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34-151-21790

Well Details

Well ID: 34-151-21790
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Country: United States
State: Ohio
County: Stark
Municipality: Sandy Township
Operator Name: DIVERSIFIED PRODUCTION LLC
Well Pad ID:
Farm/Lease Name: KING RONALD J
License Status: Producing
License Date: 2002-08-28
Spud Date: 1968-04-16
Spud Drilling Contractor:
Final Drill Date: 1968-05-01
Well Total Depth: 5009.00 ft
Configuration: Vertical
Latitude: 40.720000
Longitude: -81.290000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1968-03-06 1383 OHIO L & M CO INC GeoDate 3/6/68
Original Spud 1968-04-16 GL=1075.4, LOG TYPE=IES
Completed 1968-05-01 GL=1075.4, LOG TYPE=IES
Reached Total Depth 1968-05-01 GL=1075.4, LOG TYPE=IES
CO 1989-10-20 1383 OHIO L & M CO INC GeoDate 10/20/89
Unknown 1989-10-20 Issued Date 10/20/89 Expired Date 10/20/90 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date
APP 2002-08-28 Proposed Formations:CLINTON, Issued Date:8/28/2002, Expired Date:8/28/2003 6:00:00 AM, Drilling unit acres:44, Proposed Well Type:OG, Proposed Well Class:
Construction Permit Expires 2003-08-28 GL=1075.4, LOG TYPE=IES
Change of Owner 2006-07-14 Operator changed from 1383, OHIO L & M CO INC to 6288, ALLIANCE PETROLEUM CORPORATION
Record Last Modified 2019-04-03 GL=1075.4, LOG TYPE=IES

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4854 4924 18
4854 4924 18
4854 4924 18

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1500 Bbl 50000
N2 0 1 Mscf 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2016 ALLIANCE PETROLEUM CORPORATION 0.00 0.00 365
2017 ALLIANCE PETROLEUM CORPORATION 0.00 0.00 365
2018 ALLIANCE PETROLEUM CORPORATION 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2016 ALLIANCE PETROLEUM CORPORATION Brine 0 365
2017 ALLIANCE PETROLEUM CORPORATION Brine 0 365
2018 ALLIANCE PETROLEUM CORPORATION Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-2100684956 2003-10-3 0:00: PW No Violations
0028478988 2002-07-17 Orphan No Violations Received phone call from Denise Kopp (330-484-5226), 5570 Waynesburg Drive S.E., Waynesburg, OH 44688; regarding a old stock tank on her property. Met with Mrs. Kopp and inspected the site. Found a rusted stock tank and flow lines, and an old concrete vault. Unable to locate the wellhead. The well was drilled in 1968. A permit to plug was issued 10-20-89. No plugging report could be found. Additional research will be required to determine responsibility for stock tank.
0031179099 2002-07-23 Production Wells No Violations Conversation with Steve Nicholson (330-866-2424) at L&M. Steve said he will get a permit to plug the well or sell it to a supply company for plugging. Contacted Mrs. Kopp and informed her of the situation. Will mail out N.O.V.
2100684956 2003-10-03 Production Wells No Violations Well was sold to a private land owner (John Neff) for $1.00 for use for house gas. Stock tank was moved. N.O.V HAS BEEN RESOLVED. Steve Nicholson also removed old lines from an old well (L&M was not the owner) that was plugged many years ago and was adjacent to L&Ms tank battery.
28478988 2002-7-17 0:00: OR No Violations 1.50
31179099 2002-7-23 0:00: PW No Violations 0.50

For data sources see[9]

References