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34-151-22148

Well Details

Well ID: 34-151-22148
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Country: United States
State: Ohio
County: Stark
Municipality: Sandy Township
Operator Name: ENERVEST OPERATING LLC
Well Pad ID:
Farm/Lease Name: RINDCHEN UNIT
License Status: Producing
License Date: 1970-08-13
Spud Date: 1970-08-17
Spud Drilling Contractor:
Final Drill Date: 1970-09-29
Well Total Depth: 5000.00 ft
Configuration: Vertical
Latitude: 40.720000
Longitude: -81.300000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1970-08-13 182 BELDEN & BLAKE CO GeoDate 8/13/70
Original Spud 1970-08-17
Completed 1970-09-29
Reached Total Depth 1970-09-29
Change of Owner 2007-04-27 Operator changed from 182, BELDEN & BLAKE CORPORATION to 7578, ENERVEST OPERATING LLC
Record Last Modified 2019-06-04

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4834 4941 0
4834 4941 0
4834 4941 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 14357 Bbl 66000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 WITCO CORP 373.00 695.00 365
1985 WITCO CORP 925.00 589.00 365
1986 WITCO CORP 919.00 713.00 365
1987 BELDEN & BLAKE CORPORATION 620.00 690.00 365
1988 BELDEN & BLAKE CORPORATION 368.00 508.00 107
1990 BELDEN & BLAKE CORPORATION 966.00 681.00 345
1992 BELDEN & BLAKE CORPORATION 284.00 376.00 329
1993 BELDEN & BLAKE CORPORATION 679.00 330.00 363
1994 BELDEN & BLAKE CORPORATION 793.00 160.00 351
1995 BELDEN & BLAKE CORPORATION 1453.00 172.00 358
1996 BELDEN & BLAKE CORPORATION 632.00 342.00 352
1997 BELDEN & BLAKE CORPORATION 742.00 329.00 358
1998 BELDEN & BLAKE CORPORATION 1265.00 165.00 351
1999 BELDEN & BLAKE CORPORATION 578.00 319.00 335
2000 BELDEN & BLAKE CORPORATION 828.00 404.00 340
2001 BELDEN & BLAKE CORPORATION 1284.00 217.00 365
2002 BELDEN & BLAKE CORPORATION 393.00 560.00 295
2003 BELDEN & BLAKE CORPORATION 604.00 676.00 358
2004 BELDEN & BLAKE CORPORATION 787.00 502.00 366
2005 BELDEN & BLAKE CORPORATION 1040.00 252.00 365
2006 BELDEN & BLAKE CORPORATION 1045.00 313.00 365
2007 ENERVEST OPERATING LLC 962.00 249.00 365
2008 ENERVEST OPERATING LLC 833.00 229.00 365
2009 ENERVEST OPERATING LLC 929.00 181.00 365
2010 ENERVEST OPERATING LLC 891.00 270.00 365
2011 ENERVEST OPERATING LLC 221.00 67.00 0
2012 ENERVEST OPERATING LLC 590.00 184.00 366
2013 ENERVEST OPERATING LLC 632.00 133.00 365
2014 ENERVEST OPERATING LLC 461.00 189.00 365
2015 ENERVEST OPERATING LLC 398.00 168.00 365
2016 ENERVEST OPERATING LLC 401.00 103.00 358
2017 ENERVEST OPERATING LLC 436.00 124.00 365
2018 ENERVEST OPERATING LLC 561.00 129.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 WITCO CORP Brine 0 365
1985 WITCO CORP Brine 250 365
1986 WITCO CORP Brine 560 365
1987 BELDEN & BLAKE CORPORATION Brine 160 365
1988 BELDEN & BLAKE CORPORATION Brine 34 107
1990 BELDEN & BLAKE CORPORATION Brine 6 345
1992 BELDEN & BLAKE CORPORATION Brine 44 329
1993 BELDEN & BLAKE CORPORATION Brine 30 363
1994 BELDEN & BLAKE CORPORATION Brine 0 351
1995 BELDEN & BLAKE CORPORATION Brine 0 358
1996 BELDEN & BLAKE CORPORATION Brine 0 352
1997 BELDEN & BLAKE CORPORATION Brine 0 358
1998 BELDEN & BLAKE CORPORATION Brine 0 351
1999 BELDEN & BLAKE CORPORATION Brine 47 335
2000 BELDEN & BLAKE CORPORATION Brine 147 340
2001 BELDEN & BLAKE CORPORATION Brine 0 365
2002 BELDEN & BLAKE CORPORATION Brine 92 295
2003 BELDEN & BLAKE CORPORATION Brine 246 358
2004 BELDEN & BLAKE CORPORATION Brine 165 366
2005 BELDEN & BLAKE CORPORATION Brine 169 365
2006 BELDEN & BLAKE CORPORATION Brine 189 365
2007 ENERVEST OPERATING LLC Brine 108 365
2008 ENERVEST OPERATING LLC Brine 114 365
2009 ENERVEST OPERATING LLC Brine 59 365
2010 ENERVEST OPERATING LLC Brine 80 365
2011 ENERVEST OPERATING LLC Brine 19
2012 ENERVEST OPERATING LLC Brine 62 366
2013 ENERVEST OPERATING LLC Brine 69 365
2014 ENERVEST OPERATING LLC Brine 132 365
2015 ENERVEST OPERATING LLC Brine 108 365
2016 ENERVEST OPERATING LLC Brine 0 358
2017 ENERVEST OPERATING LLC Brine 62 365
2018 ENERVEST OPERATING LLC Brine 88 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1972679576 2004-6-29 0:00: PW No Violations
-3041072 2015-6-26 0:00: PW No Violations 2.00
-428748797 2015-7-6 0:00:0 PW No Violations 0.50
-692117127 2019-1-10 0:00: PW No Violations 0.60
0003041072 2015-06-26 Production Wells No Violations I was contacted at 9:45am by Troy Wells of Enervest stating that an oil spill had occurred at this wells tank battery. The 210bbl production tank for this well is shared with well #22249 and #22042. A load line runs from the tank to the street where oil haulers can pick up the oil load. The valve on the tank was left open and a leak formed inside the hillside on the load line. Approximately 4bbls of oil leaked from the load line before the flow of oil was stopped. The oil ran into a drainage ditch and eventually an oil sheen made it to Hypocrite Run. A hard boom was installed in the creek to stop the flow of oil in the stream. The location was tested for chlorides with Hach Quantabs and no detectable levels were found. Wade Balser of the OEPA was on scene at 2pm. The hillside near the leak in the flowline was excavated and the ditch dug out and disposed of by Sutton Supply at the Kimble landfill. Terry Whitehair of ODNR witnessed the steam cleaning of the ditch and installation of a siphon dam near the spill. The location was cleaned and prepared for a large rain storm that was coming through in the next 48hours. I will be on location 6-29-2015 to follow up on the spill.
0428748797 2015-07-06 Production Wells No Violations I was on location to follow up to the oil spill that occurred on 6-26-2015. Currently a siphon dam and a dug hole are catching any free product that is seeping out of the hillside or soil. I have requested an Enervest vacuum truck to be on location sucking to remove any residual free product in the siphon dam and the ditch. The hard boom has been removed from Hypocrite Run at the OEPA request. The tank battery has been scraped of contaminated soil and disposed of. There is a leaking valve and brine flowline that I have quested be fixed. The two (2) upright separators that are not in use are going to be steamed and removed from location by Sutton Supply. I have instructed Enervest to monitor the location and removal any free oil that may still be on location. I will follow up on the spill 7-8-2015 to check the progress.
0692117127 2019-01-10 Production Wells No Violations My inspection found the well is equipped with a pumpjack. The well has reported production for 2017. The tank battery consists of two steel production tanks, a horizontal separator, a vertical separator and a meter. There is a domestic gas connection at the tank battery. The tank battery is shared with wells #151-22042, 22249 & 22149. The well is legibly identified. No compliance issues are cited at this time.


0750936483 2015-06-30 Production Wells No Violations I was on location to follow up to the oil spill that occurred on 6-26-2015. The leak has been stopped and the contaminated soil excavated and disposed of at the Kimble landfill by Sutton Supply. Currently a siphon dam and a dug hole are catching any free product that is seeping out of the hillside or soil. I have requested an Enervest vacuum truck to be on location sucking to remove any residual free product in the siphon dam and the ditch. The hard boom is present still in the Hypocrite Run and is collecting any residual sheen on the water. The tank battery has been scraped of contaminated soil and disposed of. I have instructed Enervest to monitor the location and removal any free oil that may still be on location. I will follow up on the spill 7-2-2015 to check the progress.
0991052106 2015-07-14 Production Wells No Violations I was on location to follow up to the oil spill that occurred on 6-26-2015. Currently a siphon dam and a dug hole are catching any free product that is seeping out of the hillside or soil. A small sheen was evident on Hypocrite Run and has been stopped by a boom. The hillside is going to be dug back and any additional oil removed. I have requested an Enervest vacuum truck to be on location sucking to remove any residual free product in the siphon dam and the ditch. There is a leaking valve and brine flowline that I have requested be fixed by Sutton Supply this week.. The two (2) upright separators that were not in use have been steamed and removed from location by Sutton Supply. I have instructed Enervest to monitor the location and removal any free oil that may still be on location. I will follow up on the spill to check the progress.
1087325600 2004-06-15 Production Wells Violations Noted Wellhead needs a legible I.D. sign. Remove the stained soil from around the base of the stock tank and from around the base of the separator.
1797438609 2015-06-29 Production Wells No Violations I was on location to follow up to the oil spill that occurred on 6-26-2015. The leak has been stopped and the contaminated soil excavated and disposed of at the Kimble landfill by Sutton Supply. Currently a siphon dam and a dug hole are catching any free product that is seeping out of the hillside or soil. A Enervest vacuum truck is on location sucking an residual free product in the dam and the ditch. The hard boom is present still in the Hypocrite Run and is collecting any residual sheen on the water. The tank battery has been scraped of contaminated soil and disposed of. I have instructed Enervest to monitor the location and removal any free oil that may still be on location. I will follow up on the spill tomorrow to determine if further cleanup is needed.
1972679576 2004-06-29 Production Wells No Violations N.O.V. has been RESOLVED.
750936483 2015-6-30 0:00: PW No Violations 1.00
991052106 2015-7-14 0:00: PW No Violations 0.50

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1087325600 US-OH-102010 2004-06-15 Well operation causing pollution and contamination
1087325600 US-OH-102011 2004-06-15 Failure to legibly identify well

For data sources see[9]

References