3-94,
Annulus Pressure Monitoring Approved 2000-02-01 ONLY INJECTING INTO THE CLINTON/ MEDINA. PB-12/11/99, CONV ERT 9-3-94,
Construction Permit Expires 2000-12-08 ONLY INJECTING INTO THE CLINTON/ MEDINA. PB-12/11/99, CONV ERT 9-3-94,
Last Compliance Report 2015-05-20 ONLY INJECTING INTO THE CLINTON/ MEDINA. PB-12/11/99, CONV ERT 9-3-94,
Record Last Modified 2017-02-15 ONLY INJECTING INTO THE CLINTON/ MEDINA. PB-12/11/99, CONV ERT 9-3-94,

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2000-05-08 5107 5115 1
2000-05-08 5106 5166 0
5106 5166 0
4740 4910 0
5149 5153 3
5107 5115 1
5119 5131 1
5161 5165 2
4740 4910 0
2000-05-08 4740 4910 0
2000-05-08 5161 5165 2
2000-05-08 5149 5153 3
2000-05-08 5119 5131 1

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 0 100 SHOTS
H2O 0 148000 Gal 0 ALSO 53,000 LBS OF 20/40 SAND USED.

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 QUAKER STATE OIL REF CORP 0.00 495.00 0
1985 QUAKER STATE OIL REF CORP 0.00 488.00 365
1986 QUAKER STATE OIL REF CORP 0.00 312.00 365
1987 QUAKER STATE OIL REF CORP 0.00 346.00 365
1988 QUAKER STATE OIL REF CORP 0.00 202.00 365
1989 QUAKER STATE OIL REF CORP 0.00 127.00 365
1990 PETROCON INC 0.00 315.00 365
1991 PETROCON INC 0.00 321.00 365
1992 PETROCON INC 0.00 284.00 365
1993 PETROCON INC 0.00 228.00 365
1994 PETROCON INC 0.00 117.00 212
1995 PETROCON INC 0.00 0.00 0
1996 PETROCON INC 0.00 48.00 240
1997 PETROCON INC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 QUAKER STATE OIL REF CORP Brine 0 0
1985 QUAKER STATE OIL REF CORP Brine 405 365
1986 QUAKER STATE OIL REF CORP Brine 140 365
1987 QUAKER STATE OIL REF CORP Brine 183 365
1988 QUAKER STATE OIL REF CORP Brine 160 365
1989 QUAKER STATE OIL REF CORP Brine 58 365
1990 PETROCON INC Brine 310 365
1991 PETROCON INC Brine 202 365
1992 PETROCON INC Brine 191 365
1993 PETROCON INC Brine 75 365
1994 PETROCON INC Brine 29 212
1995 PETROCON INC Brine 0 0
1996 PETROCON INC Brine 3 240
1997 PETROCON INC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1075187773 2016-7-20 0:00: SW No Violations
-1161519752 2020-4-16 0:00: SW No Violations 0.50
-1298921626 2004-9-21 0:00: SW No Violations
-1424291865 2013-9-27 0:00: SW No Violations
-1480850139 2004-6-22 0:00: SW No Violations
-1547241550 2008-6-12 0:00: SW No Violations
-1561367699 2005-6-28 0:00: SW No Violations
-1563059674 2019-5-15 0:00: SW No Violations 1.50
-1598410388 2009-5-28 0:00: SW No Violations
-1699967759 2009-9-2 0:00:0 SW No Violations
-1716866321 2010-9-7 0:00:0 SW No Violations
-1747174095 2008-9-25 0:00: SW No Violations
-1757562614 2016-3-8 0:00:0 SW No Violations
-2051359983 2012-7-25 0:00: SW No Violations
-2052225348 2014-9-25 0:00: SW No Violations
-2068766466 2008-12-17 0:00 SW No Violations
-222902864 2015-4-6 0:00:0 SW No Violations
-246336154 2019-8-7 0:00:0 SW No Violations 0.80
-447185550 2007-3-13 0:00: SW No Violations
-477930995 2006-3-2 0:00:0 SW No Violations
-512509416 2007-9-26 0:00: SW No Violations
-514428483 2016-3-14 0:00: SW No Violations
-517988749 2017-12-20 0:00 SW No Violations 0.80
-532564670 2002-10-16 0:00 SW No Violations 1.00
-705022291 2006-8-30 0:00: SW No Violations
-745198208 2014-12-29 0:00 SW No Violations
-751434714 2016-6-22 0:00: SW No Violations
-756168453 2018-12-13 0:00 SW No Violations 0.50
-979894411 2014-3-19 0:00: SW No Violations
000UIC1659 1997-05-05 Salt Water Injection Well No Violations 1501: 9-3-07 (D) EXCEED MAX.INJ. PSI
000UIC1660 1997-05-05 Salt Water Injection Well No Violations 1509.03 RULES & REGULATIONS
000UIC1749 1999-01-29 Salt Water Injection Well No Violations 1509.22 CONSTRUCTION
001288i268 2002-01-23 Salt Water Injection Well No Violations Injection  : 800  ; Annulus  : 0  ; Last inspection on 12 / 17 01 . No violations at this time .
001288i328 2002-03-05 Salt Water Injection Well No Violations Injection  : 410  ; Annulus : 0  ; Last inspection  : 01 / 23 / 02 . No violations at this time .
0041781728 2004-09-24 Salt Water Injection Well No Violations NO VIOLATIONS. The system was not running at the time of the inspection.
0071225919 2018-08-29 Salt Water Injection Well No Violations I found the injection well not in production on the day of my inspection. Identification signs are posted. The access road gate to the facility was closed.
0076306352 2003-05-22 Salt Water Injection Well No Violations Facility is under repair. Well is not operating.
0124990549 2017-03-27 Salt Water Injection Well Violations Noted The well was found operating over the maximum allowable injection pressure. Paul Shaw was notified. He was instructed to shut down the pump and adjust the pressure shut-off switch accordingly.
0222902864 2015-04-06 Salt Water Injection Well No Violations A redressed Halliburton R-4 packer was set in compression at 5014 feet. A mechanical integrity test (MIT) was performed on the well. A pressure of 1200 psi. was placed on the tubing-casing annulus. The MIT passed without a loss, during the fifteen minute test period.
0297755979 2007-12-19 Salt Water Injection Well No Violations The injection pump was not running at the time of the inspection. There were no violations at the wellhead or at the multiple brine tank facility.
0367881384 2005-02-04 Salt Water Injection Well No Violations The system was running at the time of the inspection. NO VIOLATIONS.
0415431848 2007-06-27 Salt Water Injection Well No Violations The system was not running at the time of the inspection. The injection pump is under repair. There were no violations at the wellhead or at the brine tank. The lease road has been heavily eroded and needs to be graded.
0447185550 2007-03-13 Salt Water Injection Well No Violations The facility is idle. There is no injection pump.
0477930995 2006-03-02 Salt Water Injection Well No Violations The injection pump was running at the time of the inspection. No Violations at WH or at TB.
0509665470 2017-05-09 Salt Water Injection Well No Violations The injection well and surface facility were inspected. The pump was operating at the time. The tanks and lines had no visible leaks.

No violations were found.

0512509416 2007-09-26 Salt Water Injection Well No Violations The injection pump was not running at the time of the inspection. There were no violations at the wellhead or at the brine tanks.
0514428483 2016-03-14 Salt Water Injection Well No Violations The injection well and surface facility were inspected. The pump was not operating at the time. Pressure differential between the tubing and annulus was increasing, indicating mechanical integrity. There were no violations found at the time.
0517988749 2017-12-20 Salt Water Injection Well No Violations I found the injection and facility in good repair on the day of my inspection. I observed no leaks or spills. An identification sign is posted at the facility and well. The steel structure covering the storage tank and well is in good condition. There are no violations at this time.
0532564670 2002-10-16 Salt Water Injection Well No Violations Routine inspection revealed no violations at this time . The injection pump is apart for repairs at this time . They are also in the process of removing the storage tank from inside the dike at the wellhead . They are going to replace the liner inside the dike . Didnt check the injection pressure since the pump was apart and the wellhead partially disassembled .
0611832726 2015-03-31 Salt Water Injection Well No Violations The well operation was suspended by the company, in response to suspected mechanical integrity failure. The Division was notified on March 23, 2015. The well owner is current waiting for a service rig to become available.
0624105809 2010-12-17 Salt Water Injection Well No Violations The injection system was not running at the time of the inspection. There were no violations at the wellhead or at the brine tank battery. The electric motor was running, but the injection pump was not. The injection pump belt was being eroded by the spinning electric motor. I called Paul Shaw and shut off the power supply to the electric motor.
0652468891 2018-03-26 Salt Water Injection Well No Violations I was on location to witness Brineaway acid treat the injection well. Greg New of Brineaway, Petroset, and a D P Operating brine truck (UIC #25-282) was on location. Petroset pumped 555 gallons of acid at 15% HCL, 5 gallons of 50% Citric Acid solution, and 250 gallons of fresh water spacer followed by displacing the fluids with 20 bbl. of fresh water. I observed no issues during the treatment process.
0705022291 2006-08-30 Salt Water Injection Well No Violations The system was running at the time of the inspection. There were no violations at the wellhead or at the tank battery.
0745198208 2014-12-29 Salt Water Injection Well No Violations The injection well and surface facility were inspected. The well was found shut-in. There were no violations at the time of inspection.
0751434714 2016-06-22 Salt Water Injection Well No Violations The injection well and surface facility were inspected. Pressure readings were taken, while the pump was operating. There were no violations found at the time.
0756168453 2018-12-13 Salt Water Injection Well No Violations I found the injection well not in operation on the day of my inspection. Identification signs are posted. I observed no leaks or spills in or around the facility and injection well.
0765486711 2008-03-20 Salt Water Injection Well No Violations The injection pump was running at the time of the inspection. There were no violations at the wellhead or at the multiple brine tank facility.
0796436419 2013-06-25 Salt Water Injection Well No Violations My inspection of the well and surface facility found no violations.
0879113065 2013-12-27 Salt Water Injection Well No Violations There were no violations found at the time of inspection.
0881867059 2018-07-19 Salt Water Injection Well No Violations I found the injection well not operating on the day of my inspection. Identification sign is posted. I observed no leaks or spills. There was a facility operator on location. The pump house is in good working order.
0892500069 2015-05-29 Salt Water Injection Well No Violations The well and surface facility were inspected. There were no violations found at the time of inspection.
0922563185 2018-03-07 Salt Water Injection Well No Violations I was on location to inspect the injection well and facility. I found the well not operating on the day of my inspection. There proper identification sign is posted. There are no violations at this time.
0952903738 2005-11-14 Salt Water Injection Well No Violations The system was running at the time of the inspection. Stock tank and WH have been painted. Informed Craig (Dorfman) that a new I.D. sign must be posted.
0979894411 2014-03-19 Salt Water Injection Well No Violations No violations were found at the time of inspection.
1069502476 2009-12-04 Salt Water Injection Well No Violations The injection system was running at the time of the inspection. There were no violations at the wellhead or at the brine tank battery.
1075187773 2016-07-20 Salt Water Injection Well No Violations The injection well and surface facility were inspected. There were no violations found at the time.
1078163436 2004-03-01 Salt Water Injection Well No Violations A new plastic pit liner has been installed in the earthen pit. The system was not connected. NO VIOLATIONS.
1085057974 2004-05-19 Salt Water Injection Well No Violations Ran a newly rebuilt R-4 packer with a 9.55 tail pipe on 169 jts of used 2-3/8 upset tbg (tbg was steam cleaned and pressure tested on site). Used the same string of tbg that was in the well (see tbg tally dated 2-1-2000). Universal Well Services mixed and pumped 15 gallons of AnnHib with fresh water to load the annulus. The R-4 packer was set in compression (9,000 lbs) at a depth of 5085.50 . Universal pressured up on the annulus for the MIT.

Tried 3 MITs at 1250 psi. All failed. Tests were witnessed by Paul Shaw and Greg New of Dorfman.

Dorfman will test the 4-1/2 csg for leaks at a later date.

Old perforating info: 3-1/2 strip jet shots; .52 entry; 90 shots from 5110-5160.

1085640085 2014-06-24 Salt Water Injection Well No Violations A valve was stuck shut on the tubing, which will need replaced. No violations were found.
1088558445 2004-06-29 Salt Water Injection Well No Violations Conducted an MIT. Universal Well Services mixed and pumped 20 gallons of AnnHib with fresh water to load the annulus. The R-4 packer was set in compression (10,000 lbs) at a depth of 5041 (see tbg tally dated 2-1-2000 and subtract 1 joint). Universal pressured up to 1400 psi on the annulus. Pressure held at 1400 psi for 18 minutes. MIT PASSED. Test was witnessed by Paul Shaw of Dorfman. I called Tom Tomastik and informed him of the results. Dorfman will acidize the well with 1000 gallons of HCL.
1100176770 2010-03-30 Salt Water Injection Well No Violations The injection system was not running at the time of the inspection. There were no violations at the wellhead or at the brine tank battery.
1114313993 2011-05-20 Salt Water Injection Well No Violations The injection system was running at the time of the inspection. The injection line was over pressured at 1200 PSI. I notified Dave Eberling (330-257-6106) of Dorfman. He immediately shut the system down. The top joint of the injection tubing is spalling off and needs to be replaced. I also informed Greg New. There were no violations at the brine tank battery.
1162025241 2009-04-02 Salt Water Injection Well No Violations The injection system was not running at the time of the inspection. There were no violations at the wellhead or at the brine tank battery.
1234325897 2002-10-16 Salt Water Injection Well No Violations Routine inspection revealed no violations at this time . The injection pump is apart for repairs at this time . They are also in the process of removing the storage tank from inside the dike at the wellhead . They are going to replace the liner inside the dike . Didnt check the injection pressure since the pump was apart and the wellhead partially disassembled .
124990549 2017-3-27 0:00: SW No Violations
1283615768 2017-11-02 Salt Water Injection Well No Violations I found a storage tank and pump with a pre-fab building in good repair on the day of my inspection. The injection will is in front of the building. The well was operating on this day. An identification sign is posted on a wooden board located inside of the facility. I observed no spills or leaks. I called Brineaway and instructed the identification sign to be posted outside in a conspicuous location with a follow-up inspection by 11/9/2017
1288i268 2002-1-23 0:00: SW No Violations 1.00
1288i328 2002-3-5 0:00:0 SW No Violations 1.00
1298921626 2004-09-21 Salt Water Injection Well No Violations NO VIOLATIONS. The system was not running at the time of the inspection. I was unable to check injection pressure. Talked to Greg New. Dorfman will plumb in a new valve.
1319363014 2010-06-14 Salt Water Injection Well No Violations The injection system was running at the time of the inspection. There were no violations at the wellhead or at the brine tank battery. I called Paul Shaw and told him to clean up the oil stained gravel within the lined tank battery dike at the wellhead. It was evident that the transfer stock tank had been recently overfilled.
1321976325 2011-11-16 Salt Water Injection Well No Violations Paul Shaw called me this morning for a Mechanical Integrity Test (MIT). When I arrived at the site, the rebuilt R-4 packer had been set at 5016.50 with 9,000 pounds compression. 60 barrels of annular inhibitor was circulated in the annulus. The annulus was pressured up to 1320 PSI. The test was started at 1320 PSI and ended at 1320 PSI after 25 minutes. The MIT PASSED.
1424291865 2013-09-27 Salt Water Injection Well No Violations My inspection of the well and injection facility found no violations.
1444068890 2015-04-01 Salt Water Injection Well No Violations A service rig released the packer and was pulling the tubing. Conditions onsite were acceptable.
1480850139 2004-06-22 Salt Water Injection Well No Violations Well is not in use and is scheduled for repairs.
1497546991 2017-08-24 Salt Water Injection Well No Violations I performed a UIC inspection on the above location. ID signs were posted. No noted violations were noted at this time. The unload pad for this injection well is the same as the Foltz Brianeway 1351 and the Kolm 1295
1529680222 2018-06-22 Salt Water Injection Well No Violations I found the injection well not in operation. An identification sign is posted at the well and tank battery. I observed no leaks or spills. There are no violations at this time.
1539691489 2018-10-15 Salt Water Injection Well No Violations I was on location to witness a mechanical integrity test. Bishop Well Services was the contracted rig on location. Bishop set a new Haliburton R-

0 minutes: 1,200 psi 5 minutes: 1,200 psi 15 minutes: 1,200 psi

Pressure on the annulus held static for the entire 15 minutes. MIT passed.

1547241550 2008-06-12 Salt Water Injection Well No Violations The injection system was running at the time of the inspection. There were no violations at the wellhead or at the brine tank battery.
1559827156 2016-03-09 Salt Water Injection Well No Violations The injection well and surface facility were inspected. There were no violations found at the time.
1561367699 2005-06-28 Salt Water Injection Well No Violations NO VIOLATIONS. The disposal facility was running at the time of the inspection.
1561563499 2019-6-26 0:00: SW No Violations 1.00
1579014973 2020-1-14 0:00: SW No Violations 1.10
1598410388 2009-05-28 Salt Water Injection Well No Violations The injection system was running at the time of the inspection. There were no violations at the wellhead or at the brine tank battery.
1620889278 2011-10-25 Salt Water Injection Well No Violations The injection system was not running at the time of the inspection. The system is down for repairs. No pressure readings were taken. I discussed the repairs with Greg New and Paul Shaw. The top joint of injection tubing will be replaced and the lined stock tank/injection pump dike will be pumped out and cleaned. A service rig will be coming in next week.
1680717923 2019-2-5 0:00:0 SW No Violations 0.40
1699464840 2006-05-24 Salt Water Injection Well No Violations The system was running at the time of the inspection. There were no violations at the wellhead or at the tank battery.
1699967759 2009-09-02 Salt Water Injection Well No Violations The injection system was not running at the time of the inspection. There were no violations at the wellhead or at the brine tank battery.
1716866321 2010-09-07 Salt Water Injection Well No Violations The injection system was running at the time of the inspection. There were no violations at the wellhead or at the brine tank battery.
1744713566 2015-09-23 Salt Water Injection Well No Violations The injection well and surface facility were inspected. The pump was off, at the time. The chart recorded a larger pressure difference with the pump operating. There were no violations found.
1747174095 2008-09-25 Salt Water Injection Well No Violations The injection system was not running at the time of the inspection. There were no violations at the wellhead or at the brine tank battery.
1757562614 2016-03-08 Salt Water Injection Well No Violations The injection well and surface facility were inspected. There were no violations found at the time.
2051359983 2012-07-25 Salt Water Injection Well No Violations My inspection of the well site and injection facility found no violations. The pump was operating at the time.
2052225348 2014-09-25 Salt Water Injection Well Violations Noted The 1/4 inch valve, on the tubing, was stuck shut. The injection pressure reading was taken from the pressure shut-off switch.
2068766466 2008-12-17 Salt Water Injection Well No Violations The injection system was not running at the time of the inspection. There were no violations at the wellhead or at the brine tank battery.
262740422 2019-12-5 0:00: SW No Violations 1.30
297755979 2007-12-19 0:00 SW No Violations
33981074 2020-7-21 0:00: SW No Violations 0.60
367881384 2005-2-4 0:00:0 SW No Violations
415431848 2007-6-27 0:00: SW No Violations
41781728 2004-9-24 0:00: SW No Violations
509665470 2017-5-9 0:00:0 SW No Violations
611832726 2015-3-31 0:00: SW No Violations
624105809 2010-12-17 0:00 SW No Violations
652468891 2018-3-26 0:00: SW No Violations 3.50
71225919 2018-8-29 0:00: SW No Violations 0.40
76306352 2003-5-22 0:00: SW No Violations
765486711 2008-3-20 0:00: SW No Violations
77752597 2020-6-4 0:00:0 SW No Violations 0.80
796436419 2013-6-25 0:00: SW No Violations
823914431 2019-4-11 0:00: SW No Violations 0.40
879113065 2013-12-27 0:00 SW No Violations
881867059 2018-7-19 0:00: SW No Violations 1.00
892500069 2015-5-29 0:00: SW No Violations
922563185 2018-3-7 0:00:0 SW No Violations 1.50
952903738 2005-11-14 0:00 SW No Violations
UIC1659 1997-5-5 0:00:0 SW No Violations
UIC1660 1997-5-5 0:00:0 SW No Violations
UIC1749 1999-1-29 0:00: SW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0124990549 US-OH-106688 2017-11-21 9-3-07(D) Exceeding maximum allowable injection pressure
2052225348 US-OH-120901 2018-01-13 9-3-05(B)4 Violation of injection tubing/fitting requirements

For data sources see[9]

References