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Well ID: 34-151-21950 | Loading map...
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Country: United States | |
State: Ohio | |
County: Stark | |
Municipality: Osnaburg Township | |
Operator Name: PETROX, INC | |
Well Pad ID: | |
Farm/Lease Name: VAN VOORHIS | |
License Status: Field Inspected: Well Not Found | |
License Date: 1997-10-27 | |
Spud Date: 1968-12-18 | |
Spud Drilling Contractor: | |
Final Drill Date: 1969-02-19 | |
Well Total Depth: 5012.00 ft | |
Configuration: Vertical | |
Latitude: 40.730000 | |
Longitude: -81.270000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1968-10-22 | 182 BELDEN & BLAKE CO GeoDate 10/22/68 |
Original Spud | 1968-12-18 | |
Completed | 1969-02-19 | |
Reached Total Depth | 1969-02-19 | |
Change of Owner | 1997-10-15 | Operator changed from 182, BELDEN & BLAKE CO to 1966, PETROX INC |
APP | 1997-10-27 | Proposed Formations:CLINTON, Issued Date:10/27/97, Expired Date:10/27/98 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Construction Permit Expires | 1998-10-27 | |
Record Last Modified | 2018-07-30 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4851 | 4959 | 22 |
4851 | 4959 | 22 | |
4851 | 4959 | 22 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 15000 Bbl | 20000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | WITCO CORP | 892.00 | 310.00 | 365 |
1985 | WITCO CORP | 1269.00 | 333.00 | 365 |
1986 | WITCO CORP | 1355.00 | 128.00 | 365 |
1987 | BELDEN & BLAKE CORPORATION | 836.00 | 156.00 | 365 |
1988 | BELDEN & BLAKE CORPORATION | 494.00 | 139.00 | 366 |
1990 | BELDEN & BLAKE CORPORATION | 350.00 | 161.00 | 356 |
1992 | BELDEN & BLAKE CORPORATION | 142.00 | 0.00 | 201 |
1993 | BELDEN & BLAKE CORPORATION | 291.00 | 0.00 | 303 |
1994 | BELDEN & BLAKE CORPORATION | 1142.00 | 91.00 | 365 |
1995 | BELDEN & BLAKE CORPORATION | 332.00 | 0.00 | 361 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | WITCO CORP | Brine | 0 | 365 |
1985 | WITCO CORP | Brine | 615 | 365 |
1986 | WITCO CORP | Brine | 240 | 365 |
1987 | BELDEN & BLAKE CORPORATION | Brine | 520 | 365 |
1988 | BELDEN & BLAKE CORPORATION | Brine | 566 | 366 |
1990 | BELDEN & BLAKE CORPORATION | Brine | 433 | 356 |
1992 | BELDEN & BLAKE CORPORATION | Brine | 239 | 201 |
1993 | BELDEN & BLAKE CORPORATION | Brine | 350 | 303 |
1994 | BELDEN & BLAKE CORPORATION | Brine | 331 | 365 |
1995 | BELDEN & BLAKE CORPORATION | Brine | 620 | 361 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
1639563291 | 2017-12-18 | Field Inspected, Well Not Found | No Violations | I did a status check inspection on this well. The record shows this well as producing. I could not visually locate the well or the tank battery. A Plug & Abandon permit was issued on 10/27/1997. I checked the well file and no plugging report was found. I sent an email to Duane Clark (Petrox) on 10/19/2017 and requested his assistance in locating a plug report for this well. He advised me he would look into locating the plug report and get back in touch with me. |
For data sources see[9]