X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-151-21217

Well Details

Well ID: 34-151-21217
Loading map...
Country: United States
State: Ohio
County: <County>
Municipality:
Operator Name: G & O RESOURCES LTD
Well Pad ID:
Farm/Lease Name: STARK JOHNSON MARK UNIT
License Status: Producing
License Date: 1967-06-08
Spud Date: 1967-06-14
Spud Drilling Contractor:
Final Drill Date: 1967-08-24
Well Total Depth: 5012.00 ft
Configuration: Vertical
Latitude: 40.780000
Longitude: -81.290000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Unknown 1802-01-01
Original Spud 1967-06-14
Completed 1967-08-24
Reached Total Depth 1967-08-24
CO 1993-07-29 1071 FIDELITY PETROLEUM CORP
CO 1993-07-29 4280 JRD ENERGY GeoDate
Change of Owner 1997-08-04 Operator changed from 4280, JRD ENERGY to 5894, G & O RESOURCES LTD
Record Last Modified 2013-10-03

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4860 4950 0
4860 4950 0
4860 4950 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1400 Bbl 53000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 FIDELITY PETROLEUM CORP 522.00 161.00 0
1987 FIDELITY PETROLEUM CORP 769.00 99.00 180
1988 FIDELITY PETROLEUM CORP 517.00 102.00 180
1989 FIDELITY PETROLEUM CORP 290.00 210.00 180
1990 FIDELITY PETROLEUM CORP 694.00 141.00 180
1991 FIDELITY PETROLEUM CORP 627.00 148.00 180
1992 FIDELITY PETROLEUM CORP 772.00 107.00 120
1993 JRD ENERGY 41.00 0.00 150
1994 JRD ENERGY 294.00 200.00 365
1995 JRD ENERGY 412.00 105.00 365
1996 JRD ENERGY 608.00 106.00 365
1997 JRD ENERGY 352.00 0.00 197
1998 G & O RESOURCES LTD 565.00 58.00 365
1999 G & O RESOURCES LTD 493.00 89.00 360
2000 G & O RESOURCES LTD 451.00 159.00 330
2001 G & O RESOURCES LTD 345.00 128.00 365
2002 G & O RESOURCES LTD 507.00 121.00 365
2003 G & O RESOURCES LTD 321.00 82.00 365
2004 G & O RESOURCES LTD 522.00 79.00 365
2005 G & O RESOURCES LTD 135.00 80.00 365
2006 G & O RESOURCES LTD 117.00 93.00 365
2007 G & O RESOURCES LTD 132.00 31.00 365
2008 G & O RESOURCES LTD 119.00 29.00 366
2009 G & O RESOURCES LTD 96.00 32.00 365
2010 G & O RESOURCES LTD 67.00 0.00 365
2011 G & O RESOURCES LTD 81.00 30.00 365
2012 G & O RESOURCES LTD 0.00 0.00 0
2013 G & O RESOURCES LTD 20.00 18.00 365
2014 G & O RESOURCES LTD 0.00 0.00 0
2015 G & O RESOURCES LTD 0.00 0.00 0
2016 G & O RESOURCES LTD 0.00 47.00 365
2017 G & O RESOURCES LTD 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 FIDELITY PETROLEUM CORP Brine 25 0
1987 FIDELITY PETROLEUM CORP Brine 10 180
1988 FIDELITY PETROLEUM CORP Brine 10 180
1989 FIDELITY PETROLEUM CORP Brine 20 180
1990 FIDELITY PETROLEUM CORP Brine 15 180
1991 FIDELITY PETROLEUM CORP Brine 15 180
1992 FIDELITY PETROLEUM CORP Brine 12 120
1993 JRD ENERGY Brine 79 150
1994 JRD ENERGY Brine 12 365
1995 JRD ENERGY Brine 117 365
1996 JRD ENERGY Brine 71 365
1997 JRD ENERGY Brine 0 197
1998 G & O RESOURCES LTD Brine 297 365
1999 G & O RESOURCES LTD Brine 196 360
2000 G & O RESOURCES LTD Brine 129 330
2001 G & O RESOURCES LTD Brine 127 365
2002 G & O RESOURCES LTD Brine 63 365
2003 G & O RESOURCES LTD Brine 58 365
2004 G & O RESOURCES LTD Brine 30 365
2005 G & O RESOURCES LTD Brine 17 365
2006 G & O RESOURCES LTD Brine 26 365
2007 G & O RESOURCES LTD Brine 0 365
2008 G & O RESOURCES LTD Brine 0 366
2009 G & O RESOURCES LTD Brine 0 365
2010 G & O RESOURCES LTD Brine 0 365
2011 G & O RESOURCES LTD Brine 0 365
2012 G & O RESOURCES LTD Brine 0 0
2013 G & O RESOURCES LTD Brine 39 365
2014 G & O RESOURCES LTD Brine 0 0
2015 G & O RESOURCES LTD Brine 0 0
2016 G & O RESOURCES LTD Brine 0 365
2017 G & O RESOURCES LTD Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1241362836 2009-05-02 Production Wells No Violations I received a message from Columbus Dispatch at 1104 hrs regarding a gas and crude oil leak at 426 High Ave. in East Canton. Osnaburg Township Fire and Rescue, OEPA (Bart Ray 330-418-1288), and G & O Resources, had already been notified. I arrived at the site and met with the contract pumper, Dave Widuck (330-323-6732). The release (less than 2 barrels) was from a flow line leak (40.79062, 81.29435). The release traveled 350 in length in a width ranging from 4 near the tank battery, down the lease road, and in a 2 width along High Ave. The clean up was already in progress when I arrived. I met with Ron Hammen (Lakeside Multi-Service) and requested that all crude oil contaminated soils be removed and disposed. I met with the property owner (Terry Dillinger 330-301-1001), who reported the release to the Osnaburg Township Fire and Rescue and another resident Carolyn Wilson and discussed the release and the remediation. I called Bart Ray and informed him that I would oversee the remediation.
1241450689 2009-05-04 Production Wells No Violations The release has been cleaned up and the flow line has been repaired. All crude oil stained soil has been removed and clean topsoil has been placed and graded. The property owner will seed and mulch the top soiled areas. The complaint has been RESOLVED.

For data sources see[9]

References