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Well ID: 34-133-24252 | Loading map...
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Country: United States | |
State: Ohio | |
County: Portage | |
Municipality: Atwater Township | |
Operator Name: PEP DRILLING LLC | |
Well Pad ID: | |
Farm/Lease Name: ABBE | |
License Status: Producing | |
License Date: 2002-12-30 | |
Spud Date: 2002-06-10 | |
Spud Drilling Contractor: PEP DRLG | |
Final Drill Date: 2002-06-22 | |
Well Total Depth: 7500.00 ft | |
Configuration: Vertical | |
Latitude: 41.010000 | |
Longitude: -81.180000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2001-05-02 | 124 MOORE JERRY INC Proposed Formation ROSE RUN Issued Date 5/2/01 Expired Date 5/2/02 6:00:00 AM |
APP | 2002-05-15 | Proposed Formations:ROSE RUN (MAY NOT PRODUCE CLINTON), Issued Date:5/15/2002, Expired Date:5/15/2003 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:POOL |
Original Spud | 2002-06-10 | |
Completed | 2002-06-22 | |
Plugged Back | 2002-06-22 | |
Reached Total Depth | 2002-06-22 | |
Change of Owner | 2002-07-05 | Operator changed from 124, MOORE JERRY INC to 1198, PIPES PURSIE E |
APP | 2002-12-30 | Proposed Formations:ROSE RUN, Issued Date:12/30/2002, Expired Date:12/30/2003 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:POOL |
Completion Report Received | 2003-11-12 | |
Construction Permit Expires | 2003-12-30 | |
Change of Owner | 2016-03-04 | Operator changed from 1198, PIPES PURSIE E to 9640, PEP DRILLING LLC |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2003-12-30 | 7387 | 7439 | 0 |
7387 | 7439 | 0 | |
7387 | 7439 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 15 | 2150 Bbl | 20000 | 1000 GALLONS HCL ACID |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2003 | PIPES PURSIE E | 1864.00 | 535.00 | 106 |
2004 | PIPES PURSIE E | 11008.00 | 5629.00 | 365 |
2005 | PIPES PURSIE E | 10081.00 | 4537.00 | 365 |
2006 | PIPES PURSIE E | 7581.00 | 4353.00 | 365 |
2007 | PIPES PURSIE E | 5133.00 | 3524.00 | 365 |
2008 | PIPES PURSIE E | 5186.00 | 3562.00 | 365 |
2009 | PIPES PURSIE E | 5420.00 | 3044.00 | 365 |
2010 | PIPES PURSIE E | 6559.00 | 2829.00 | 365 |
2011 | PIPES PURSIE E | 5719.00 | 2238.00 | 365 |
2012 | PIPES PURSIE E | 7915.00 | 2084.00 | 366 |
2013 | PIPES PURSIE E | 8129.00 | 2101.00 | 365 |
2016 | PEP DRILLING LLC | 2627.00 | 1177.00 | 365 |
2017 | PEP DRILLING LLC | 3972.00 | 675.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2003 | PIPES PURSIE E | Brine | 3505 | 106 |
2004 | PIPES PURSIE E | Brine | 5605 | 365 |
2005 | PIPES PURSIE E | Brine | 3535 | 365 |
2006 | PIPES PURSIE E | Brine | 3080 | 365 |
2007 | PIPES PURSIE E | Brine | 3100 | 365 |
2008 | PIPES PURSIE E | Brine | 2699 | 365 |
2009 | PIPES PURSIE E | Brine | 2375 | 365 |
2010 | PIPES PURSIE E | Brine | 1775 | 365 |
2011 | PIPES PURSIE E | Brine | 1780 | 365 |
2012 | PIPES PURSIE E | Brine | 1655 | 366 |
2013 | PIPES PURSIE E | Brine | 2115 | 365 |
2016 | PEP DRILLING LLC | Brine | 0 | 365 |
2017 | PEP DRILLING LLC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-115356680 | 2013-7-26 0:00: | PW | No Violations | |
-1308733964 | 2003-6-25 0:00: | DD | No Violations | |
-160576163 | 2013-9-25 0:00: | PL | No Violations | |
-1944042368 | 2015-9-2 0:00:0 | PW | No Violations | 0.50 |
0021579168 | 2002-06-18 | Drill / Deepen / Reopen | No Violations | Drilling at 5630; Pits and liners are intact; NO VIOLATIONS. |
0023479213 | 2002-06-24 | Plug / Plug Back | No Violations | Dry hole. Well was P&A using PEPs Drilling Rig on 6-22-02. Rig was rigging down to move to Ashtabula Co. Pits and liners were intact. NO VIOLATIONS. |
0026379219 | 2002-07-02 | Final Restoration | No Violations | Random inspection of site. Well was P&A with drilling rig on 6-22-02. Pits are still open and 8-5/8 csg. needs to be cut off below ground level. |
0115356680 | 2013-07-26 | Production Wells | No Violations | My final restoration inspection showed that this permit number is a producing well. The well ID card photographed (#4 RR) suggests that this well was deep-plugged and is now a Rose Run well. A review of the records revealed that the well was PLUGGED AS DRY IN JUNE, 2002. REOPENED FOR PRODUCTION IN JUNE, 2003. Also photographed are an old separator, line and additional material left on site. Final restoration inspection not necessary and the status needs to be amended to PR. |
0160576163 | 2013-09-25 | Preliminary Restoration | No Violations | This well was listed as plugged and abandoned in RBDMS and required Final Restoration approval. I reviewed the well files and found that this well was plugged as a dry hole in June of 2002 and reopened in June 2003 and has been reporting production since. My inspection found this Rose Run well operating with the aid of a pumping unit. The tank battery was diked and contained 3-210 barrel tanks and a horizontal separator. There was an old separator sitting on location. I e-mailed Steve Opritza about the discrepency and he has changed the status to producing in RBDMS. This well now requires preliminary restoration approval. Preliminary restoration is approved. I will talk to PEP about the old separator on location. No violations. |
0465319308 | 2015-10-26 | UrbanProduction Wells | No Violations | Follow-up to an inspection conducted on 9-2-15. The concrete pad of the pumping unit that was coated in motor oil has been steam cleaned. The affected soil behind the unit has been removed and a containment dike has been constructed around the pumping unit. The issues I found previously have been resolved. No violations. |
0824193461 | 2003-12-24 | Production Wells | No Violations | Status check inspection - no violations at this time. |
1308733964 | 2003-06-25 | Drill / Deepen / Reopen | No Violations | Reopening plugged well. Reaming at 450. |
1944042368 | 2015-09-02 | Production Wells | No Violations | I inspected this Rose Run well while following up on Complaint #5108 concerning the Abbe #3 (PN#24247). The landowner, Mr. Plymale, had mentioned that oil was also leaking from the pumping unit motor on this well when I spoke to him earlier in the day. My inspection found the well equipped and producing with the aid of a natural gas-powered pumping unit with 130psi on the 2.875 tubing and 100psi on the 4.5 production casing. The unit is spotted on a concrete pad and the rear of the pad (8 X 5) from below the motor to the north corner of the concrete is stained with motor oil. The oil has migrated and stained the ground off the north corner of the pad for 10. The pumper, Steven Pero, arrived on location to change the meter chart and I spoke with him about the issues I found at the pumping unit. He told me that he would get a contractor in to steam clean the pad and remove the affected soil. I instructed him to either use pads to catch the motor oil where it is leaking and replace them as necessary or use a bucket to collect the leaking oil and empty it as needed. I will follow-up in thirty days and issue a compliance notice if the remedial and recommended actions are not taken and implemented. |
21579168 | 2002-6-18 0:00: | DD | No Violations | 1.00 |
23479213 | 2002-6-24 0:00: | PB | No Violations | 0.50 |
26379219 | 2002-7-2 0:00:0 | FR | No Violations | 1.00 |
465319308 | 2015-10-26 0:00 | UP | No Violations | 0.50 |
824193461 | 2003-12-24 0:00 | PW | No Violations |
For data sources see[9]