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Well ID: 34-151-21152 | Loading map...
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Country: United States | |
State: Ohio | |
County: Stark | |
Municipality: Osnaburg Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: PERFECTION DEVELOPERS INC | |
License Status: Producing | |
License Date: 1967-03-21 | |
Spud Date: 1967-03-25 | |
Spud Drilling Contractor: | |
Final Drill Date: 1967-04-03 | |
Well Total Depth: 5000.00 ft | |
Configuration: Vertical | |
Latitude: 40.780000 | |
Longitude: -81.280000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1967-03-25 | |
Completed | 1967-04-03 | |
Reached Total Depth | 1967-04-03 | |
CO | 1970-08-25 | 9 EDC GeoDate 8/25/70 |
Unknown | 1970-08-25 | Issued Date 8/25/70 Expired Date 8/25/71 Acres 0026730 Tool Type Proposed Formation Proposed Depth 00000 Proposed Drill Depth 00000 |
Change of Owner | 2008-07-21 | Operator changed from 9, POWER GAS MARKETING & TRANS to 1388, EXCO - NORTH COAST ENERGY INC |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
Record Last Modified | 2013-10-03 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4842 | 4844 | 12 |
2006-09-11 | 4857 | 4885 | 12 |
4842 | 4844 | 12 | |
4842 | 4844 | 12 | |
2006-09-11 | 4912 | 4938 | 9 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1500 Bbl | 43000 | |||
Not Treated | 0 | 200 Gal | 0 | MCA |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1191391383 | 2015-2-27 0:00: | PW | No Violations | 2.00 |
-1858979035 | 2015-3-16 0:00: | PW | No Violations | 1.00 |
1191391383 | 2015-02-27 | Production Wells | No Violations | I was on location to perform an inspection on this production well. The tank battery is fenced in and contains a 210bbl production tank with charcoal filter, a poly brine tank and vertical separator. There is a steady drip from the valve on the 210bbl tank leaking brine. The well is a pumpjack well with a considerable amount of paraffin/oil on the wellhead. The well is fenced in. There is no legible identification posted at the tank battery or the wellhead. This well is located in a residential neighborhood and adjacent to a childrens playground. Post proper identification at the well and tank battery, stop the dripping brine and clean any significant spills. |
1533235682 | 2018-08-02 | Production Wells | No Violations | I did a status check inspection for this well. The well is equipped with a pumpjack. The tank battery consists of a steel production tank, a plastic brine tank and a vertical separator. The well is legibly identified. The well and tank battery are fenced in with locked gates. No compliance issues are cited at this time. |
1858979035 | 2015-03-16 | Production Wells | No Violations | I was on location to follow up to ensure identification has been placed on this well and the valve on the 210bbl production tank has been fixed. The valve on the 210bbl tank has been replaced and is no longer leaking. Proper identification has been placed on the tank battery. There are no violations at this time. |
For data sources see[9]