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Well ID: 34-143-20304 | Loading map...
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Country: United States | |
State: Ohio | |
County: Sandusky | |
Municipality: York Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: KEEGAN E UNIT | |
License Status: Lost Hole | |
License Date: 2008-02-11 | |
Spud Date: | |
Spud Drilling Contractor: | |
Final Drill Date: 2008-03-17 | |
Well Total Depth: 67.00 ft | |
Configuration: Vertical | |
Latitude: 41.320000 | |
Longitude: -82.880000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2008-02-11 | Proposed Formations:QUEENSTON THROUGH COPPER RIDGE, Issued Date:2/11/2008, Expired Date:2/10/2009 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:POOL |
Plugged/Abandoned | 2008-03-17 | LOST HOLE WHILE DRILLING SURFACE. SKID TO DRILL #4-A |
Reached Total Depth | 2008-03-17 | LOST HOLE WHILE DRILLING SURFACE. SKID TO DRILL #4-A |
Construction Permit Expires | 2009-02-10 | LOST HOLE WHILE DRILLING SURFACE. SKID TO DRILL #4-A |
Record Last Modified | 2012-06-01 | LOST HOLE WHILE DRILLING SURFACE. SKID TO DRILL #4-A |
For data sources see[2]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2008 | ENERVEST OPERATING LLC | 241.00 | 0.00 | 245 |
2009 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2010 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2011 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2012 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2008 | ENERVEST OPERATING LLC | Brine | 286 | 245 |
2009 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
2010 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
2011 | ENERVEST OPERATING LLC | Brine | 0 | |
2012 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1296337828 | 2015-6-11 0:00: | PW | No Violations | |
-166096703 | 2008-3-13 0:00: | DD | No Violations | |
-1950496313 | 2016-2-10 0:00: | AM | No Violations | |
-2142434368 | 2008-3-11 0:00: | DD | No Violations | |
0166096703 | 2008-03-13 | Drill / Deepen / Reopen | No Violations | Inspect drill site. Drilling has progressed to 75 feet. Loss of circulation fluids at 70 feet. Circulation can be established but as soon as drilling stops the mud is washed away and circulation is lost. In the process of mixing a high viscous mud to attempt to maintain circulation. |
1206475335 | 2008-03-25 | Plug / Plug Back | No Violations | Spoke to Jim Kramer of Enervest on site. He said cement poured in lost hole set up 1-2 feet below ground elevation. He checked with landowner who said that was acceptable. Dirt covers well at this time. Well 308 completed and rig moving to next site. |
1207688088 | 2008-03-17 | Production Wells | No Violations | Operator had to skid rig 50 feet due to lost hole. This area is karst topography and water table is very high. Sandy material on surface collapsed into hole, leaving a water filled pit. Operator ordered 4 yards of grout and poured into hole. Refer to plug report for details. |
1296337828 | 2015-06-11 | Production Wells | No Violations | Identification is posted and no violations are observed at the present time. One hundred barrel storage tank within dike area. |
1950496313 | 2016-02-10 | Administrative Inspection | No Violations | Previous inspection from 06/11/2015 should have been applied to API number 34143203080000 since this well was never completed. |
2142434368 | 2008-03-11 | Drill / Deepen / Reopen | No Violations | Inspect drill location. Rig set up. Hole has not been spudded. Mud pump repairs. |
For data sources see[7]